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Well ID: 34-059-24370 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Londonderry Township | |
Operator Name: ASCENT RESOURCES UTICA LLC | |
Well Pad ID: US-OH-000908 | |
Farm/Lease Name: RED HILL FARM MDS GR | |
License Status: Producing | |
License Date: 2014-05-07 | |
Spud Date: 2014-06-27 | |
Spud Drilling Contractor: NOMAC DRILLING CORP | |
Final Drill Date: 2014-12-02 | |
Well Total Depth: 16027.00 ft | |
Configuration: Horizontal | |
Latitude: 40.120000 | |
Longitude: -81.340000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2014-05-07 | Proposed Formations:POINT PLEASANT, Issued Date:5/7/2014, Expired Date:5/6/2016 12:00:00 PM, Drilling unit acres:639.87, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2014-12-02 | |
Correction to Well | 2015-01-09 | CHANGE IN TARGET AND TAKE-POINT INFORMATION (FOOTAGES AND COORDINATES) FROM AS DRILLED SURVEY PLAT. UPDATE TO UNIT SIZE (638.922 ACRES). |
Change of Owner | 2015-08-19 | Operator changed from 9193, AMERICAN ENERGY UTICA LLC to 9520, ASCENT RESOURCES UTICA LLC |
Completion Report Received | 2015-09-28 | |
Construction Permit Expires | 2016-05-06 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 06/12/2015 | 06/30/2015 | 7301 | 12,791,400.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | FE-200L | FTSI | Iron Control | Iminodiacetate disodium salt | 17593-73-6 | 0.2 | 0.00001469 | 17.85 |
Sodium glycolate | 2836-32-0 | 1.5 | 0.000110181 | 133.9 | ||||
Tetrasodium EDTA | 64-02-8 | 41 | 0.00301161 | 3659.87 | ||||
Trisodium Nitrilotriacetic acid | 5064-31-3 | 2 | 0.000146908 | 178.53 | ||||
Sodium Hydroxide | 1310-73-2 | 2 | 0.000146908 | 178.53 | ||||
Water | 7732-18-5 | 60 | 0.00440723 | 5355.9 | ||||
Ethylenediaminetriaceticacid, trisodium salt | 19019-43-3 | 0.8 | 0.00005876 | 71.41 | ||||
Sodium formate | 141-53-7 | 0.6 | 0.00004407 | 53.56 | ||||
NE-100W | FTSI | Non-emulsifier | 2-Propanol | 67-63-0 | 10 | 0.00008694 | 105.65 | |
Water | 7732-18-5 | 80 | 0.0006955 | 845.21 | ||||
Sulfuric Acid | 7664-93-9 | 0.01 | 0.00000012 | 0.15 | ||||
Benzene, C10-16 Alkyl Derivatives | 68648-87-3 | 0.04 | 0.00000037 | 0.44 | ||||
2-Butoxyethanol | 111-76-2 | 10 | 0.00008694 | 105.65 | ||||
Sulfur Dioxide | 7446-09-5 | 0 | 0.00000001 | 0.01 | ||||
Methanol | 67-56-1 | 15 | 0.000130406 | 158.48 | ||||
Dodecylbenzenesulfonic acid | 27176-87-0 | 5 | 0.00004347 | 52.83 | ||||
Unsulphonated Matter | Proprietary | 0.03 | 0.00000024 | 0.3 | ||||
30/50 White | FTSI | proppant | Silica, Quartz | 14808-60-7 | 100 | 9.05168 | 11,000,100.0 | |
LTB-1 | FTSI | Breaker | Ammonium Persulfate | 7727-54-0 | 100 | 0.00041802 | 508 | |
Cured acrylic resin | Proprietary | 100 | 0.00041802 | 508 | ||||
Silica, Crystalline- Quartz | 14808-60-7 | 10 | 0.00004180 | 50.8 | ||||
Proprietary | Proprietary | 0 | 0 | 0 | ||||
100 Mesh Sand | FTSI | proppant | Silica, Quartz | 14808-60-7 | 100 | 1.74692 | 2,122,950.0 | |
Water | Operator | Carrier | Water | 7732-18-5 | 100 | 87.7845 | 106,680,000.0 | |
APB-1 | FTSI | Gel breaker | Ammonium Persulfate | 7727-54-0 | 100 | 0.00041802 | 508 | |
CS-250 SI | FTSI | Scale Inhibitor | Water | 7732-18-5 | 81 | 0.0189358 | 23011.8 | |
Sodium Polyacrylate | 9003-04-7 | 10 | 0.00233775 | 2840.96 | ||||
Ethylene glycol | 107-21-1 | 10 | 0.00233775 | 2840.96 | ||||
Sodium chloride | 7647-14-5 | 6 | 0.00140265 | 1704.58 | ||||
NE-100 | FTSI | Non-emulsifier | 2-Butoxyethanol | 111-76-2 | 10 | 0.00399932 | 4860.18 | |
Dodecylbenzenesulfonic acid | 27176-87-0 | 5 | 0.00199966 | 2430.09 | ||||
2-Propanol | 67-63-0 | 10 | 0.00399932 | 4860.18 | ||||
Sulfur Dioxide | 7446-09-5 | 0 | 0.00000056 | 0.68 | ||||
Unsulphonated Matter | Proprietary | 0.03 | 0.00001120 | 13.61 | ||||
Sulfuric Acid | 7664-93-9 | 0.01 | 0.00000560 | 6.8 | ||||
Benzene, C10-16 Alkyl Derivatives | 68648-87-3 | 0.04 | 0.00001680 | 20.41 | ||||
