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34-055-21513

Well Details

Well ID: 34-055-21513
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Country: United States
State: Ohio
County: Geauga
Municipality: Newbury Township
Operator Name: INDUSTRY STANDARD SUPPLIES INC
Well Pad ID:
Farm/Lease Name: BULLARD UNIT
License Status: Producing
License Date: 1987-12-23
Spud Date: 1988-01-28
Spud Drilling Contractor: [[EPC [EASTERN PETROLEUM]]]
Final Drill Date: 1988-02-01
Well Total Depth: 4080.00 ft
Configuration: Vertical
Latitude: 41.470000
Longitude: -81.210000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1987-12-23 Issued Date 12/23/87 Expired Date 12/22/88 Acres 0027180 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04080 Proposed Drill Depth 04080
Original Spud 1988-01-28
Completed 1988-02-01
Reached Total Depth 1988-02-01
CO 1988-03-17 1840 GRIMSBY EXPLORATION INC GeoDate 12/23/87
Completion Report Received 1988-04-13
Construction Permit Expires 1988-12-22
Change of Owner 2018-10-01 Operator changed from 1840, GRIMSBY EXPLORATION INC to 8104, INDUSTRY STANDARD SUPPLIES INC
Record Last Modified 2018-10-01

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3887 3902 9
2006-09-11 3908 3921 1
3887 3902 9
3887 3902 9
2006-09-11 3930 3933 7

