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34-055-20877

Well Details

Well ID: 34-055-20877
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Country: United States
State: Ohio
County: Trumbull
Municipality: Farmington Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: HUNT GARY
License Status: Producing
License Date: 1984-06-25
Spud Date: 1984-06-26
Spud Drilling Contractor: PERKINS DRLG
Final Drill Date: 1984-07-02
Well Total Depth: 4203.00 ft
Configuration: Vertical
Latitude: 41.390000
Longitude: -81.000000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-06-25 9 EDC GeoDate 6/25/84
Oil and Gas 1984-06-25 Issued Date 6/25/84 Expired Date 12/22/84 Acres 0093570 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04203 Proposed Drill Depth 04203
Original Spud 1984-06-26
Completed 1984-07-02
Reached Total Depth 1984-07-02
Completion Report Received 1984-09-07
Construction Permit Expires 1984-12-22
Change of Owner 2008-07-21 Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
Change of Owner 2017-05-01 Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2017-05-01

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3990 4110 0
3990 4110 0
2006-09-11 4030 4060 16
4030 4060 16
3990 4110 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 72600 Gal 78000 FRAC: H2O,SAND,N2
N2 0 160 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS 373.00 292.00 0
1985 POWER GAS MARKETING & TRANS 1754.00 654.00 365
1986 ATWOOD ENERGY INC 3637.00 432.00 365
1987 POWER GAS MARKETING & TRANS 3213.00 280.00 365
1988 POWER GAS MARKETING & TRANS 2214.00 164.00 365
1989 POWER GAS MARKETING & TRANS 1468.00 159.00 365
1990 POWER GAS MARKETING & TRANS 2765.00 215.00 365
1991 POWER GAS MARKETING & TRANS 1041.00 117.00 365
1992 ATWOOD RESOURCES INC 1376.00 0.00 365
1993 POWER GAS MARKETING & TRANS 2964.00 178.00 365
1994 POWER GAS MARKETING & TRANS 2876.00 97.00 0
1995 POWER GAS MARKETING & TRANS 1984.00 90.00 0
1996 POWER GAS MARKETING & TRANS 2456.00 162.00 0
1997 POWER GAS MARKETING & TRANS 2406.00 132.00 365
1998 POWER GAS MARKETING & TRANS 2175.00 74.00 365
1999 POWER GAS MARKETING & TRANS 1728.00 88.00 365
2000 POWER GAS MARKETING & TRANS 1893.00 88.00 365
2001 POWER GAS MARKETING & TRANS 1162.00 0.00 365
2002 POWER GAS MARKETING & TRANS 961.00 82.00 365
2003 POWER GAS MARKETING & TRANS 1269.00 75.00 365
2004 POWER GAS MARKETING & TRANS 1831.00 79.00 365
2005 POWER GAS MARKETING & TRANS 1359.00 87.00 365
2006 EXCO - NORTH COAST ENERGY INC 767.00 63.00 365
2007 EXCO - NORTH COAST ENERGY INC 1077.00 0.00 365
2008 EXCO - NORTH COAST ENERGY INC 915.00 43.00 366
2009 EXCO - NORTH COAST ENERGY INC 659.00 0.00 365
2010 ENERVEST OPERATING LLC 1156.00 63.00 365
2011 ENERVEST OPERATING LLC 1345.00 50.00 0
2012 ENERVEST OPERATING LLC 713.00 0.00 366
2013 ENERVEST OPERATING LLC 720.00 31.00 365
2014 ENERVEST OPERATING LLC 925.00 23.00 365
2015 ENERVEST OPERATING LLC 729.00 27.00 365
2016 ENERVEST OPERATING LLC 382.00 30.00 366
2017 M & R INVESTMENTS OHIO LLC 261.00 0.00 365
2018 M & R INVESTMENTS OHIO LLC 68.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS Brine 54 0
1985 POWER GAS MARKETING & TRANS Brine 95 365
1986 ATWOOD ENERGY INC Brine 400 365
1987 POWER GAS MARKETING & TRANS Brine 226 365
1988 POWER GAS MARKETING & TRANS Brine 226 365
1989 POWER GAS MARKETING & TRANS Brine 85 365
1990 POWER GAS MARKETING & TRANS Brine 263 365
1991 POWER GAS MARKETING & TRANS Brine 84 365
1992 ATWOOD RESOURCES INC Brine 70 365
1993 POWER GAS MARKETING & TRANS Brine 209 365
1994 POWER GAS MARKETING & TRANS Brine 156 0
1995 POWER GAS MARKETING & TRANS Brine 120 0
1996 POWER GAS MARKETING & TRANS Brine 158 0
1997 POWER GAS MARKETING & TRANS Brine 233 365
