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34-067-20381

Well Details

Well ID: 34-067-20381
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Country: United States
State: Ohio
County: Harrison
Municipality: Washington Township
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL
Well Pad ID:
Farm/Lease Name: SCHLINGER NORMAN
License Status: Producing
License Date: 1980-05-16
Spud Date: 1980-05-30
Spud Drilling Contractor:
Final Drill Date: 1980-06-04
Well Total Depth: 6140.00 ft
Configuration: Vertical
Latitude: 40.300000
Longitude: -81.220000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-05-16 168 RED HILL DEVELOPMENT GeoDate 5/16/80
Original Spud 1980-05-30
Completed 1980-06-04
Reached Total Depth 1980-06-04
Record Last Modified 2019-06-04

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5958 5965 6
2006-09-11 5978 5995 0
5958 5965 6
5958 5965 6
2006-09-11 6025 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 180 Mscf 0
H2O 0 87000 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RHDK OIL & GAS LLC/DBA RED HIL 3765.00 127.00 0
1985 RHDK OIL & GAS LLC/DBA RED HIL 5425.00 0.00 365
1986 RHDK OIL & GAS LLC/DBA RED HIL 2155.00 118.00 365
1987 RHDK OIL & GAS LLC/DBA RED HIL 4028.00 0.00 365
1988 RHDK OIL & GAS LLC/DBA RED HIL 2765.00 102.00 365
1989 RHDK OIL & GAS LLC/DBA RED HIL 2085.00 0.00 365
1990 RHDK OIL & GAS LLC/DBA RED HIL 1918.00 128.00 365
1991 RHDK OIL & GAS LLC/DBA RED HIL 1179.00 0.00 365
1992 RHDK OIL & GAS LLC/DBA RED HIL 1486.00 96.00 365
1993 RHDK OIL & GAS LLC/DBA RED HIL 2055.00 0.00 365
1994 RHDK OIL & GAS LLC/DBA RED HIL 1525.00 0.00 365
1995 RHDK OIL & GAS LLC/DBA RED HIL 1708.00 115.00 365
1996 RHDK OIL & GAS LLC/DBA RED HIL 1026.00 0.00 365
1997 RHDK OIL & GAS LLC/DBA RED HIL 692.00 68.00 365
1998 RHDK OIL & GAS LLC/DBA RED HIL 1165.00 0.00 365
1999 RHDK OIL & GAS LLC/DBA RED HIL 1252.00 0.00 365
2000 RHDK OIL & GAS LLC/DBA RED HIL 725.00 0.00 365
2001 RHDK OIL & GAS LLC/DBA RED HIL 2044.00 148.00 365
2002 RHDK OIL & GAS LLC/DBA RED HIL 2295.00 0.00 365
2003 RHDK OIL & GAS LLC/DBA RED HIL 1905.00 105.00 365
2004 RHDK OIL & GAS LLC/DBA RED HIL 2425.00 0.00 365
2005 RHDK OIL & GAS LLC/DBA RED HIL 1837.00 0.00 365
2006 RHDK OIL & GAS LLC/DBA RED HIL 1599.00 65.00 365
2007 RHDK OIL & GAS LLC/DBA RED HIL 1326.00 64.00 365
2008 RHDK OIL & GAS LLC/DBA RED HIL 1422.00 31.00 365
2009 RHDK OIL & GAS LLC/DBA RED HIL 1344.00 0.00 365
2010 RHDK OIL & GAS LLC/DBA RED HIL 1368.00 95.00 365
2011 RHDK OIL & GAS LLC/DBA RED HIL 1391.00 0.00 365
2012 RHDK OIL & GAS LLC/DBA RED HIL 2522.00 0.00 366
2013 RHDK OIL & GAS LLC/DBA RED HIL 1951.00 60.00 365
2014 RHDK OIL & GAS LLC/DBA RED HIL 1640.00 46.00 365
2015 RHDK OIL & GAS LLC/DBA RED HIL 1217.00 0.00 365
2016 RHDK OIL & GAS LLC/DBA RED HIL 1271.00 0.00 365
2017 RHDK OIL & GAS LLC/DBA RED HIL 712.00 0.00 365
2018 RHDK OIL & GAS LLC/DBA RED HIL 1162.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 0
1985 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1986 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1987 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1988 RHDK OIL & GAS LLC/DBA RED HIL Brine 50 365
1989 RHDK OIL & GAS LLC/DBA RED HIL Brine 40 365
1990 RHDK OIL & GAS LLC/DBA RED HIL Brine 25 365
1991 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1992 RHDK OIL & GAS LLC/DBA RED HIL Brine 55 365
1993 RHDK OIL & GAS LLC/DBA RED HIL Brine 50 365
1994 RHDK OIL & GAS LLC/DBA RED HIL Brine 70 365
