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Well ID: 34-059-24091 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Richland Township | |
Operator Name: ASCENT RESOURCES UTICA LLC | |
Well Pad ID: | |
Farm/Lease Name: HENDERSHOT/ROE UNIT | |
License Status: Final Restoration | |
License Date: 2018-05-17 | |
Spud Date: 2008-11-27 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2008-12-12 | |
Well Total Depth: 6006.00 ft | |
Configuration: Vertical | |
Latitude: 39.970000 | |
Longitude: -81.400000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2008-09-02 | Proposed Formations:CLINTON/MEDINA, Issued Date:9/2/2008, Expired Date:9/2/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2008-12-12 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Completion Report Received | 2009-07-13 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Change of Owner | 2017-01-25 | Operator changed from 490, DAVID R HILL INC to 8928, CARRIZO (UTICA) LLC |
Change of Owner | 2017-12-14 | Operator changed from 8928, CARRIZO (UTICA) LLC to 9520, ASCENT RESOURCES UTICA LLC |
APP | 2018-05-17 | Proposed Formations:CLINTON-MEDINA, Issued Date:5/17/2018, Expired Date:5/16/2020 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-06-18 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Record Last Modified | 2018-10-31 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
Construction Permit Expires | 2020-05-16 | GMM UPDATED PLUG STATUS PER PLUG REPORT |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2009-10-02 | 5739 | 5829 | 70 |
2009-10-02 | 5874 | 5880 | 13 |
5739 | 5829 | 70 | |
5874 | 5880 | 13 | |
5739 | 5829 | 70 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 83873 Gal | 40000 | FRACED INTERVAL INCLUDED THE MEDINA SANDSTONE |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | DAVID R HILL INC | 5478.00 | 0.00 | 163 |
2010 | DAVID R HILL INC | 4372.00 | 49.00 | 365 |
2011 | DAVID R HILL INC | 2746.00 | 51.00 | 365 |
2012 | DAVID R HILL INC | 2037.00 | 69.00 | 366 |
2013 | DAVID R HILL INC | 1129.00 | 34.00 | 365 |
2014 | DAVID R HILL INC | 1509.00 | 0.00 | 365 |
2015 | DAVID R HILL INC | 1107.00 | 41.00 | 365 |
2016 | DAVID R HILL INC | 892.00 | 0.00 | 365 |
2017 | CARRIZO (UTICA) LLC | 245.00 | 0.00 | 0 |
2018 | ASCENT RESOURCES UTICA LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2009 | DAVID R HILL INC | Brine | 445 | 163 |
2010 | DAVID R HILL INC | Brine | 330 | 365 |
2011 | DAVID R HILL INC | Brine | 141 | 365 |
2012 | DAVID R HILL INC | Brine | 108 | 366 |
2013 | DAVID R HILL INC | Brine | 56 | 365 |
2014 | DAVID R HILL INC | Brine | 215 | 365 |
2015 | DAVID R HILL INC | Brine | 50 | 365 |
2016 | DAVID R HILL INC | Brine | 0 | 365 |
2017 | DAVID R HILL INC | Brine | 149 | 365 |
2018 | ASCENT RESOURCES UTICA LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1239600726 | 2008-12-12 0:00 | DD | No Violations | |
-1449528049 | 2012-12-28 0:00 | PW | No Violations | |
-1682454333 | 2019-7-31 0:00: | FR | No Violations | 0.60 |
-973327976 | 2018-1-29 0:00: | PW | No Violations | 0.90 |
0523927395 | 2018-06-17 | Plug / Plug Back | No Violations | KLX rigged up on location and perforated the 8.625 inch diameter surface casing with six shots each at 1453 feet, 1214 feet, 400 feet, and 200 feet. Unlimited tripped the 2.375 inch tubing into 1493 feet. |
0530975808 | 2008-12-09 | Drill / Deepen / Reopen | No Violations | KILBARGER DRILLING #17. DILLING AT 3809 |
0827379718 | 2012-12-28 | Production Wells | No Violations | On the day of my inspection I found the divisions production records current, the pumping unit at the well site was running at the time of my inspection, there is (1) one hundred barrel production tank/ separator/ drip/ chart setting inside a containment dike, the I.D. is posted on the tank. |
0897275496 | 2018-06-18 | Plug / Plug Back | No Violations | Unlimited pumped a class A cement plug from 1493 feet to 1143 feet. The tubing was pulled up to 414 feet and a class A cement plug was pumped from 414 feet to surface. Cement circulation was established within the conductor and filled the 8.625 inch surface casing. |
0944919358 | 2018-05-10 | Production Wells | Violations Noted | |
0973327976 | 2018-01-29 | Production Wells | No Violations | On the day of my inspection I witnessed the production equipment included a 140 barrel tank, a 37 barrel plastic tank, a vertical separator, a drip, a 2 inch meter run with a .25 inch orifice and a chart recorder all within an earthen dike. The well was equipped with 8.625 inch diameter casing; 4.5 inch diameter casing, 2.375 inch diameter tubing, rods and an American pumping unit powered by electricity with valves closed on the tubing and closed on the casing. Identification was present and production records were current. |
1227706149 | 2008-11-26 | Drill / Deepen / Reopen | No Violations | WAREEN DRILLING #7. DRILLING AT 2480. PLAN TO DRILL TO 3300 AND SHUT DOWN FOR T-GIVING. ON EDGE OF COLUMBIA GAS STORAGE AREA. TO HAVE COLUMBIA GAS S PEOPLE OUT WHEN DRILLING COMMMENCES AFTER HOLIDAY. |
1228850064 | 2008-12-08 | Drill / Deepen / Reopen | No Violations | KILBARGER DRILLING #17. DRILLING AT 2054 |