1998 POWER GAS MARKETING & TRANS Brine 59 365
1999 POWER GAS MARKETING & TRANS Brine 125 365
2000 POWER GAS MARKETING & TRANS Brine 0 365
2001 POWER GAS MARKETING & TRANS Brine 203 365
2002 POWER GAS MARKETING & TRANS Brine 166 365
2003 POWER GAS MARKETING & TRANS Brine 140 365
2004 POWER GAS MARKETING & TRANS Brine 97 365
2005 POWER GAS MARKETING & TRANS Brine 7 365
2006 EXCO - NORTH COAST ENERGY INC Brine 35 365
2007 EXCO - NORTH COAST ENERGY INC Brine 0 365
2008 EXCO - NORTH COAST ENERGY INC Brine 142 366
2009 EXCO - NORTH COAST ENERGY INC Brine 100 365
2010 ENERVEST OPERATING LLC Brine 23 365
2011 ENERVEST OPERATING LLC Brine 100
2012 ENERVEST OPERATING LLC Brine 0 366
2013 ENERVEST OPERATING LLC Brine 36 365
2014 ENERVEST OPERATING LLC Brine 89 365
2015 ENERVEST OPERATING LLC Brine 67 365
2016 ENERVEST OPERATING LLC Brine 67 366
2017 ENERVEST OPERATING LLC Brine 56 193
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1092693560 2018-8-21 0:00: PW No Violations
-1514033419 2018-10-11 0:00 PW No Violations
-629416174 2018-10-12 0:00 PW No Violations
-861354796 2015-3-25 0:00: PW No Violations
0051570224 2003-06-19 Production Wells No Violations well & TB
0629416174 2018-10-12 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice 1092693560 and complaint #5937. I was on location with Bill Fitzmartin from M&R Investments at the time of this inspection to confirm the remedial work on the dike has been completed. The dike has been completely installed, all new soil and stone had been previously emplaced within the diked battery and the 100 BBL tank has been reconnected to the mechanical separator. New signage has been installed at the tank battery. I spoke with landowner William Dieterle regarding the site cleanup and closure of complaint. Compliance notice closed.
0861354796 2015-03-25 Production Wells No Violations My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair. The tank battery consists of a 100 BBL production tank and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition.
1092693560 2018-08-21 Production Wells Violations Noted I conducted an inspection on this well regarding complaint #5937 with DOGRM-Emergency Operations Coordinator Fred Romeo. Landowner Mr. William Dieterle stated that a previous release of oil had occurred inside the tank battery and that cleanup efforts had not been done correctly. At the time of this inspection, the well was equipped with a plunger lift assembly and was not in production. The gate valve on the tubing and flow line valve were closed. The tank battery consisted of one 100 BBL tank and a mechanical separator. Valves on the separator were open. The tank battery had standing water and a sheen was observed on the water. The water in the dike was tested with a high range Quantab. No reading was obtained on the Quantab. Soil samples were taken using a soil auger and residual oil was observed in the stone and soil sample. The dike had been cut to release water on the north side, and outside of the diked battery, oily sheen was observed on the standing water. North of the tank battery was vegetated with grass which was observed to be stressed. The signage was located at the tank battery but needed to be updated to reflect the current owner information. Bill Fitzmartin from M&R Investments was contacted regarding the findings of residual oil in the battery and signage. Mr. Fitzmartin stated that a tank did overflow and M&R Investments had intially cleaned the area but needed to come back to the site to finish the cleanup. Mr. Fitzmartin also stated that landowner Mr. Dieterle would not allow M&R access to his property to complete the cleanup activities.