Water | 7732-18-5 | 90 | 0.0359939 | 43741.7 | ||||
Hydrochloric Acid (HCl) | FTSI | Acid | Water | 7732-18-5 | 63 | 0.794646 | 965696 | |
Hydrogen Chloride | 7647-01-0 | 37 | 0.466697 | 567155 | ||||
CI-150 | FTSI | Acid Corrosion Inhibitor | Organic amine resin salt | Proprietary | 30 | 0.000334005 | 405.9 | |
Dimethylformamide | 68-12-2 | 10 | 0.000111335 | 135.3 | ||||
Fatty Acid Salt | Proprietary | 0.1 | 0.00000111 | 1.35 | ||||
Quaternary ammonium compound | Proprietary | 10 | 0.000111335 | 135.3 | ||||
Isopropanol | 67-63-0 | 30 | 0.000334005 | 405.9 | ||||
Aliphatic alcohol | Proprietary | 0.1 | 0.00000111 | 1.35 | ||||
Fatty Acid | Proprietary | 0.1 | 0.00000111 | 1.35 | ||||
Alkylene Oxide Block Polymer | Proprietary | 10 | 0.000111335 | 135.3 | ||||
Water | 7732-18-5 | 5 | 0.00005567 | 67.65 | ||||
Ethylene Glycol | 107-21-1 | 30 | 0.000334005 | 405.9 | ||||
Diethylene glycol | 111-46-6 | 1 | 0.00001113 | 13.53 | ||||
Aromatic aldehyde | Proprietary | 10 | 0.000111335 | 135.3 | ||||
FRW-200 | FTSI | Friction reducer | Dewaxed heavy paraffinic | 64742-65-0 | 1.5 | 0.000835554 | 1015.41 | |
Acrylamide | 79-06-1 | 0.1 | 0.00005570 | 67.69 | ||||
Copolymer of acrylamide and sodium acrylate | 25987-30-8 | 33 | 0.0183822 | 22339 | ||||
Hydrotreated heavy paraffinic | 64742-54-7 | 5 | 0.00278518 | 3384.69 | ||||
Isopropanol | 67-63-0 | 0.3 | 0.000167111 | 203.08 | ||||
Surfactant | Proprietary | 7 | 0.00389925 | 4738.57 | ||||
Acrylamide P/W acrylic acid, ammonium salt | 26100-47-0 | 25 | 0.0139259 | 16923.5 | ||||
Ammonium Chloride | 12125-02-9 | 12 | 0.00668443 | 8123.27 | ||||
Ammonium Acrylate | 10604-69-0 | 0.5 | 0.000278518 | 338.47 | ||||
Water | 7732-18-5 | 48 | 0.0267377 | 32493.1 | ||||
Alcohols (C12-C14), ethoxylated | 68439-50-9 | 4 | 0.00222814 | 2707.76 | ||||
Alcohols (C12-C16), ethoxylated | 68551-12-2 | 4 | 0.00222814 | 2707.76 | ||||
Sorbitol Tetraoleate | 61723-83-9 | 2 | 0.00111407 | 1353.88 | ||||
Petroleum distillate hydrotreated light | 64742-47-8 | 26 | 0.0144829 | 17600.4 | ||||
Alkyloxypolyethyleneoxyethanol | 84133-50-6 | 1 | 0.000557036 | 676.94 | ||||
Sorbitan Monooleate | 1338-43-8 | 3 | 0.00167111 | 2030.82 | ||||
Alcohols (C10-C16), ethoxylated | 68002-97-1 | 4 | 0.00222814 | 2707.76 | ||||
Polyethylene glycol monooleate | 9004-96-0 | 3 | 0.00167111 | 2030.82 | ||||
FRW-900 | FTSI | Friction Reducer | Anionic polymer | 25085-02-3 | 40 | 0.000723616 | 879.38 | |
Oxyalkylated alcohol A | Proprietary | 5 | 0.00009045 | 109.92 | ||||
Sorbitan, mono-(9Z)-9-octadecenoate | 1338-43-8 | 5 | 0.00009045 | 109.92 | ||||
Hydrotreated Light Distillate | 64742-47-8 | 30 | 0.000542712 | 659.53 | ||||
Sodium chloride (NaCl) | 7647-14-5 | 5 | 0.00009045 | 109.92 | ||||
Alkyl Alcohol | Proprietary | 10 | 0.000180904 | 219.84 | ||||
Water | 7732-18-5 | 40 | 0.000723616 | 879.38 | ||||
ICI-3240 | FTSI | Biocide | Dazomet (Tetrahydro-3, 5-dimethyl-2H-1,
3, 5-thiadiazine-2-thione. |
533-74-4 | 24 | 0.00589114 | 7159.22 | |
Water | 7732-18-5 | 55 | 0.0135005 | 16406.5 | ||||
Sodium Hydroxide | 1310-73-2 | 23 | 0.00564568 | 6860.92 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2015-06-15 | H2O | 0 | 6174 Bbl | 250626 | Frac Tech Services | 30 total perforations from 14616 feet to 14495 feet
39041lbs of 100 mesh white 21178lbs of 30/50 white |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ASCENT RESOURCES UTICA LLC | 274640 | 108202 | 158 |
2016 | ASCENT RESOURCES UTICA LLC | 467031 | 115263 | 366 |
2017 | ASCENT RESOURCES UTICA LLC | 307132 | 44683 | 365 |
2018 | ASCENT RESOURCES UTICA LLC | 116043 | 13835 | 187 |
2019 | ASCENT RESOURCES UTICA LLC | 56 | 0 | 2 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ASCENT RESOURCES UTICA LLC | Brine | 9936 | 158 |
2016 | ASCENT RESOURCES UTICA LLC | Brine | 11059 | 366 |
2017 | ASCENT RESOURCES UTICA LLC | Brine | 6887 | 365 |
