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Well ID: 34-059-24059 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Monroe Township | |
Operator Name: M & R INVESTMENTS OHIO LLC | |
Well Pad ID: | |
Farm/Lease Name: GALBRAITH/GETZ | |
License Status: Final Restoration | |
License Date: 2017-12-19 | |
Spud Date: 2007-08-09 | |
Spud Drilling Contractor: FMS DRILLING | |
Final Drill Date: 2007-08-19 | |
Well Total Depth: 5540.00 ft | |
Configuration: Vertical | |
Latitude: 40.200000 | |
Longitude: -81.440000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2007-05-25 | Proposed Formations:CLINTON/MEDINA, Issued Date:5/25/2007, Expired Date:5/24/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2007-08-19 | UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. |
Reached Total Depth | 2007-08-19 | UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. |
Completion Report Received | 2007-12-18 | UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. |
Change of Owner | 2017-10-17 | Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC |
APP | 2017-12-19 | Proposed Formations:CLINTON, Issued Date:12/19/2017, Expired Date:12/19/2019 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-09-19 | UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. |
Record Last Modified | 2018-11-02 | UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. |
Construction Permit Expires | 2019-12-19 | UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2008-03-06 | 5249 | 5300 | 37 |
5249 | 5300 | 37 | |
5249 | 5300 | 37 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 2095 Bbl | 80000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | ATLAS ENERGY GROUP INC | 196.00 | 72.00 | 105 |
2008 | ATLAS ENERGY GROUP INC | 8384.00 | 95.00 | 105 |
2009 | ATLAS ENERGY GROUP INC | 4327.00 | 62.00 | 365 |
2010 | ATLAS NOBLE LLC | 2810.00 | 29.00 | 365 |
2011 | ATLAS ENERGY GROUP INC | 1603.00 | 23.00 | 365 |
2012 | ATLAS NOBLE LLC | 734.00 | 0.00 | 137 |
2013 | ATLAS NOBLE LLC | 7.00 | 0.00 | 137 |
2014 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2015 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2016 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2017 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2007 | ATLAS ENERGY GROUP INC | Brine | 30 | 105 |
2008 | ATLAS ENERGY GROUP INC | Brine | 20 | 105 |
2009 | ATLAS ENERGY GROUP INC | Brine | 66 | 365 |
2010 | ATLAS NOBLE LLC | Brine | 55 | 365 |
2011 | ATLAS ENERGY GROUP INC | Brine | 70 | 365 |
2012 | ATLAS NOBLE LLC | Brine | 159 | 137 |
2013 | ATLAS NOBLE LLC | Brine | 76 | 137 |
2014 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2015 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2016 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2017 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1073932175 | 2017-10-17 0:00 | PW | No Violations | 1.50 |
-1114391442 | 2018-2-21 0:00: | PW | No Violations | 1.00 |
-125199580 | 2019-4-29 0:00: | FR | No Violations | 0.50 |
-128898712 | 2018-8-27 0:00: | PW | No Violations | 1.00 |
-145437603 | 2017-7-31 0:00: | PW | No Violations | 0.80 |
-1729077731 | 2016-8-31 0:00: | PW | No Violations | 2.00 |
-1902205729 | 2007-8-27 0:00: | PW | No Violations | |
-2045061053 | 2007-9-24 0:00: | PW | No Violations | |
-2132507873 | 2018-9-12 0:00: | PB | No Violations | 4.00 |
-441826059 | 2008-10-9 0:00: | PW | No Violations | |
-69766455 | 2017-6-22 0:00: | PW | No Violations | 1.00 |
-901082844 | 2016-12-7 0:00: | PW | No Violations | 2.50 |
0069766455 | 2017-06-22 | Production Wells | No Violations | |
0125199580 | 2019-04-29 | Final Restoration | No Violations | The purpose of my inspection was a status check on a final restoration. During my inspection the pits used during plugging operations had been back filled. Vegetation was very thin and spotty and production equipment remained on location. A follow up inspection will be conducted to ensure location meets 1509.072 (B) restoration requirements. |
0128898712 | 2018-08-27 | Production Wells | No Violations | The purpose of my inspection was a follow up on compliance notice numbered -1729077731. Larry Federman with Diversified MR Investments contacted me on 8/24/18 to inform me that a service rig will be mobilized to location to plug 3405921969 and 3405924059. During my inspection today, the well was equipped with 8.62- inch diameter casing, 4.5-inch diameter casing, 1.5-inch diameter tubing, a plunger lift system, and a domestic gas service. All valves were in the closed position. |
