If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-059-22886 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.12,"lon":-81.25,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Londonderry Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: BOND R | |
License Status: Producing | |
License Date: 1980-12-31 | |
Spud Date: 1981-04-01 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-04-06 | |
Well Total Depth: 6210.00 ft | |
Configuration: Vertical | |
Latitude: 40.120000 | |
Longitude: -81.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-12-31 | 2143 CARLESS RESOURCES INC GeoDate 12/31/80 |
Oil and Gas | 1980-12-31 | Issued Date 12/31/80 Expired Date Acres 0040000 Tool Type Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1981-04-01 | |
Completed | 1981-04-06 | |
Reached Total Depth | 1981-04-06 | |
Change of Owner | 1998-06-15 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6026 | 6036 | 6 |
2006-09-11 | 6042 | 6057 | 8 |
6026 | 6036 | 6 | |
6026 | 6036 | 6 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | ZILKHA ENERGY INC | 1456.00 | 2.00 | 265 |
1987 | ZILKHA ENERGY INC | 2255.00 | 6.00 | 178 |
1988 | CARLESS RESOURCES INC | 1147.00 | 0.00 | 365 |
1989 | CARLESS RESOURCES INC | 1006.00 | 0.00 | 350 |
1990 | CARLESS RESOURCES INC | 940.00 | 0.00 | 365 |
1991 | CARLESS RESOURCES INC | 966.00 | 0.00 | 365 |
1992 | CARLESS RESOURCES INC | 1112.00 | 0.00 | 365 |
1993 | CARLESS RESOURCES INC | 1013.00 | 0.00 | 365 |
1994 | CARLESS RESOURCES INC | 914.00 | 0.00 | 365 |
1995 | CARLESS RESOURCES INC | 716.00 | 0.00 | 365 |
1996 | CARLESS RESOURCES INC | 758.00 | 0.00 | 365 |
1997 | CARLESS RESOURCES INC | 734.00 | 0.00 | 365 |
1998 | EXCO - NORTH COAST ENERGY INC | 810.00 | 0.00 | 365 |
1999 | EXCO - NORTH COAST ENERGY INC | 605.00 | 0.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 622.00 | 57.00 | 365 |
2001 | EXCO - NORTH COAST ENERGY INC | 712.00 | 0.00 | 365 |
2002 | EXCO - NORTH COAST ENERGY INC | 740.00 | 0.00 | 365 |
2003 | EXCO - NORTH COAST ENERGY INC | 711.00 | 0.00 | 365 |
2004 | EXCO - NORTH COAST ENERGY INC | 655.00 | 0.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 454.00 | 51.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 346.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 419.00 | 0.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 421.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 405.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 507.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 381.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 419.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 292.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 298.00 | 0.00 | 365 |
2015 | ENERVEST OPERATING LLC | 174.00 | 0.00 | 241 |
2016 | ENERVEST OPERATING LLC | 262.00 | 0.00 | 108 |
2017 | ENERVEST OPERATING LLC | 1128.00 | 0.00 | 146 |
2018 | ENERVEST OPERATING LLC | 465.00 | 18.00 | 205 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1467083184 | 2005-4-29 0:00: | PW | No Violations | |
-1481439811 | 2017-7-5 0:00:0 | PW | No Violations | 0.50 |
-1527167056 | 2015-12-15 0:00 | PW | No Violations | 1.00 |
-1876612685 | 2018-5-30 0:00: | PW | No Violations | 1.00 |
-2030123775 | 2019-11-20 0:00 | PW | No Violations | 0.20 |
-310392590 | 2003-12-9 0:00: | PW | No Violations | |
-690724446 | 2019-11-20 0:00 | PW | No Violations | 0.50 |
0255089000 | 2017-06-06 | Production Wells | No Violations | On the day of my inspection to record well pressures near the 34059231340000 Shepard 1, I witnessed that the production equipment included a 210 barrel tank, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves open on the tubing and 1 of 2 open on the casing supplying the domestic gas and the motor valve. Gauges present read 420 pounds per square inch on the tubing and the casing. Well identification was present and production records are current. |
0310392590 | 2003-12-09 | Production Wells | No Violations | status check |
0581609473 | 2019-02-14 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with 8.625-inch diameter surface casing with a casing head, 4.5-inch diameter production casing with a tubing head, 1.5-inch diameter tubing, and a plunger lift system. Production valves were in the closed position. A domestic gas service was attached to the 4.5-inch casing with a regulator, meter, and an open valve. The production equipment consisted of one 210-barrel tank, one horizontal separator, one drip, and a sales meter. The sales meter had a 2-inch diameter sales line, a .75-inch orifice plate, and a chart recorder with current chart. The production records were current. The identification was located on the tank. |
