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34-059-22154

Well Details

Well ID: 34-059-22154
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Country: United States
State: Ohio
County: Guernsey
Municipality: Londonderry Township
Operator Name: CASTON MAX
Well Pad ID:
Farm/Lease Name: CASTEN EARL
License Status: Domestic Well
License Date: 2003-01-29
Spud Date: 1977-09-06
Spud Drilling Contractor:
Final Drill Date: 1977-09-14
Well Total Depth: 5972.00 ft
Configuration: Vertical
Latitude: 40.130000
Longitude: -81.320000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-08-26 2143 CARLESS RESOURCES INC GeoDate 8/26/77
Original Spud 1977-09-06
Completed 1977-09-14
Reached Total Depth 1977-09-14
Plugging Plan Approved 1998-02-20
Change of Owner 1998-11-17 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2002-11-14 Operator changed from 1388, NORTH COAST ENERGY INC to 1, HOPEWELL OIL & GAS
APP 2003-01-29 Proposed Formations:CLINTON, Issued Date:1/29/2003, Expired Date:1/29/2004 6:00:00 AM, Drilling unit acres:203, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2003-03-07 Operator changed from 1, HOPEWELL OIL & GAS to 7410, CASTON EARL
Construction Permit Expires 2004-01-29
Record Last Modified 2012-06-01

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-11-05 5770 5873 20
5770 5873 20
5770 5873 20

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 74970 Gal 63500

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RSC ENERGY CORP 2972.00 89.00 0
1985 CARLESS RESOURCES INC 2345.00 0.00 365
1986 CARLESS RESOURCES INC 2575.00 95.00 365
1987 CARLESS RESOURCES INC 1878.00 68.00 304
1988 CARLESS RESOURCES INC 0.00 0.00 0
1989 CARLESS RESOURCES INC 2217.00 0.00 350
1990 CARLESS RESOURCES INC 1033.00 0.00 365
1991 CARLESS RESOURCES INC 3846.00 64.00 365
1992 CARLESS RESOURCES INC 2708.00 0.00 365
1993 CARLESS RESOURCES INC 2659.00 155.00 365
1994 CARLESS RESOURCES INC 0.00 0.00 0
1995 CARLESS RESOURCES INC 2389.00 93.00 365
1996 CARLESS RESOURCES INC 1602.00 51.00 0
1997 CARLESS RESOURCES INC 141.00 0.00 90
1998 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
1999 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2001 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2002 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RSC ENERGY CORP Brine 0 0
1985 CARLESS RESOURCES INC Brine 0 365
1986 CARLESS RESOURCES INC Brine 141 365
1987 CARLESS RESOURCES INC Brine 0 304
1988 CARLESS RESOURCES INC Brine 0 0
1989 CARLESS RESOURCES INC Brine 120 350
1990 CARLESS RESOURCES INC Brine 0 365
1991 CARLESS RESOURCES INC Brine 105 365
1992 CARLESS RESOURCES INC Brine 159 365
1993 CARLESS RESOURCES INC Brine 0 365
1994 CARLESS RESOURCES INC Brine 0 0
1995 CARLESS RESOURCES INC Brine 156 365
1996 CARLESS RESOURCES INC Brine 0 0
1997 CARLESS RESOURCES INC Brine 0 90
1998 EXCO - NORTH COAST ENERGY INC Brine 0 0
1999 EXCO - NORTH COAST ENERGY INC Brine 365
2000 EXCO - NORTH COAST ENERGY INC Brine 0 0
2001 EXCO - NORTH COAST ENERGY INC Brine 0 0
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1024739966 2011-7-5 0:00:0 PW No Violations
-1754020206 2013-10-24 0:00 PW No Violations
-1773869017 2011-6-16 0:00: PW No Violations
-1891779631 2005-11-9 0:00: PW No Violations
-410649776 2006-1-10 0:00: PW No Violations
0410649776 2006-01-10 Production Wells No Violations DOMESTIC WELL
0486082025 2013-10-24 Production Wells No Violations On the day of my inspection, I found the well was being used for domestic use only, the area of containment ion around the well head was cleaned up, there is a separator and (2) one hundred barrel production tanks setting inside a containment dike, the I.D. is posted on the tank and the well head.
1024739966 2011-07-05 Production Wells No Violations Talked to property owner Max Casten in regards to getting well properly registered in his name and getting well back into production and cleaning up around wellhead and getting proper identification posted.
1316460287 2011-09-19 Production Wells No Violations Inspection revealed that landowner has cleaned up well site but still needs to get well registered in his name(Max Caston) in conversation with him he stated that he was in process of doing so.
1382486099 2003-04-14 Production Wells No Violations status check. Bought off north coast energy, to plug due to h2s gas.
1591190888 2011-06-16 Production Wells No Violations FOLLOW UP TO NOV # -1773869017 Upon receiving anonymous complaint of leaking well on property inspected site and found well to be leaking around tubing and also 4.5 casing there is a kill area approximately 20 wide and 40 long that needs to be cleaned up and well does not have proper identification on it and also the well has a sulfur odor noted at wellhead, well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing and 2-100 bbl tanks and separator.

Plug or Produce well and clean up affected area and properly Identify well and haul contamininated soil to a approved landfill. Failure to complymay result in bond forfiture.

1754020206 2013-10-24 Production Wells No Violations Previous compliance notice issued for this well has been resolved.
1773180730 2013-10-29 Production Wells No Violations The well is being used for domestic use only, and is registered to Earl Casten, all the compliance issues have been resolved.
1773869017 2011-06-16 Production Wells Violations Noted Upon receiving anonymous complaint of leaking well on property inspected site and found well to be leaking around tubing and also 4.5 casing there is a kill area approximately 20 wide and 40 long that needs to be cleaned up and well does not have proper identification on it and also the well has a sulfur odor noted at wellhead, well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing and 2-100 bbl tanks and separator.

Plug or Produce well and clean up affected area and properly Identify well and haul contamininated soil to a approved landfill. Failure to complymay result in bond forfiture.

1891779631 2005-11-09 Production Wells No Violations DOMESTIC WELL
1974705702 2009-03-03 Production Wells No Violations DOMESTIC WELL
2120044934 2015-01-12 Administrative Inspection No Violations On the day of my inspection following up on NOV-159190888, I witnessed production equipment included 2-100bbl tanks, a 50bbl tank and a horizontal separator all within an earthen dike. The well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing, a plunger lift system and domestic gas service. Valves were closed on the tubing and 1 of 2 valves was open on the casing supplying the domestic gas service. Identification was present and all issues being resolved with the transfer of the well.
486082025 2013-10-24 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1773869017 US-OH-117666 2014-04-23 Well operation causing pollution and contamination
1773869017 US-OH-117667 2014-04-23 Failure to legibly identify well
1773869017 US-OH-117668 2014-04-23 Defective casing, leaking well

For data sources see[9]

References