0145437603 | 2017-07-31 | Production Wells | No Violations | |
0227390124 | 2018-09-19 | Plug / Plug Back | No Violations | Formations Cementing pumped a 200-foot Big Lime plug from 3758 feet to 3558 feet with 60 sacks, a 200-foot Bottom of Surface plug from 1450 feet to 1250 feet with 60 sacks, and a 150-foot surface plug with 60 sacks. The cement was class A neat cement pumped through the 4.5-inch casing. The cement stayed at surface. Compliance notice -1729077731 stated well shall be plugged. On this date plugging of the well has been completed leaving the well no longer in violation. |
0285705513 | 2017-03-29 | Production Wells | No Violations | |
0340777179 | 2007-08-28 | Drill / Deepen / Reopen | No Violations | FMS DRILLING, DRILLING AT 2140 |
0441826059 | 2008-10-09 | Production Wells | No Violations | PRELIMENARY RESTORATION COMPLETE |
0675371216 | 2007-09-04 | Drill / Deepen / Reopen | No Violations | FMS DRILLING TD HOLE RUN 4, MOVE RIG TO NEXT LOCATION. |
0890259169 | 2008-09-17 | Preliminary Restoration | No Violations | PRELIMENARY RESTORATION |
0901082844 | 2016-12-07 | Production Wells | No Violations | |
1073932175 | 2017-10-17 | Production Wells | No Violations | |
1114391442 | 2018-02-21 | Production Wells | No Violations | |
1186672206 | 2007-08-09 | Drill / Deepen / Reopen | No Violations | FMS DRILLING AT 45 CONDUCTOR HOLE. ON FLUID. |
1186932950 | 2007-08-10 | Drill / Deepen / Reopen | No Violations | FMS DRILLING. DRILLED 110 15.750 HOLE. SET 96 OF 11.750 CEMENTED WITH 90 SX. UNIVERSAL THRU WATER ZONE. |
1187308166 | 2007-08-16 | Drill / Deepen / Reopen | No Violations | STATUS CHECK. FMS DRILLING AT 3318 |
1237187416 | 2017-02-06 | Production Wells | No Violations | |
1537339478 | 2018-09-17 | Plug / Plug Back | No Violations | Jet Wireline Services ran a bond log on the 4.5-inch diameter casing to verify a free point. The deepest free point was verified at 3800 feet, 230 feet into Big Lime formation. A collar buster was shot off at 3800 feet to part the 4.5-inch casing. Kenny Wright tripped one joint out verifying the casing was free. |
1564140766 | 2019-7-24 0:00: | FR | No Violations | 0.50 |
1729077731 | 2016-08-31 | Production Wells | Violations Noted | On the day of my inspection I witnessed the production equipment included a 100 barrel tank, a horizontal separator, a drip, a 2 inch salesmeter with a .75 inch orifice and a chart recorder all within an earthen dike and the chart was dated 10/9/13. Caution Hazard Area Hydrogen Sulfide (H2S) signs were posted at the tank and at the well along with a windsock at the wellhead. The well was equipped with 8.625 inch casing; 4.5 inch casing, 1.5 inch tubing, a plunger lift system and domestic gas service with all valves in the closed position. H2S was detected at the wellhead. Identification was present and production records were current with zero production reported for 2014 and 2015. The well owner/operator shall submit a written plugging schedule to Doug Bennett at 5880 Memory Road Zanesville, Ohio 43701-9553 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1736873723 | 2019-8-5 0:00:0 | FR | No Violations | 0.40 |
1882603809 | 2019-8-20 0:00: | FR | No Violations | 0.40 |
1902205729 | 2007-08-27 | Production Wells | No Violations | PSC INC. FRAC WELL TODAY |
2045061053 | 2007-09-24 | Production Wells | No Violations | WELL FRACED. LINE BEING INSTALLED. LOCATION BEING ROUGHED IN. |
2132507873 | 2018-09-12 | Plug / Plug Back | No Violations | The purpose of my inspection was to witness plugging operations. Kenny Wright and Formations were on location. 1.5-inch diameter tubing was tripped within the 4.5-inch casing to 5250 feet and Formations cementing pumped a 400-foot class A cement plug with 30 sacks. |
227390124 | 2018-9-19 0:00: | PB | No Violations | 8.00 |
285705513 | 2017-3-29 0:00: | PW | No Violations | 1.00 |
340777179 | 2007-8-28 0:00: | DD | No Violations | |
675371216 | 2007-9-4 0:00:0 | DD | No Violations | |
890259169 | 2008-9-17 0:00: | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1729077731 | US-OH-117160 | 2016-09-06 | Well shall be plugged |
For data sources see[9]