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34-055-20227

Well Details

Well ID: 34-055-20227
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Country: United States
State: Ohio
County: Geauga
Municipality: Parkman Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: WEAVER M
License Status: Producing
License Date: 1982-07-22
Spud Date: 1976-04-30
Spud Drilling Contractor:
Final Drill Date: 1977-08-19
Well Total Depth: 4226.00 ft
Configuration: Vertical
Latitude: 41.410000
Longitude: -81.050000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1976-04-30
Completed 1977-08-19
Reached Total Depth 1977-08-19
CO 1982-07-22 9 EDC GeoDate 7/22/82
Correction to Well 2007-05-04 UNIT SIZE REDUCED TO 100.71 ACRES.
Correction to Well 2008-03-14 UNIT SIZE DECREASED TO 76.64 ACRES.
Change of Owner 2008-07-21 Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
Record Last Modified 2019-06-14

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4097 4181 18
4097 4181 18
4097 4181 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1250 Bbl 47250

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS 1531.00 131.00 0
1985 POWER GAS MARKETING & TRANS 1414.00 131.00 365
1986 POWER GAS MARKETING & TRANS 742.00 57.00 365
1987 POWER GAS MARKETING & TRANS 827.00 70.00 365
1988 POWER GAS MARKETING & TRANS 965.00 71.00 365
1989 POWER GAS MARKETING & TRANS 576.00 68.00 365
1990 POWER GAS MARKETING & TRANS 867.00 71.00 365
1991 POWER GAS MARKETING & TRANS 72.00 56.00 365
1992 POWER GAS MARKETING & TRANS 1250.00 0.00 365
1993 POWER GAS MARKETING & TRANS 1163.00 52.00 365
1994 POWER GAS MARKETING & TRANS 1155.00 58.00 0
1995 POWER GAS MARKETING & TRANS 1306.00 49.00 0
1996 POWER GAS MARKETING & TRANS 1112.00 111.00 0
1997 POWER GAS MARKETING & TRANS 1290.00 80.00 365
1998 POWER GAS MARKETING & TRANS 1222.00 66.00 365
1999 POWER GAS MARKETING & TRANS 800.00 66.00 365
2000 POWER GAS MARKETING & TRANS 864.00 66.00 339
2001 POWER GAS MARKETING & TRANS 834.00 63.00 344
2002 POWER GAS MARKETING & TRANS 872.00 49.00 365
2003 POWER GAS MARKETING & TRANS 424.00 62.00 365
2004 POWER GAS MARKETING & TRANS 775.00 69.00 365
2005 POWER GAS MARKETING & TRANS 1224.00 51.00 365
2006 EXCO - NORTH COAST ENERGY INC 1142.00 187.00 365
2007 EXCO - NORTH COAST ENERGY INC 1036.00 37.00 365
2008 EXCO - NORTH COAST ENERGY INC 832.00 0.00 366
2009 ENERVEST OPERATING LLC 703.00 0.00 92
2010 ENERVEST OPERATING LLC 557.00 69.00 365
2011 ENERVEST OPERATING LLC 700.00 0.00 0
2012 ENERVEST OPERATING LLC 848.00 72.00 366
2013 ENERVEST OPERATING LLC 834.00 0.00 365
2014 ENERVEST OPERATING LLC 666.00 56.00 365
2015 ENERVEST OPERATING LLC 716.00 0.00 365
2016 ENERVEST OPERATING LLC 558.00 70.00 209
2017 ENERVEST OPERATING LLC 50.00 0.00 14
2018 ENERVEST OPERATING LLC 950.00 46.00 218

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS Brine 13 0
1985 POWER GAS MARKETING & TRANS Brine 19 365
1986 POWER GAS MARKETING & TRANS Brine 5 365
1987 POWER GAS MARKETING & TRANS Brine 5 365
1988 POWER GAS MARKETING & TRANS Brine 5 365
1989 POWER GAS MARKETING & TRANS Brine 2 365
1990 POWER GAS MARKETING & TRANS Brine 0 365
1991 POWER GAS MARKETING & TRANS Brine 2 365
1992 POWER GAS MARKETING & TRANS Brine 6 365
1993 POWER GAS MARKETING & TRANS Brine 1 365
1994 POWER GAS MARKETING & TRANS Brine 5 0
1995 POWER GAS MARKETING & TRANS Brine 4 0
1996 POWER GAS MARKETING & TRANS Brine 9 0
1997 POWER GAS MARKETING & TRANS Brine 60 365
1998 POWER GAS MARKETING & TRANS Brine 40 365
1999 POWER GAS MARKETING & TRANS Brine 50 365
2000 POWER GAS MARKETING & TRANS Brine 0 339
2001 POWER GAS MARKETING & TRANS Brine 58 344
2002 POWER GAS MARKETING & TRANS Brine 45 365
2003 POWER GAS MARKETING & TRANS Brine 0 365
2004 POWER GAS MARKETING & TRANS Brine 25 365
2005 POWER GAS MARKETING & TRANS Brine 44 365
2006 EXCO - NORTH COAST ENERGY INC Brine 34 365
2007 EXCO - NORTH COAST ENERGY INC Brine 68 365
2008 EXCO - NORTH COAST ENERGY INC Brine 74 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 365
2010 ENERVEST OPERATING LLC Brine 0 365
2011 ENERVEST OPERATING LLC Brine 5
2012 ENERVEST OPERATING LLC Brine 9 366
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 2 365
2015 ENERVEST OPERATING LLC Brine 0 365
2016 ENERVEST OPERATING LLC Brine 0 209
2017 ENERVEST OPERATING LLC Brine 0 14
2018 ENERVEST OPERATING LLC Brine 0 218

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1312459435 2011-08-03 Production Wells No Violations On site for oil leak at the separator. At approximately 16:00 the resident was mowing the area around the separator. The flow line coming into the separator from the well was hit with the mower. The hit caused a 2 inch lateral cut in the side of the flow line. The release of pressure from the flow lined threw the mower 20 feet west. No injuries to operator of the mower reported. At 16:45 Parkman Fire Department was on scene and shut well down at the demco valve. Pumper on scene shortly after 16:45, jumper adjusted demco valve to completely shut well off. Operator contacted me 17:27 in regards to release. I was on scene at 18:00. Pumper had placed boom in the drainage swale west of the release to contain oil. Pumper had constructed a temporary dam west of the boom as a secondary containment. Oil release was stabilized at this time. The swale runs east and west adjacent to a pasture. The swale has minimal fall, sump and dam will be constructed in the swale to gather residual oil. 19:30 large containment dam had been built by contractor, additional booms were in place. Grossly contaminated soil had been gathered and stockpiled on site. Sprayed vegetation had been cut and stockpiled. Well was repaired at 20:45. Operator will: 1. Remove grossly contaminated soil from location. 2. Remove cut vegetation from location. 3. Maintain sump to gather free crude oil. 4. Apply peat sorb and mix into soil of minimally contamination to add in the break down of the crude oil. 5. Wash down stone lease road with fresh water into sump to remove free crude from the stone. If free crude remains, remove stone from location. 6. During clean up, the removal of the cement brine vault in the tank battery was requested. Vault is no longer in use. The vault was open and flooded with fresh water. Residual oil was coming out of the tank. 7. Remove from site any contaminated soil from around or under the vault
1371527582 2013-04-04 Production Wells No Violations My inspection found the well to be equipped with a plunger lift unit. The tank battery consists of a 100 BBL production tank and a mechanical separator. The tank battery was in need of a dike and there was no identification sign. I spoke with Joe Phillips from Enervest about getting the well repaired. The lease road is in stable condition.

For data sources see[9]

References