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Well ID: 34-031-22883 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Crawford Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: WILSON WW & DG ETAL | |
License Status: Producing | |
License Date: 2018-08-30 | |
Spud Date: 1976-10-22 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-11-10 | |
Well Total Depth: 6695.00 ft | |
Configuration: Vertical | |
Latitude: 40.410000 | |
Longitude: -81.720000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-10-18 | 9 EDC GeoDate 10/18/76 |
Original Spud | 1976-10-22 | PD.NAT. 2.150MCFG & TRACE/OIL |
Completed | 1976-11-10 | PD.NAT. 2.150MCFG & TRACE/OIL |
Reached Total Depth | 1976-11-10 | PD.NAT. 2.150MCFG & TRACE/OIL |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2017-05-01 | Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC |
APP | 2018-08-30 | Proposed Formations:ROSE RUN, Issued Date:8/30/2018, Expired Date:8/29/2020 12:00:00 PM, Drilling unit acres:222, Proposed Well Type:OG, Proposed Well Class: |
Record Last Modified | 2018-09-06 | PD.NAT. 2.150MCFG & TRACE/OIL |
Construction Permit Expires | 2020-08-29 | PD.NAT. 2.150MCFG & TRACE/OIL |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | NO TREATMENT; OPEN HOLE |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-107187879 | 2019-8-15 0:00: | PW | No Violations | 0.50 |
-1477475286 | 2020-10-9 0:00: | PW | No Violations | 0.80 |
1135267879 | 2005-12-22 | Production Wells | Violations Noted | Well idle . No identification for well . Last production reported 1995 . |
1141922593 | 2006-03-09 | Production Wells | No Violations | Follow up for idle well and identification . Storage tanks identified . Well shut in @ well head . |
1152206442 | 2006-07-06 | Production Wells | No Violations | Well head is shut in , separator is shut in . Well isnt in production . Identification is posted on storage tank . Took pictures of well and separator . REQUEST CHIRFS ORDER TO PLUG . |
1184957072 | 2007-07-20 | Production Wells | No Violations | Follow up inspection for idle well . All valves on well head are shut in , took pictures of valves , well is idle . Reports started this inspection for chiefs order to plug . |
1187102920 | 2007-08-14 | Production Wells | No Violations | Well has been plumed up for production , new chart for gas sales hooked up . Well isnt on line this inspection . May be waiting for gas contract . Chiefs order has been requested . |
1315137445 | 2018-10-25 | Production Wells | No Violations | On the day of my inspection I found that there were fresh vehicle tracks back to the well. There was a new circle chart in place but it was not dated and it showed minimal gas production. The well is equipped with a plunger lift and the main Demco valve on the tubing was closed. The casing valve was open, and they were feeding the casing gas through a vertical drip bottle and back into the tubing line. The gauge showed 120 pounds on the drip. I called John Raber with M&R to ask what the status was. John said that they had a rig in to swab the well but they still couldnt get it to cycle. He claimed that he was going to contract a dozer and another swab rig to clean it out again. I told him that a plugging permit was issued on 8/30/18, which he was not aware of. John said that he would look into it and get back to me, because he has not heard that they were going to plug the well. |
1523634133 | 2018-04-13 | Production Wells | Violations Noted | I received a phone call from Allen Yoder to request and inspection on this well. Mr. Yoder claimed that he recently purchased the property and he was concerned that the well was idle and leaking. He claimed that the chart had not been changed in three years. On the day of my inspection I found that the well was equipped as a gas well with a plunger lift. The lines were connected at the wellhead. The Demco valve on the tubing was open and there was another Demco valve off of the casing that was open back to the tubing. The gate valve to the flow line back to the separator was closed. The tubing was rusted just above the wellhead and there was gas leaking from that general area. I found no fluid leaks from the wellhead and no contamination on the ground around the wellhead. The production equipment consisted of one 210 barrel steel tank, one 100 barrel steel tank and one horizontal separator in an earthen dike. The 100 barrel tank was corroded with several large holes in the side. It was empty and not in use. I did not find any fluid leaks from the tanks or contamination on the ground around the production equipment. Correct, legible identification was posted on the 210 tank. The chart at the separator was dated 5/23/15. The access road back to the well and tanks did not show any signs of recent use. The annual production report for 2016 shows zero (0) cubic feet of gas and zero (0) barrels of oil. The 2017 annual production report was not listed. There is no visible evidence that this well is currently being produced. The valve from the wellhead to the production equipment was closed and the chart has not been changed in years. The tubing is so rusted that it is starting to leak gas. There are no signs of any recent vehicle traffic back to the well and tanks. The well owner/operator shall submit a written plugging schedule to Chris Grimm at 5880 Memory Rd, Zanesville, OH 43701 within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/op |
1578583819 | 2020-1-9 0:00:0 | PW | No Violations | 0.70 |
1673902954 | 2018-07-12 | Production Wells | No Violations | I received a phone call from the landowner Allen Yoder to let me know that M&R had put a new chart on the separator, and he thought the well was still leaking gas. On the day of my inspection I found that there was a line clamp on the tubing, just above the hammer union on the casing head. I did not hear any hissing or smell any gas at the time of my inspection. The Demco valve on the tubing was open, but the tubing valve back to the production equipment was closed. The casing line was plumbed in a loop back to the tubing. Both of the valves in the loop were partially opened. The chart showed 20 percent line pressure and there was a 1.000 inch orifice plate installed. The production line on the chart showed no gas production. I called Allen to report what I had found. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1135267879 | US-OH-103426 | 2005-12-22 | Failure to legibly identify well | |
1135267879 | US-OH-103427 | 2005-12-22 | Well shall be plugged | |
1523634133 | US-OH-114539 | 2018-04-16 | Well insufficiently equipped to prevent escape of oil and gas | |
1523634133 | US-OH-114540 | 2018-04-16 | Well shall be plugged |
For data sources see[8]