0680436265 | 2017-02-24 | Production Wells | No Violations | On the day of my inspection accompanied by ODNR Inspector Austin Gutridge to record well pressures near the 34059231340000 Shepard 1, I witnessed that the production equipment included a 210 barrel tank, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves open on the tubing and 1 of 2 open on the casing supplying the domestic gas and the motor valve. Gauges present read 480 pounds per square inch on the tubing and the casing. Well identification was present and production records are current. |
0906054398 | 2014-09-10 | Production Wells | No Violations | On the day of my inspection I witnessed that the production equipment included a 210bbl tank which was shared with the 34059230910000 Bond 3, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system with valves open on the tubing. Well identification was present and production records are current. |
1010400026 | 2005-09-01 | Final Restoration | No Violations | FINAL RESTORATION |
1145879355 | 2006-04-21 | Production Wells | No Violations | PRODUCTION WELL. |
1467083184 | 2005-04-29 | Production Wells | No Violations | STATUS CHECK |
1481439811 | 2017-07-05 | Production Wells | No Violations | On the day of my inspection to record well pressures near the 34059231340000 Shepard 1, I witnessed that the production equipment included a 210 barrel tank, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves open on the tubing and 1 of 2 open on the casing supplying the domestic gas and the motor valve. Gauges present read 180 pounds per square inch on the tubing and 220 pounds per square inch the casing. Well identification was present and production records are current. |
1487959824 | 2017-02-24 | Production Wells | No Violations | On the day of my inspection accompanied by ODNR Inspector Doug Bennett to record well pressures near the 34059231340000 Shepard 1, I witnessed that the production equipment included a 210 barrel tank, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing, a plunger lift system and domestic gas service with valves open on the tubing and 1 of 2 open on the casing supplying the domestic gas and the motor valve. Gauges present read 480 pounds per square inch on the tubing and the casing. Well identification was present and production records are current. |
1527167056 | 2015-12-15 | Production Wells | No Violations | On the day of my inspection I witnessed that the production equipment included a 210bbl tank, a horizontal separator, a 2 inch sales meter with a .75 inch orifice and a chart recorder. The well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system and domestic gas service with valves closed on the tubing and 1 of 2 open on the casing supplying the domestic gas and the motor valve. Well identification was present and production records are current. |
1527693754 | 2018-05-29 | Production Wells | No Violations | One 210 barrel tank and one horizontal separator are placed within an earthen dike. Inspection found 45 feet by 8 feet area of stressed vegetation on the downhill slope of the west side of the dike. The source of the stressed vegetation was a 4 inch PVC dike drain that was located in the base of the dike. A layer of produced fluids surrounding the 210 barrel tank roughly 2 inches deep was lying in the bottom of the dike that makes up a 35 feet by 18 feet area. The 210 barrel tank was leaking through the valve on the sales outlet connection. I tested the fluid within the dike with high range Quantab titrators for Chloride and the results exceeded the maximum readable limit of 6298 parts per million. I called Tim McConaughey with Enervest operating and he stated that he would send someone out as soon as possible. Enervest well tender Rick Spratt arrived on location and evaluated the area. Mr. Spratt called a water truck and the roustabout crew to assist in clean-up operations. A water truck arrived and removed the fluids from within the dike and placed a solid plug within the sales outlet connection on the tank and prevented the tank from leaking. A roustabout crew will be here tomorrow to remove the contaminated soil, seed and mulch the area. |
1876612685 | 2018-05-30 | Production Wells | No Violations | The purpose of my inspection was to witness clean-up operations. Enervest Operating roustabout crew removed the dike drain, rebuilt the dike wall, removed the contaminated soil, and seeded and mulched the area where the soil was removed. I evaluated the tank and found that it was not leaking. |
255089000 | 2017-6-6 0:00:0 | PW | No Violations | 0.50 |
581609473 | 2019-2-14 0:00: | PW | No Violations | 0.30 |
680436265 | 2017-2-24 0:00: | PW | No Violations | 1.00 |
906054398 | 2014-9-10 0:00: | PW | No Violations | 1.00 |
For data sources see[9]