2018 | ASCENT RESOURCES UTICA LLC | Brine | 2358 | 187 |
2019 | ASCENT RESOURCES UTICA LLC | Brine | 2 | 2 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1006905922 | 2020-6-22 0:00: | PW | No Violations | 1.00 |
-1021016748 | 2019-2-21 0:00: | PW | No Violations | 0.20 |
-1449453923 | 2017-2-7 0:00:0 | PW | No Violations | 0.50 |
-1618683193 | 2018-9-25 0:00: | PW | No Violations | 2.50 |
-648851518 | 2019-12-12 0:00 | PW | No Violations | 0.20 |
0049663816 | 2019-01-18 | Production Wells | No Violations | The well remains temporarily abandon with two cast iron bridge plugs. Ascent plans to drill out the plugs and install 2.875-inch diameter production tubing and bring the well back into production. Fortis Energy Services had a derrick service rig on location to drill out plugs. |
0082029087 | 2015-07-14 | Completion Testing | No Violations | On the day of my inspection I witnessed that drill out was completed and a production tree was in place. Clean-up of location and construction of the production facilities was 80% completed. Completed walk around with Construction Supervisor Travis Fortson revealing no violations. |
0180623669 | 2016-12-14 | Production Wells | No Violations | On the day of my inspection I witnessed the ground was snow covered and that the well is online and equipped with a Universal Wellhead LLC casing and production wellhead along with a Universal Wellhead LLC production tree with valves in the open position. Casing pressure was at 800 pounds per square inch and the tubing was at 400 pounds per square inch with annular pressure monitoring in place. Production equipment included a sand trap, a GP Unit, a line heater, a vapor recovery system, 2-NGL tanks, 2 compressor units, a combustor unit and a total of 12-400 barrel tanks all within containment and shared with the 1H and 5H. |
0446540628 | 2015-09-28 | Production Wells | No Violations | On the day of my inspection I witnessed that the well is online and equipped with a Universal Wellhead LLC casing and production wellhead along with a Universal Wellhead LLC production tree with valves in the open position. Casing pressure was at 2350psi and the tubing was a 1950psi. Production equipment included a sand trap, a GP Unit, a line heater, a vapor recovery system, 2-NGL tanks, 2 compressor units, a combustor unit and a total of 12-400bbl tanks all within containment and shared with the 1Hand 5H. |
0589398768 | 2019-03-18 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with open valves. Gauges present read 0 pounds per square inch on the 13.375-inch diameter surface casing, 0 pounds per square inch on the 9.625-inch diameter intermediate casing, 1600 pounds per square inch on the 5.5-inch diameter production casing, 900 pounds per square inch on the production tubing. The production equipment on location consisted on seven sand traps, seven gas production units, three horizontal heater treaters, four compressors, six 400-barrel tanks, five 500-barrel tanks, two vapor recovery towers, and one combustor. |
0733984184 | 2016-09-06 | Production Wells | No Violations | On the day of my inspection I witnessed that the well is online and equipped with a Universal Wellhead LLC casing and production wellhead along with a Universal Wellhead LLC production tree with valves in the open position. Casing pressure was at 1200 pounds per square inch and the tubing was at 800 pounds per square inch with annular pressure monitoring in place. Production equipment included a sand trap, a GP Unit, a line heater, a vapor recovery system, 2-NGL tanks, 2 compressor units, a combustor unit and a total of 12-400 barrel tanks all within containment and shared with the 1H and 5H. |
0930912668 | 2018-10-11 | Production Wells | No Violations | During my inspection Patterson 577 was no longer on location and the well was awaiting to be put back into production after being decommissioned for drilling operations on 4 new wells on pad. |