1229038588 | 2008-12-11 | Drill / Deepen / Reopen | No Violations | KILBARGER DRILLING#17, DRILLING AT 5633 |
1239600726 | 2008-12-12 | Drill / Deepen / Reopen | No Violations | KILBARGER DRILLING #17. HOLE LOGGED AND RUNNING PIPE |
1258577988 | 2009-11-16 | Preliminary Restoration | No Violations | Inspection revealed that restoration work at site is satisfactory,pit has been filled in and site reclaimed and vegatation has been established. Well is equipped with pumping unit and tubing and rods and 1-100 bbl tank and 1-50 bbl water tank located within dike area. |
1449528049 | 2012-12-28 | Production Wells | No Violations | On the day of my inspection I found the divisions production records current, the valve on the production line is open, there are (2) one hundred barrel production tanks/ (2) plastic brine tanks/ (2) separators/ (2) drips/ (2) charts setting inside a containment dike, the I.D. is posted on the tank. |
1527248653 | 2018-05-16 | Production Wells | No Violations | During my inspection today the well continued to gas on the backside of the 8.625 inch diameter surface casing. There have not been any produced fluids released. |
1528413559 | 2018-06-06 | Production Wells | No Violations | The purpose of my inspection was a status check on plugging operations. Ascent Production Superintendent Adam Pence stated via email that Ascent planned to begin moving in to plug the well today. During my inspection the service company had not mobilized the rig to the location. Ascent well tenders were at the tank battery preparing to disassemble the equipment. I called Mr. Pence and asked him what his timeline was for mobilizing the rig and he stated that he would be rigging up on location this afternoon. |
1528990691 | 2018-06-13 | Plug / Plug Back | No Violations | Unlimited Energy Services was on location with their double pole service rig, cement pump truck, cement bulk truck, and water truck. Unlimited pumped a 400 foot bottom hole plug within the 4.5 inch casing from 5652 feet to 5252 feet with class A cement weighing 15.6 pound per gallon. The plug was displaced with 20 barrels of water. When the lines were disconnected from the tubing the well could be heard going on a vacuum. Unlimited pulled the tubing up out of the cement plug to 4652 feet. Unlimited waited on cement to cure and then tripped the tubing back down to tag the cement plug. The plug descended downhole past the reach of the tubing at 5652 feet. Unlimited pumped a 9 barrel gel pill and 30 sacks of class A cement with lost circulation material from 5652 feet to 5252 feet. the plan was to pump a 60 sack plug but due to pump truck complications we stopped pumping cement at 30 sacks and went into displacement with 20 barrels of fresh water. The tubing was tripped up out of the cement and the well was shut in overnight. |
1529252069 | 2018-06-14 | Plug / Plug Back | No Violations | Unlimited tripped the tubing down and tagged the cured cement plug at 5531 feet which was 208 feet above the top perforation within the 4.5 inch diameter production casing. Unlimited began to trip the tubing out of hole and KLX arrived on location. The rig experienced issues with the power tongs and breaking apart the tubing with pipe wrenches. Once the tubing was completely out of hole KLX ran a bond logon the 4.5 inch casing. A cave in was recorded at 1620 feet on the backside of the 4.5 inch casing. KLX shot the casing off at 4234 feet. |
1530473514 | 2018-06-15 | Plug / Plug Back | No Violations | Unlimited attempted to remove the 4.5 inch diameter casing from hole but could not do so. Unlimited began to pump water ahead of the big lime cement plug through the 4.5 inch casing and circulation was established inside the conductor. The conductor did not have any casing head to contain and control the circulation so Unlimited stopped pumping and shut down for the day to construct a lined earthen pit and a trench to the wellhead. |
1534433991 | 2018-08-16 | Final Restoration | No Violations | The purpose of my inspection was a status check on a final restoration. During my inspection the production equipment had been removed and the location had been graded. Once the vegetation is established the location will potentially meet requirements for final restoration. A follow up inspection will be conducted. |
1649551234 | 2008-11-26 | Drill / Deepen / Reopen | No Violations | KILBARGER DRILLING#17 RIGGED UP. BUT ARE WORKING ON RIG TODAY. TO DRILL CONDUCTOR HOLE AND SET CONDUCTOR PIPE THEN SHUT DOWN FOR DEER SEASON NEXT WEEK. |
523927395 | 2018-6-17 0:00: | PB | No Violations | 7.00 |
530975808 | 2008-12-9 0:00: | DD | No Violations | |
827379718 | 2012-12-28 0:00 | PW | No Violations | |
897275496 | 2018-6-18 0:00: | PB | No Violations | 4.00 |
941631999 | 2018-5-10 0:00: | PW | No Violations | 1.50 |
944919358 | 2018-5-10 0:00: | PW | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0944919358 | US-OH-130801 | 2018-05-24 | 9-9-02 | General Safety |
0944919358 | US-OH-130802 | 2018-05-24 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
0944919358 | US-OH-130803 | 2018-05-24 | NONE18 | Defective casing, leaking well |
For data sources see[9]