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 500 Gal 0 FE, BREAKDOWN 1015 PSI; AVG. TREATMENT 1689 PSI, AVG. RATE 30 BPM; ISIP 1285.
H2O 0 67795 Gal 50000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 GRIMSBY EXPLORATION INC 12942.00 269.00 365
1990 GRIMSBY EXPLORATION INC 9536.00 87.00 365
1991 EUREKA NATURAL G&PET CORP 6721.00 97.00 365
1992 GRIMSBY EXPLORATION INC 4023.00 96.00 365
1993 GRIMSBY EXPLORATION INC 3167.00 96.00 365
1994 GRIMSBY EXPLORATION INC 2576.00 90.00 365
1995 GRIMSBY EXPLORATION INC 2168.00 72.00 365
1996 GRIMSBY EXPLORATION INC 1504.00 37.00 365
1997 GRIMSBY EXPLORATION INC 1569.00 0.00 365
1998 GRIMSBY EXPLORATION INC 1666.00 103.00 365
1999 GRIMSBY EXPLORATION INC 1296.00 0.00 365
2000 GRIMSBY EXPLORATION INC 1080.00 87.00 365
2001 GRIMSBY EXPLORATION INC 1074.00 54.00 365
2002 GRIMSBY EXPLORATION INC 1088.00 0.00 365
2003 GRIMSBY EXPLORATION INC 886.00 0.00 365
2004 GRIMSBY EXPLORATION INC 524.00 56.00 365
2005 GRIMSBY EXPLORATION INC 623.00 23.00 365
2006 GRIMSBY EXPLORATION INC 293.00 0.00 365
2007 GRIMSBY EXPLORATION INC 729.00 0.00 365
2008 GRIMSBY EXPLORATION INC 575.00 0.00 365
2009 GRIMSBY EXPLORATION INC 363.00 0.00 365
2010 GRIMSBY EXPLORATION INC 522.00 58.00 365
2015 GRIMSBY EXPLORATION INC 546.00 0.00 365
2016 GRIMSBY EXPLORATION INC 438.00 21.00 365
2017 GRIMSBY EXPLORATION INC 364.00 15.00 365
2018 INDUSTRY STANDARD SUPPLIES INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 GRIMSBY EXPLORATION INC Brine 0 365
1990 GRIMSBY EXPLORATION INC Brine 0 365
1991 EUREKA NATURAL G&PET CORP Brine 0 365
1992 GRIMSBY EXPLORATION INC Brine 68 365
1993 GRIMSBY EXPLORATION INC Brine 0 365
1994 GRIMSBY EXPLORATION INC Brine 0 365
1995 GRIMSBY EXPLORATION INC Brine 0 365
1996 GRIMSBY EXPLORATION INC Brine 67 365
1997 GRIMSBY EXPLORATION INC Brine 0 365
1998 GRIMSBY EXPLORATION INC Brine 80 365
1999 GRIMSBY EXPLORATION INC Brine 0 365
2000 GRIMSBY EXPLORATION INC Brine 65 365
2001 GRIMSBY EXPLORATION INC Brine 0 365
2002 GRIMSBY EXPLORATION INC Brine 0 365
2003 GRIMSBY EXPLORATION INC Brine 0 365
2004 GRIMSBY EXPLORATION INC Brine 0 365
2005 GRIMSBY EXPLORATION INC Brine 0 365
2006 GRIMSBY EXPLORATION INC Brine 0 365
2007 GRIMSBY EXPLORATION INC Brine 0 365
2008 GRIMSBY EXPLORATION INC Brine 0 365
2009 GRIMSBY EXPLORATION INC Brine 0 365
2010 GRIMSBY EXPLORATION INC Brine 0 365
2015 GRIMSBY EXPLORATION INC Brine 0 365
2016 GRIMSBY EXPLORATION INC Brine 0 365
2017 GRIMSBY EXPLORATION INC Brine 0 365
2018 INDUSTRY STANDARD SUPPLIES INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0836700926 2018-01-10 UrbanProduction Wells No Violations I conducted an order follow- up inspection on this well to see if the well was in production. The well was equipped with a plunger lift assembly and the annulus and flow line valves were closed. There was a domestic line with a meter and a regulator off of the 4.5 inch casing. The valve on the domestic line was open. I contacted Swallen, Lawhun and Co. who is the firm that does the accounting on behalf of Grimsby Exploration, Inc. and spoke with Kristie Lear, regarding liability insurance. Ms. Lear forwarded a copy of the liability insurance to me, which I forwarded to DOGRM, Surety and Bonding section.
1497886622 2017-06-19 UrbanProduction Wells Violations Noted I conducted an inspection on this well as a request from landowner, Luke Reed. Mr. Reed indicated that the well is leaking and wanted it inspected. The well is located on his property and was equipped with a plunger lift assembly. Valves were closed on the wellhead but off of the 4.5 inch casing, was a domestic line with one regulator. Valves were open on the domestic line. The 4.5 inch casing above the hammer union and below the gate valve on the tubing has holes in it and is leaking gas. The well casing has been clamped but the leak has not stopped or been repaired. The tank battery consisted of one 210 BBL production tank, one 100 BBL brine tank and a mechanical separator. Valves on the separator were open and the chart dated 6/5/17 showed production. The 210 BBL tank had holes in the side of it and needs removed/replaced. The tank valves were equipped with flat plugs. The tank battery was diked and had legible signage. The lease access was stable. Per ORC 1509.12 the well needs repaired immediately.
1502305874 2017-08-09 UrbanProduction Wells No Violations I conducted a compliance notice follow up inspection for compliance notice inspection 1497886622. The well casing has been clamped and the leak has stopped. There was no audible or visible leak at the time of this inspection. Compliance notice can be closed.
1859888218 2013-10-15 UrbanProduction Wells No Violations My inspection found the tank battery to be in good repair. The tank battery consists of a 210 BBL production tank, a 100 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. The company has not reported production for 2011 and 2012. I will contact the company about the issue.
1892857189 2011-09-29 Production Wells No Violations Tank battery has one 210 barrel production tank, one 100barrel brine tank and a mechincal separator. Tank battery needs painted, operator will be contacted.
836700926 2018-1-10 0:00: UP No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1497886622 US-OH-114045 2017-09-01 Defective casing, leaking well

For data sources see[9]

References