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34-067-20525

Well Details

Well ID: 34-067-20525
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Country: United States
State: Ohio
County: Harrison
Municipality: Washington Township
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL
Well Pad ID:
Farm/Lease Name: DUNLAP PHILLIP & NEAL
License Status: Producing
License Date: 1982-03-12
Spud Date: 1982-03-16
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1982-03-19
Well Total Depth: 6276.00 ft
Configuration: Vertical
Latitude: 40.230000
Longitude: -81.230000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-03-12 Issued Date 3/15/82 Expired Date 9/11/82 Acres 0279830 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06276 Proposed Drill Depth 06276
Original Spud 1982-03-15
Completed 1982-03-19
Reached Total Depth 1982-03-19
CO 1982-04-19 168 RED HILL DEVELOPMENT GeoDate 3/12/82
Construction Permit Expires 1982-09-11
Completion Report Received 1984-01-30
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 6065 6180 0
6065 6180 0
2006-09-11 6086 6142 6
6086 6142 6
6065 6180 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 67880 Gal 0 FRAC: WATER

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RHDK OIL & GAS LLC/DBA RED HIL 11226.00 0.00 0
1985 RHDK OIL & GAS LLC/DBA RED HIL 7345.00 109.00 365
1986 RHDK OIL & GAS LLC/DBA RED HIL 12177.00 0.00 365
1987 RHDK OIL & GAS LLC/DBA RED HIL 11134.00 0.00 365
1988 RHDK OIL & GAS LLC/DBA RED HIL 11088.00 0.00 365
1989 RHDK OIL & GAS LLC/DBA RED HIL 9616.00 103.00 365
1990 RHDK OIL & GAS LLC/DBA RED HIL 8802.00 0.00 365
1991 RHDK OIL & GAS LLC/DBA RED HIL 7634.00 0.00 365
1992 RHDK OIL & GAS LLC/DBA RED HIL 7294.00 0.00 365
1993 RHDK OIL & GAS LLC/DBA RED HIL 6585.00 0.00 365
1994 RHDK OIL & GAS LLC/DBA RED HIL 6074.00 0.00 365
1995 RHDK OIL & GAS LLC/DBA RED HIL 5498.00 0.00 365
1996 RHDK OIL & GAS LLC/DBA RED HIL 5594.00 0.00 365
1997 RHDK OIL & GAS LLC/DBA RED HIL 2862.00 69.00 365
1998 RHDK OIL & GAS LLC/DBA RED HIL 2740.00 0.00 365
1999 RHDK OIL & GAS LLC/DBA RED HIL 4146.00 0.00 365
2000 RHDK OIL & GAS LLC/DBA RED HIL 4016.00 0.00 365
2001 RHDK OIL & GAS LLC/DBA RED HIL 3811.00 0.00 365
2002 RHDK OIL & GAS LLC/DBA RED HIL 3692.00 0.00 365
2003 RHDK OIL & GAS LLC/DBA RED HIL 3284.00 0.00 365
2004 RHDK OIL & GAS LLC/DBA RED HIL 4101.00 0.00 365
2005 RHDK OIL & GAS LLC/DBA RED HIL 4386.00 0.00 365
2006 RHDK OIL & GAS LLC/DBA RED HIL 4746.00 76.00 365
2007 RHDK OIL & GAS LLC/DBA RED HIL 5746.00 0.00 365
2008 RHDK OIL & GAS LLC/DBA RED HIL 5273.00 0.00 365
2009 RHDK OIL & GAS LLC/DBA RED HIL 3169.00 0.00 365
2010 RHDK OIL & GAS LLC/DBA RED HIL 3064.00 0.00 365
2011 RHDK OIL & GAS LLC/DBA RED HIL 2671.00 62.00 365
2012 RHDK OIL & GAS LLC/DBA RED HIL 3641.00 0.00 366
2013 RHDK OIL & GAS LLC/DBA RED HIL 5891.00 0.00 365
2014 RHDK OIL & GAS LLC/DBA RED HIL 8979.00 0.00 365
2015 RHDK OIL & GAS LLC/DBA RED HIL 5707.00 26.00 365
2016 RHDK OIL & GAS LLC/DBA RED HIL 1871.00 0.00 365
2017 RHDK OIL & GAS LLC/DBA RED HIL 3251.00 0.00 365
2018 RHDK OIL & GAS LLC/DBA RED HIL 3313.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 0
1985 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1986 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1987 RHDK OIL & GAS LLC/DBA RED HIL Brine 240 365
1988 RHDK OIL & GAS LLC/DBA RED HIL Brine 160 365
1989 RHDK OIL & GAS LLC/DBA RED HIL Brine 40 365
