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Well ID: 34-059-22282 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Spencer Township | |
Operator Name: SABRE ENERGY CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: WILSON-SCHWARZ | |
License Status: Final Restoration | |
License Date: 2013-05-17 | |
Spud Date: 1978-03-22 | |
Spud Drilling Contractor: | |
Final Drill Date: 1978-04-02 | |
Well Total Depth: 5163.00 ft | |
Configuration: Vertical | |
Latitude: 39.850000 | |
Longitude: -81.630000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1977-12-08 | 182 BELDEN & BLAKE CO GeoDate 12/8/77 |
Original Spud | 1978-03-22 | |
Completed | 1978-04-02 | |
Reached Total Depth | 1978-04-02 | |
Completion Report Received | 1978-07-20 | |
CO | 1994-10-25 | 4381 PELICAN PRODUCING INC GeoDate 12/8/77 |
CO | 1996-12-10 | 5244 SABRE ENERGY CORPORATION GeoDate 12/8/77 |
APP | 2003-07-09 | Proposed Formations:CLINTON, Issued Date:7/9/2003, Expired Date:7/8/2004 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
APP | 2013-05-17 | Proposed Formations:QUEENSTON, Issued Date:5/17/2013, Expired Date:5/17/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-07-18 | |
Construction Permit Expires | 2015-05-17 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5016 | 5063 | 2 |
5016 | 5063 | 2 | |
5016 | 5063 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1620 Bbl | 76000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1525508403 | 2016-5-2 0:00:0 | FR | No Violations | 0.50 |
-22689633 | 2012-3-9 0:00:0 | PW | No Violations | |
0022689633 | 2012-03-09 | Production Wells | No Violations | Inspection revealed that well is equipped with 8 surface casing and 4.5 production casing and 2.375 tubing and all valves were shut on the day of my inspection, contacted well owner and he stated that he was going to apply for temporary inactive status for said well. |
1373902330 | 2013-07-15 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Cemenco place a 400 class A cement plug at a depth of 4600 up to 4260, the 4.5 casing was shot apart at 4660, the tubing and the 4.5 casing is being pulled out so the tubing can be ran back in to the big lime, the pit was constructed and lined with ten mill black plastic through the flow ditch and around the well head. |
1374080201 | 2013-07-17 | Plug / Plug Back | No Violations | On the day of my inspection, I witnessed Cemenco attempt to break circulate water before pumping the cement plug over the Clinton formation but was uncessful due to a blockage in the tubing, at that point the rig crew was pulling the tubing back out of the hole and shutting down for the day. |
1455615479 | 2013-10-24 | Plug / Plug Back | No Violations | This well is plugged. |
1525508403 | 2016-05-02 | Final Restoration | No Violations | On the day of my inspection following up on prior final restoration which passed on 10/24/13 the site met ORC 1509.072B. |
For data sources see[9]