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34-059-21669

Well Details

Well ID: 34-059-21669
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Country: United States
State: Ohio
County: Guernsey
Municipality: Spencer Township
Operator Name: G-R CONTRACTING INC
Well Pad ID:
Farm/Lease Name: LESTOCK-HOWELL
License Status: Final Restoration
License Date: 2009-02-23
Spud Date: 1973-05-31
Spud Drilling Contractor:
Final Drill Date: 1973-06-11
Well Total Depth: 5090.00 ft
Configuration: Vertical
Latitude: 39.880000
Longitude: -81.640000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1973-05-10 182 BELDEN & BLAKE CO GeoDate 5/10/73
Original Spud 1973-05-31
Completed 1973-06-11
Reached Total Depth 1973-06-11
CO 1993-01-28 4381 PELICAN PRODUCING INC GeoDate 5/10/73
CO 1995-11-24 1217 HARRISON ENERGY GeoDate 5/10/73
CO 1996-04-10 952 G-R CONTRACTING INC GeoDate 5/10/73
Change of Owner 2007-11-14 Operator changed from 952, G-R CONTRACTING INC to 8308, LESTOCK WAYNE
Change of Owner 2008-10-07 Operator changed from 8308, LESTOCK WAYNE to 0952, G-R CONTRACTING INC
APP 2009-02-23 Proposed Formations:CLINTON, Issued Date:2/23/2009, Expired Date:2/23/2010 6:00:00 AM, Drilling unit acres:407, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2009-03-12
Construction Permit Expires 2010-02-23
Record Last Modified 2013-03-14

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4920 4940 2
4920 4940 2
4920 4940 2

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ENTERPRISE ENERGY CORP 1446.00 388.00 0
1985 OXFORD OIL 1073.00 182.00 365
1986 OXFORD OIL 628.00 97.00 365
1987 BELDEN & BLAKE CORPORATION 518.00 83.00 365
1988 OXFORD OIL 925.00 347.00 365
1990 BELDEN & BLAKE CORPORATION 760.00 388.00 265
1991 BELDEN & BLAKE CORPORATION 546.00 153.00 365
1992 BELDEN & BLAKE CORPORATION 547.00 94.00 239
1993 BELDEN & BLAKE CORPORATION 25.00 0.00 366
1994 PELICAN PRODUCING INC 378.00 322.00 365
1995 PELICAN PRODUCING INC 393.00 271.00 310
1996 G-R CONTRACTING INC 305.00 95.00 365
1997 G-R CONTRACTING INC 404.00 185.00 365
1998 G-R CONTRACTING INC 239.00 0.00 365
2000 G-R CONTRACTING INC 167.00 84.00 365
2001 G-R CONTRACTING INC 76.00 0.00 365
2002 G-R CONTRACTING INC 25.00 0.00 365
2003 G-R CONTRACTING INC 12.00 116.00 365
2004 G-R CONTRACTING INC 150.00 0.00 365
2005 G-R CONTRACTING INC 0.00 0.00 365
2006 G-R CONTRACTING INC 0.00 0.00 365
2007 G-R CONTRACTING INC 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ENTERPRISE ENERGY CORP Brine 150 0
1985 OXFORD OIL Brine 0 365
1986 OXFORD OIL Brine 0 365
1987 BELDEN & BLAKE CORPORATION Brine 4 365
1988 OXFORD OIL Brine 0 365
1990 BELDEN & BLAKE CORPORATION Brine 7 265
1991 BELDEN & BLAKE CORPORATION Brine 26 365
1992 BELDEN & BLAKE CORPORATION Brine 7 239
1993 BELDEN & BLAKE CORPORATION Brine 0 366
1994 PELICAN PRODUCING INC Brine 30 365
1995 PELICAN PRODUCING INC Brine 0 310
1996 G-R CONTRACTING INC Brine 0 365
1997 G-R CONTRACTING INC Brine 0 365
1998 G-R CONTRACTING INC Brine 0 365
2000 G-R CONTRACTING INC Brine 0 365
2001 G-R CONTRACTING INC Brine 0 365
2002 G-R CONTRACTING INC Brine 0 365
2003 G-R CONTRACTING INC Brine 0 365
2004 G-R CONTRACTING INC Brine 0 365
2005 G-R CONTRACTING INC Brine 0 365
2006 G-R CONTRACTING INC Brine 0 365
2007 G-R CONTRACTING INC Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1998540308 2010-1-20 0:00: FR No Violations
0837356230 2008-11-10 Production Wells No Violations POWER SWIVEL AT 3000. COMPLAINT FROM HEALTH DEPT. AND OEPA.
1226006988 2008-11-06 Production Wells No Violations HUMAN WAIST PUMPED DOWN WELL. ALSO SPREAD ALONG STREAM BANK AND IN STREAM. COMPANY WANTS TO RUN RODS AND TUBING IN HOLE. THICK WASTE IN CASING WILL HAVE TO POWER SWIVEL OUT WASTE TO GET RODS AND TUBING DOWNHOLE. GUERNSEY HEALTH DEPT. AND OEPA NOTIFIED OF SPREADING. OEPA WILL CONTACT PEOPLE IN CHARGE OF THIS AND GUERNSEY BASICALLY WAS OF NO HELP. TOLD ME TO NOTIFY OEPA. START TO DIG PITS FOR SWIVEL JOB AND RIG UP POWER SWIVEL. NO SAMPLES TAKEN. HUMAN WASTE.
1226528762 2008-11-12 Production Wells No Violations CO TOOLS POWER SWIVEL DOWN TO 3978. ON TO SOMETHING HARD. CONTINUE TO POWER SWIVEL.
1490815738 2015-08-25 Final Restoration No Violations On the day of my inspection following up on Complaint ID #5100, the final restoration was approved on 1/20/12 and utilizing a hand held GPS unit, a plat and coordinates from RBDMS locating the well site I found no signs of contamination present.
1505827346 2007-07-17 Production Wells No Violations WELL HAD NO ID PUMPER PLACED ID ON WELL WHILE WE WERE ON SITE. THIS WELL IS A UNITIZED WELL AND THE HOWELL HEIRS ARS UPSET BECAUSE WELL WAS SOLD TO THE LESTOCKS WITH OUT THEIR KNOWLEDGE. FOR THE TIM BEING THER HAS BEEN NO FORM 7 SUBMITTED TO COLUMBUS, NO
1998540308 2010-01-20 Final Restoration No Violations Restoration work at site satisfactory, pit has been filled in and site restored and vegetation has been established.

Note: Landowner turned cattle in on property before area was totally vegetated.

837356230 2008-11-10 0:00 PW No Violations

For data sources see[8]

References