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34-059-21224

Well Details

Well ID: 34-059-21224
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Country: United States
State: Ohio
County: Guernsey
Municipality: Adams Township
Operator Name: PAVLIK CHARLES E
Well Pad ID:
Farm/Lease Name: MEHAFFEY FRANCIS
License Status: Final Restoration
License Date: 2009-12-30
Spud Date: 2010-01-29
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1970-06-11
Well Total Depth: 1251.00 ft
Configuration: Vertical
Latitude: 40.030000
Longitude: -81.670000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1970-03-23 OTD: 4970' IN CLINTON

ATTEMPTED REOPEN 1/10/2010. ENCOUNTERED CEMENT PLUG AT 1133'. PLUGGED TO SURFACE.

Completed 1970-06-11 OTD: 4970' IN CLINTON

ATTEMPTED REOPEN 1/10/2010. ENCOUNTERED CEMENT PLUG AT 1133'. PLUGGED TO SURFACE.

Reached Total Depth 1970-06-11 OTD: 4970' IN CLINTON

ATTEMPTED REOPEN 1/10/2010. ENCOUNTERED CEMENT PLUG AT 1133'. PLUGGED TO SURFACE.

CO 1981-08-26 218 ENERGY RECOVERY CO GeoDate 8/26/81
Change of Owner 2009-12-15 Operator changed from 218, ENERGY RECOVERY CO to 2244, PAVLIK CHARLES E
APP 2009-12-30 Proposed Formations:BEREA/ORISKANY, Issued Date:12/30/2009, Expired Date:12/30/2010 6:00:00 AM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged/Abandoned 2010-01-30 OTD: 4970' IN CLINTON

ATTEMPTED REOPEN 1/10/2010. ENCOUNTERED CEMENT PLUG AT 1133'. PLUGGED TO SURFACE.

Completion Report Received 2010-04-15 OTD: 4970' IN CLINTON

ATTEMPTED REOPEN 1/10/2010. ENCOUNTERED CEMENT PLUG AT 1133'. PLUGGED TO SURFACE.

Construction Permit Expires 2010-12-30 OTD: 4970' IN CLINTON

ATTEMPTED REOPEN 1/10/2010. ENCOUNTERED CEMENT PLUG AT 1133'. PLUGGED TO SURFACE.

Record Last Modified 2013-03-14 OTD: 4970' IN CLINTON

ATTEMPTED REOPEN 1/10/2010. ENCOUNTERED CEMENT PLUG AT 1133'. PLUGGED TO SURFACE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4758 4772 0
4758 4772 0
4758 4772 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 500 Bbl 8450

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2119520656 2010-1-8 0:00:0 DD No Violations
1273272850 2010-05-10 Final Restoration No Violations Restoration work at site satisfactory pit was filled in and site reclaimed and vegetation has been established.
1790286284 2009-12-24 Drill / Deepen / Reopen No Violations Cable tool rig moving in on site for reopen project,they dug up existing 8 casing and removed cap and installed 8 valve on casing and owner stated that as soon as permit is issued he will begin drilling out top plug.
2119520656 2010-01-08 Drill / Deepen / Reopen No Violations Driller started to drill top plug 12/30/09,drilling cement plug 1/8/10@410,1/09/10 driller called and stated they encountered Berea plug@1133 shut down for the evening will resume drilling 1/11/10.

For data sources see[5]

References