1021016748 | 2019-02-21 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a production tree style wellhead with open valves. The production equipment on location consisted on seven sand traps, seven gas production units, three horizontal heater treaters, four compressors, six 400-barrel tanks, five 500-barrel tanks, two vapor recovery towers, and one combustor. The four recently completed wells on location were flowing back. The flow back equipment on location consisted of three gas buster tanks, one frac tank, and three horizontal line heaters. |
1364793328 | 2018-09-25 | Production Wells | No Violations | The purpose of my inspection was a status check on drilling operations. Accompanied by ODNR Kenn Frye, during our inspection we completed a walk around with Ascent Resources Superintendent James McGee. Patterson 577 was on location in the process of drilling the 10H. This well had been decommissioned prior to rig Patterson 577 moving onto location. The well was equipped with valves on all casing strings. All valves showed 0 pounds per square inch and the a cage was placed over the well. |
1416320435 | 2014-11-16 | Casing String Witnessed | No Violations | On the day of my inspection I found that Nomac Drilling rig 80 had drilled a 17.5 hole to a depth of 979. They had new 13.375 casing in the ground, and were circulating when I arrived. They had to wash the last 40 of casing in. O-Tex Pumping broke circulation and pumped gel spacer followed by cement. Good circulation was maintained throughout the mixing process and there were no significant increases in pressure. They released the plug and were 15.3 barrels into displacement when the well instantly pressured up to 1760 psi. They shut down and let the pressure fall below 1500 psi. They attempted to pump again and the pressure immediately increased again after 0.2 barrels of displacement. O-Tex tried this two more times with the same result. AEU shut the job down and let the cement set up. They drilled the cement out of the casing and had a cement bond log ran. The log showed the top of the cement at 240. |
1416336692 | 2014-11-18 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found that Nomac Drilling rig 80 ran 1 tubing to a depth of 140 in the annulus of the 13.375 casing. O-Tex Pumping grouted the casing with class H cement. The wellhead had just been made up and pressure tested to 750 psi. They installed the blow out preventer and pressure tested the surface casing at 500 psi. for 30 minutes. There was no decrease in the pressure during the test. |
1417019746 | 2014-11-24 | Casing String Witnessed | No Violations | On the day of my inspection I found that Nomac Drilling rig 80 had drilled a 12.25 hole on air to a depth of 6507. They were in the process of running new 9.625 casing, equipped with a multi-stage tool at 3408. They were having problems getting the last 70 in and had to wash the casing down. O-Tex Pumping established circulation and pumped the first stage of the job. They landed the plug, increased the pressure by 500 psi and held for 5 minutes. Weatherford opened the multi-stage tool and O-Tex pumped to confirm the tool was open. Nomac 80 circulated through the tool for three hours. O-Tex hooked up and pumped the second stage of the job. Good circulation was maintained throughout with approximately 58 barrels of cement circulated to surface. |
1449453923 | 2017-02-07 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with a plunger lift system with valves in the open position. Casing pressure was at 650 pounds per square inch and the tubing was at 500 pounds per square inch with annular pressure monitoring in place. The production equipment included 12-400 barrel tanks within containment, 2-NGL tanks, a vapor recovery tower, 2-compressor units, 2-horizontal heater treaters, 2-oil stabilizer units and a gas combustor all shared with the 1H and 5H. Also present a GP Unit and a sand trap with identification present and production records current. |