1995 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1996 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1997 RHDK OIL & GAS LLC/DBA RED HIL Brine 30 365
1998 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1999 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2000 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2001 RHDK OIL & GAS LLC/DBA RED HIL Brine 138 365
2002 RHDK OIL & GAS LLC/DBA RED HIL Brine 100 365
2003 RHDK OIL & GAS LLC/DBA RED HIL Brine 77 365
2004 RHDK OIL & GAS LLC/DBA RED HIL Brine 90 365
2005 RHDK OIL & GAS LLC/DBA RED HIL Brine 65 365
2006 RHDK OIL & GAS LLC/DBA RED HIL Brine 5 365
2007 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2008 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2009 RHDK OIL & GAS LLC/DBA RED HIL Brine 65 365
2010 RHDK OIL & GAS LLC/DBA RED HIL Brine 51 365
2011 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2012 RHDK OIL & GAS LLC/DBA RED HIL Brine 70 366
2013 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2014 RHDK OIL & GAS LLC/DBA RED HIL Brine 206 365
2015 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2016 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2017 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2018 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1697574161 2014-3-31 0:00: PW No Violations 1.00
-2060555037 2017-10-3 0:00: PW No Violations 1.00
-521221898 2014-3-25 0:00: CS No Violations 7.00
0380795139 2014-03-25 Casing String Witnessed No Violations RHD has casing 10 ft above the backed off joint looking up in the well. There is 10 ft of fill and they are mudding up and washing over the casing. Most likely will cement Weds.
0502181014 2014-03-18 Production Wells No Violations Check on the status of the service rig and found nobody of site. Return later and found that they will pull the 4-1/2 inch diameter casing and run another casing string back. The casing will be cemented to surface to make repairs.
0521221898 2014-03-25 Casing String Witnessed No Violations I am on site today to witness the cementing of the 4.5 inch casing string. RHD has replaced the casing down to 4400 ft and has a DV Cementing tool at that depth. The ball has been dropped and the casing has circulated to surface. Universal Well Cementing was to be on site at 4:30 and has multiple vehicles lost. They did arrive 3.5 hours later to cement casing with class A lite cement 455 sacks of lead cement with a yield of 2.27 and tail cement of 265 sacks of 50-50 Poz cement with a yield of 1.28 . Had 10 bbls of good cement returns.
1485028365 2014-03-24 Production Wells No Violations I arrived today to check on the status of the service rig which is pulling the 4.5 inch casing and running new casing back in its place. Today they are in the process of mudding up the hole to condition it before cementing.
1697574161 2014-03-31 Production Wells No Violations The service rig is still over the well and nobody is around today? I am checking because the rig should be done with the repairs.
2060555037 2017-10-03 Production Wells No Violations On the day of my inspection I found this plunger lift well equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and a motor valve. Production equipment includes a horizontal seperator, meter box with 1.0 inch diameter sales line orfice, and a 140 barrel steel tank, all contained in an earthen dike. Production records are current and chart indicates well is producing. Tank is labeled.
380795139 2014-3-25 0:00: CS No Violations 1.00
502181014 2014-3-18 0:00: PW No Violations 2.00

For data sources see[9]

References