1990 RHDK OIL & GAS LLC/DBA RED HIL Brine 90 365
1991 RHDK OIL & GAS LLC/DBA RED HIL Brine 180 365
1992 RHDK OIL & GAS LLC/DBA RED HIL Brine 90 365
1993 RHDK OIL & GAS LLC/DBA RED HIL Brine 95 365
1994 RHDK OIL & GAS LLC/DBA RED HIL Brine 40 365
1995 RHDK OIL & GAS LLC/DBA RED HIL Brine 80 365
1996 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1997 RHDK OIL & GAS LLC/DBA RED HIL Brine 315 365
1998 RHDK OIL & GAS LLC/DBA RED HIL Brine 175 365
1999 RHDK OIL & GAS LLC/DBA RED HIL Brine 80 365
2000 RHDK OIL & GAS LLC/DBA RED HIL Brine 95 365
2001 RHDK OIL & GAS LLC/DBA RED HIL Brine 176 365
2002 RHDK OIL & GAS LLC/DBA RED HIL Brine 96 365
2003 RHDK OIL & GAS LLC/DBA RED HIL Brine 70 365
2004 RHDK OIL & GAS LLC/DBA RED HIL Brine 56 365
2005 RHDK OIL & GAS LLC/DBA RED HIL Brine 34 365
2006 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2007 RHDK OIL & GAS LLC/DBA RED HIL Brine 91 365
2008 RHDK OIL & GAS LLC/DBA RED HIL Brine 96 365
2009 RHDK OIL & GAS LLC/DBA RED HIL Brine 82 365
2010 RHDK OIL & GAS LLC/DBA RED HIL Brine 76 365
2011 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2012 RHDK OIL & GAS LLC/DBA RED HIL Brine 60 366
2013 RHDK OIL & GAS LLC/DBA RED HIL Brine 34 365
2014 RHDK OIL & GAS LLC/DBA RED HIL Brine 39 365
2015 RHDK OIL & GAS LLC/DBA RED HIL Brine 106 365
2016 RHDK OIL & GAS LLC/DBA RED HIL Brine 49 365
2017 RHDK OIL & GAS LLC/DBA RED HIL Brine 114 365
2018 RHDK OIL & GAS LLC/DBA RED HIL Brine 274 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1747379136 2006-3-22 0:00: PW No Violations 1.00
0093377304 2006-02-24 Production Wells Violations Noted Inspection revealed that there are several small leaks in the oil storage tank app. 2/3 of the way up the tank . The biggest hole has a stick stuck in it to try to prevent it from leaking . The other spots look like rust bubbles and they are leaking (weeping) oil . There is pollution and contamination inside the tank battery SPCC dike ; less than 5 gallons of free oil . The rest of the pollution and contamination is black stained stone and dirt inside the dike . The tank battery consists of one 210 bbl oil storage tank .
1347757565 2020-3-17 0:00: PW No Violations 1.00
1501165314 2017-07-27 Production Wells No Violations On the day of my inspection I found this plunger lift well equipped with a motor valve, 4.5 inch diameter casing, and 2.375 inch diameter tubing. Domestic meter off of the 4.5 inch diameter casing. Production equipment includes a 100 barrel steel production tank, a horziontal seperator with meter box and a 1 inch diameter sales line orfice, all contained in an earthened dike. Tank is identified and production is current in RBDMS. Well is shut in on tubing and partially open on casing.
1747379136 2006-03-22 Production Wells No Violations Follow-up inspection revealed that the leaking oil storage tank has been removed and replaced with a new 100 bbl oil storage tank . The pollution and contamination inside the tank battery SPCC dike has been cleaned up and new stone placed inside the dike . The SPCC dike has been reconstructed to meet the SPCC requirements . All violations have been corrected at this time . Case RESOLVED at this time .
93377304 2006-2-24 0:00: PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0093377304 US-OH-130678 2006-03-06 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[9]

References