M&R Investments needs to: 1) Cleanup the water and residual oil within and adjacent to the tank battery 2) Dispose of properly any impacted soil/stone within and adjacent to the tank battery 3) Install signage

1168760564 2018-08-21 Production Wells No Violations I was on location with DOGRM-Emergency Operations Coordinator, Fred Romeo regarding a previous release at this location. At the time of this inspection, landowner, William Dieterle requested an inspection of the well and tank battery. Mr. Dieterle stated that the previous cleanup efforts from a tank release into the tank battery by M&R Investments, was not done properly. There was not an active leak at the time of this inspection. The well was equipped with a plunger lift assembly and not in production at the time of this inspection. The tank battery consisted of one 100 BBL tank and a mechanical separator. Inside the diked battery, standing water was noted. A high range Quantab test was taken of the water and no chlorides were present. Mr. Romeo used a soil auger to gather samples of the soil and stone within the battery. Residual oil was present each time the soil/stone medium was sampled with the soil auger. The north side of the dike needed to be rebuilt. The area north of the dike showed some stressed vegetation. Bill Fitzmartin from M&R Investments was contacted with regards to the tank battery condition and findings of the residual oil. Mr. Fitzmartin stated that the company would come out to the site and assess what cleanup would need conducted. Informed Mr. Dieterle that M&R Investments would come out to the site and conduct cleanup accordingly.
1478882473 2003-06-19 Production Wells No Violations Well and TB 210 BBLS / Buried septic tank
1514033419 2018-10-11 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice 1092693560 and complaint #5937. The remedial work that was still needed to complete the tank battery area was finishing the rebuilding of the dike. I was on location with Pete Lower, subcontractor for M&R Investments who stated that more soil was needed to complete the installation of the dike around the tank battery. The soil was in transit at the time of this inspection. Another inspection will be conducted once the dike has been completed.
1539282584 2018-10-10 Production Wells No Violations I was on location with Pete Lower, subcontractor for M&R Investments Ohio to conduct the cleanup of the tank battery residual oil, for complaint #5937 and compliance notice 1092693560. The remedial work that was conducted at the tank battey location consisted of removing the 100 BBL tank out of the battery. The tank was checked for integrity and found to be intact and the bottom integrity of the tank had not been compromised. Removal of the existing stone and soil that contained the residual oil was placed into a truck to be offloaded at a proper disposal facility. New soil and stone was emplaced into the tank battery and the dike was partially rebuilt. More soil was needed to complete the dike and the reattachment and installation of the 100 BBL tank would also need to be completed. I spoke with landowner William Dieterle on location and kept him apprised of the ongoing cleanup activity throughout the day. I will return the following day, 10/11/2018 to conduct another inspection once the cleanup has been completed.
2106224027 2018-09-12 Production Wells No Violations I met on site with Bill Fitzmartin of M&R Investments and landowner William Dieterle to discuss what actions will be needed to conduct the final cleanup at the tank battery regarding complaint #5937 and compliance notice 1092693560. It was discussed that M&R Investments would remove the existing 100 BBL tank and stone/soil medium beneath it. Any oily stone/soil would be removed and disposed of properly from the tank battery and the dike would be rebuilt accordingly. Mr. Fitzmartin stated that he would setup a date for the cleanup and would contact myself and the landowner when the cleanup would be conducted.
51570224 2003-6-19 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1092693560 US-OH-102162 2018-11-16 9-9-05(A)10 Failure to legibly identify well
1092693560 US-OH-102163 2018-11-16 9-9-05(A)9 No SPCC dike/or failure to keep dike free of water or oil

For data sources see[9]

References