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Well ID: 34-059-21471 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Valley Township | |
Operator Name: GREEN GAS CO | |
Well Pad ID: | |
Farm/Lease Name: ROLLING HILLS | |
License Status: Producing | |
License Date: 2016-08-03 | |
Spud Date: 1989-09-28 | |
Spud Drilling Contractor: | |
Final Drill Date: 1971-09-13 | |
Well Total Depth: 5387.00 ft | |
Configuration: Vertical | |
Latitude: 39.930000 | |
Longitude: -81.560000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 201 GREEN GAS CO |
Original Spud | 1971-09-02 | PB 6-10-89 |
Completed | 1971-09-13 | PB 6-10-89 |
Reached Total Depth | 1971-09-13 | PB 6-10-89 |
CO | 1989-06-06 | 201 GREEN GAS CO GeoDate 6/6/89 |
Oil and Gas | 1989-06-06 | Issued Date 6/6/89 Expired Date 6/6/90 Acres 0040000 Tool Type RTF Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Plugged Back | 1989-09-28 | PB 6-10-89 |
APP | 2016-08-03 | Proposed Formations:BEREA, Issued Date:8/3/2016, Expired Date:8/3/2018 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Record Last Modified | 2017-02-10 | PB 6-10-89 |
Construction Permit Expires | 2018-08-03 | PB 6-10-89 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5119 | 5184 | 21 |
5119 | 5184 | 21 | |
5119 | 5184 | 21 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1864 Bbl | 35000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | AN-CAR OIL CO INC | 0.00 | 289.00 | 0 |
1985 | AN-CAR OIL CO INC | 0.00 | 202.00 | 0 |
1986 | AN-CAR OIL CO INC | 0.00 | 132.00 | 365 |
1987 | AN-CAR OIL CO INC | 0.00 | 160.00 | 365 |
1988 | NOBLE GAS CO | 0.00 | 227.00 | 365 |
1989 | NOBLE GAS CO | 0.00 | 26.00 | 365 |
1990 | WALDRON DAVID A | 0.00 | 572.00 | 365 |
1991 | GREEN GAS CO | 0.00 | 0.00 | 365 |
2016 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2017 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2018 | GREEN GAS CO | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | AN-CAR OIL CO INC | Brine | 0 | 0 |
1985 | AN-CAR OIL CO INC | Brine | 0 | 0 |
1986 | AN-CAR OIL CO INC | Brine | 0 | 365 |
1987 | AN-CAR OIL CO INC | Brine | 0 | 365 |
1988 | NOBLE GAS CO | Brine | 145 | 365 |
1989 | NOBLE GAS CO | Brine | 145 | 365 |
1990 | WALDRON DAVID A | Brine | 0 | 365 |
1991 | GREEN GAS CO | Brine | 0 | 365 |
2016 | GREEN GAS CO | Brine | 0 | 0 |
2017 | GREEN GAS CO | Brine | 0 | 0 |
2018 | GREEN GAS CO | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1081085741 | 2017-10-11 0:00 | PW | No Violations | 1.60 |
-1589190530 | 2017-6-13 0:00: | PW | No Violations | 1.00 |
-18307532 | 2017-7-7 0:00:0 | PW | No Violations | 1.00 |
-185421963 | 2017-9-28 0:00: | PW | No Violations | 1.00 |
-1950947529 | 2017-3-30 0:00: | PW | No Violations | 1.00 |
-268556 | 2016-6-24 0:00: | PW | No Violations | 1.00 |
-317264761 | 2017-5-4 0:00:0 | PW | No Violations | 1.50 |
-583001331 | 2020-7-20 0:00: | PW | No Violations | 1.00 |
-606309653 | 2020-6-9 0:00:0 | PW | No Violations | 1.00 |
-698918014 | 2020-4-21 0:00: | PW | No Violations | 1.00 |
0000268556 | 2016-06-24 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I found no change in status of well since the last inspection on 5/27/16 and no plugging permit has been received. |
0018307532 | 2017-07-07 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on June 13, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
0068397086 | 2016-03-08 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I found no change in status of well and no plug permit has been issued. |
0106787188 | 2016-01-25 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I found no change in status of well. I met with Green Gas representative Rusty Walters at 34059229230000 Rolling Hills School District 2 and discussed status of well. Mr. Walters stated that Green Gas will be plugging said well and he was unsure of the time frame. |
0185421963 | 2017-09-28 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on August 9, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
0193462019 | 2016-12-05 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I found the well remains incapable of production with no change in the status of well since the last inspection on 9/12/16. |
0317264761 | 2017-05-04 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on March 30, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
0566079865 | 2016-04-06 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I found no change in status of well since the last inspection on 3/8/16. |
0619224396 | 2017-01-30 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on 12/5/16. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported was in 1991. |
1022166626 | 2019-12-18 0:00 | PW | No Violations | 1.10 |
106787188 | 2016-1-25 0:00: | PW | No Violations | 1.00 |
1081085741 | 2017-10-11 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on October 6, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. The access road is heavily vegetated and major erosion is occurring. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
1288834128 | 2017-08-09 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on July 7, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
1450803157 | 2015-12-22 | Production Wells | Violations Noted | On the day of my inspection I witnessed a Bethlehem pumping unit along the access road. The well was equipped with 8.625 inch casing and 4.5 inch casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported to the State was in 1991. The well owner/operator shall submit a written plugging schedule to Doug Bennett at 5880 Memory Road Zanesville, Ohio 43701-9553 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1468169436 | 2016-07-10 | Administrative Inspection | No Violations | |
1468347239 | 2016-07-12 | Administrative Inspection | No Violations | Research yielded a plugging report revealing the well was plugged back beginning on 9/27/89 with prepared clay washed in from total depth to 4800 feet. The 4.5 inch casing was ripped at 4079 feet and a 200 foot big lime cement plug was set from 3839 feet to 3639 feet. A 200 foot cement plug was set from 1700 feet to 1500 feet completing the plug back on 9/28/89. |
1559646036 | 2019-5-31 0:00: | PW | No Violations | 1.50 |
1589190530 | 2017-06-13 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on May 4, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
1689297791 | 2016-05-27 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I found no change in status of well since the last inspection on 3/8/16. I received a call from Dean Davis of Green Gas Company stating that they plan on plugging the well this summer. I stated that action for the compliance notice is due on 6/22/16 and no plug permit has been applied for. |
1801579507 | 2018-02-14 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on October 11, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. The access road is heavily vegetated and major erosion is occurring. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
193462019 | 2016-12-5 0:00: | PW | No Violations | 2.00 |
1950947529 | 2017-03-30 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice-1450803157, I witnessed no change in the status of well since the last inspection on January 30, 2017. A Bethlehem pumping unit remains along the access road. The well was equipped with 8.625 inch diameter casing and 4.5 inch diameter casing reduced to 2 inches with the valve in the closed position and the flowline disconnected. No identification was present and last production reported was in 1991. There has been no communication from Green Gas regarding plugging of the well. |
2109326629 | 2020-5-7 0:00:0 | PW | No Violations | 1.00 |
2130086461 | 2019-12-18 0:00 | PW | No Violations | 1.00 |
566079865 | 2016-4-6 0:00:0 | PW | No Violations | 2.00 |
619224396 | 2017-1-30 0:00: | PW | No Violations | 1.00 |
68397086 | 2016-3-8 0:00:0 | PW | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1450803157 | US-OH-113072 | 2015-12-31 | Failure to legibly identify well | |
1450803157 | US-OH-113073 | 2015-12-31 | Well shall be plugged |
For data sources see[9]