1536101889 | 2018-09-04 | Production Wells | No Violations | The purpose of my inspection was a status check. The well was not in production while Patterson 577 was on location drilling 34059245250000. I spoke with Ascent Company man and he stated that the well is checked at least one time a day. |
1618683193 | 2018-09-25 | Production Wells | No Violations | The purpose of my inspection was to witness the status of temporary abandonment on well #2-4370. Guernsey County Inspector Austin Gutridge was present during the inspection. While on location we met with Ascent Drilling Superintendent James McGee. At the time of inspection, Patterson #577 was on location drilling on well Red Hill Farm 10H- #2-4526. The drilling crew was making a trip to change the drilling assembly. Well 3H was temporarily abandoned. The production tree was removed and night cap was in place. Annular valve had pressure gauges installed for monitoring. Pressure transducers were installed on the night cap monitoring port to allow for constant monitoring with alarms. A steel cage was located over the well head. A total of three (3) wells were temporarily abandoned. The surface production equipment had been removed. The transfer point was isolated. No simultaneous operations or anti-collision issues were identified during the inspection. |
1729709171 | 2015-06-15 | Completion Testing | No Violations | On the day of my inspection I witnessed FTS International frac stage 9 of 54 with a breakdown pressure of 7771psi, average treating pressure of 8665psi, average rate of 80.3bbls/min with 250626lbs of propant pumped. Completed walk around with company men Jim Andrews and Malcom Trahan revealing no violations. |
180623669 | 2016-12-14 0:00 | PW | No Violations | 0.50 |
1952107034 | 2018-06-28 | Production Wells | No Violations | The inspection is conducted as a simultaneous operation. The well is shut in and idle. The lubricator is in place and there is no pressure at surface. The intermediate casing and production is locked out and tagged out with 0 psi at surface. Cage has been placed around the well. |
2044222068 | 2015-08-10 | Production Wells | No Violations | On the day of my inspection I witnessed that the well is online and equipped with a Universal Wellhead LLC casing and production wellhead along with a Universal Wellhead LLC production tree with valves in the open position. Casing pressure was at 2500psi and the tubing was a 2400psi. Production equipment included a sand trap, a GP Unit, a line heater, a vapor recovery system, 2-NGL tanks, 2 compressor units, a combustor unit and a total of 12-400bbl tanks all within containment and shared with the 1Hand 5H. The well has been online for two weeks and current production levels are 800bbls of oil, 168bbls of water and 2MMCF of gas per day. |
2126564436 | 2015-04-09 | Preliminary Restoration | No Violations | On the day of my inspection production equipment has been installed and awaiting on frac. The site passed preliminary restoration according to ORC 1509.072A. |
2129345211 | 2018-12-28 | Production Wells | No Violations | During my inspection the well was temporarily abandoned and equipped with a night cap. Annular pressure monitoring was present and the well was caged. Four additional wells on pad had just finished hydraulic stimulation operations and the frac equipment was demobilizing off pad. |
446540628 | 2015-9-28 0:00: | PW | No Violations | 0.50 |
49663816 | 2019-1-18 0:00: | PW | No Violations | 0.30 |
589398768 | 2019-3-18 0:00: | PW | No Violations | 0.20 |
733984184 | 2016-9-6 0:00:0 | PW | No Violations | 0.50 |
82029087 | 2015-7-14 0:00: | CT | No Violations | 2.00 |
930912668 | 2018-10-11 0:00 | PW | No Violations | 0.10 |
For data sources see[9]