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34-031-22883

Well Details

Well ID: 34-031-22883
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Country: United States
State: Ohio
County: Coshocton
Municipality: Crawford Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: WILSON WW & DG ETAL
License Status: Producing
License Date: 2018-08-30
Spud Date: 1976-10-22
Spud Drilling Contractor:
Final Drill Date: 1976-11-10
Well Total Depth: 6695.00 ft
Configuration: Vertical
Latitude: 40.410000
Longitude: -81.720000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-10-18 9 EDC GeoDate 10/18/76
Original Spud 1976-10-22 PD.NAT. 2.150MCFG & TRACE/OIL
Completed 1976-11-10 PD.NAT. 2.150MCFG & TRACE/OIL
Reached Total Depth 1976-11-10 PD.NAT. 2.150MCFG & TRACE/OIL
Change of Owner 2008-07-21 Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
Change of Owner 2017-05-01 Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC
APP 2018-08-30 Proposed Formations:ROSE RUN, Issued Date:8/30/2018, Expired Date:8/29/2020 12:00:00 PM, Drilling unit acres:222, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2018-09-06 PD.NAT. 2.150MCFG & TRACE/OIL
Construction Permit Expires 2020-08-29 PD.NAT. 2.150MCFG & TRACE/OIL

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NO TREATMENT; OPEN HOLE

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS 15023.00 0.00 0
1985 POWER GAS MARKETING & TRANS 11687.00 0.00 365
1987 POWER GAS MARKETING & TRANS 6785.00 0.00 365
1988 POWER GAS MARKETING & TRANS 3641.00 0.00 365
1989 POWER GAS MARKETING & TRANS 4037.00 0.00 365
1990 POWER GAS MARKETING & TRANS 2429.00 0.00 365
1991 POWER GAS MARKETING & TRANS 1911.00 0.00 365
1992 POWER GAS MARKETING & TRANS 1894.00 0.00 365
1993 POWER GAS MARKETING & TRANS 186.00 0.00 365
1994 POWER GAS MARKETING & TRANS 82.00 0.00 0
1995 POWER GAS MARKETING & TRANS 41.00 0.00 0
1996 POWER GAS MARKETING & TRANS 3.00 0.00 0
1997 POWER GAS MARKETING & TRANS 0.00 0.00 0
1998 POWER GAS MARKETING & TRANS 0.00 0.00 0
1999 POWER GAS MARKETING & TRANS 0.00 0.00 0
2000 POWER GAS MARKETING & TRANS 0.00 0.00 0
2001 POWER GAS MARKETING & TRANS 0.00 0.00 0
2002 POWER GAS MARKETING & TRANS 0.00 0.00 0
2003 POWER GAS MARKETING & TRANS 0.00 0.00 0
2004 POWER GAS MARKETING & TRANS 0.00 0.00 0
2005 POWER GAS MARKETING & TRANS 0.00 0.00 0
2006 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2007 EXCO - NORTH COAST ENERGY INC 52.00 0.00 365
2008 EXCO - NORTH COAST ENERGY INC 2859.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 4619.00 0.00 365
2010 ENERVEST OPERATING LLC 5150.00 0.00 365
2011 ENERVEST OPERATING LLC 1244.00 0.00 0
2012 ENERVEST OPERATING LLC 351.00 0.00 366
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 118.00 0.00 60
2016 ENERVEST OPERATING LLC 0.00 0.00 0
2017 M & R INVESTMENTS OHIO LLC 251.00 0.00 365
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 POWER GAS MARKETING & TRANS Brine 0 0
1985 POWER GAS MARKETING & TRANS Brine 0 365
1987 POWER GAS MARKETING & TRANS Brine 116 365
1988 POWER GAS MARKETING & TRANS Brine 124 365
1989 POWER GAS MARKETING & TRANS Brine 0 365
1990 POWER GAS MARKETING & TRANS Brine 0 365
1991 POWER GAS MARKETING & TRANS Brine 96 365
1992 POWER GAS MARKETING & TRANS Brine 9 365
1993 POWER GAS MARKETING & TRANS Brine 0 365
1994 POWER GAS MARKETING & TRANS Brine 0 0
1995 POWER GAS MARKETING & TRANS Brine 6 0
1996 POWER GAS MARKETING & TRANS Brine 0 0
1997 POWER GAS MARKETING & TRANS Brine 0 0
1998 POWER GAS MARKETING & TRANS Brine 0 0
1999 POWER GAS MARKETING & TRANS Brine 78 0
2000 POWER GAS MARKETING & TRANS Brine 0 0
2001 POWER GAS MARKETING & TRANS Brine 0 0
2002 POWER GAS MARKETING & TRANS Brine 0 0
2003 POWER GAS MARKETING & TRANS Brine 0 0
2004 POWER GAS MARKETING & TRANS Brine 0 0
2005 POWER GAS MARKETING & TRANS Brine 0 0
2006 EXCO - NORTH COAST ENERGY INC Brine 0 0
2007 EXCO - NORTH COAST ENERGY INC Brine 0 365
2008 EXCO - NORTH COAST ENERGY INC Brine 61 366
2009 EXCO - NORTH COAST ENERGY INC Brine 43 365
2010 ENERVEST OPERATING LLC Brine 0 365
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 366
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 60
2016 ENERVEST OPERATING LLC Brine 0 0
2017 ENERVEST OPERATING LLC Brine 0 34
2018 M & R INVESTMENTS OHIO LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-107187879 2019-8-15 0:00: PW No Violations 0.50
-1477475286 2020-10-9 0:00: PW No Violations 0.80
1135267879 2005-12-22 Production Wells Violations Noted Well idle . No identification for well . Last production reported 1995 .
1141922593 2006-03-09 Production Wells No Violations Follow up for idle well and identification . Storage tanks identified . Well shut in @ well head .
1152206442 2006-07-06 Production Wells No Violations Well head is shut in , separator is shut in . Well isnt in production . Identification is posted on storage tank . Took pictures of well and separator . REQUEST CHIRFS ORDER TO PLUG .
1184957072 2007-07-20 Production Wells No Violations Follow up inspection for idle well . All valves on well head are shut in , took pictures of valves , well is idle . Reports started this inspection for chiefs order to plug .
1187102920 2007-08-14 Production Wells No Violations Well has been plumed up for production , new chart for gas sales hooked up . Well isnt on line this inspection . May be waiting for gas contract . Chiefs order has been requested .
1315137445 2018-10-25 Production Wells No Violations On the day of my inspection I found that there were fresh vehicle tracks back to the well. There was a new circle chart in place but it was not dated and it showed minimal gas production. The well is equipped with a plunger lift and the main Demco valve on the tubing was closed. The casing valve was open, and they were feeding the casing gas through a vertical drip bottle and back into the tubing line. The gauge showed 120 pounds on the drip. I called John Raber with M&R to ask what the status was. John said that they had a rig in to swab the well but they still couldnt get it to cycle. He claimed that he was going to contract a dozer and another swab rig to clean it out again. I told him that a plugging permit was issued on 8/30/18, which he was not aware of. John said that he would look into it and get back to me, because he has not heard that they were going to plug the well.
1523634133 2018-04-13 Production Wells Violations Noted I received a phone call from Allen Yoder to request and inspection on this well. Mr. Yoder claimed that he recently purchased the property and he was concerned that the well was idle and leaking. He claimed that the chart had not been changed in three years. On the day of my inspection I found that the well was equipped as a gas well with a plunger lift. The lines were connected at the wellhead. The Demco valve on the tubing was open and there was another Demco valve off of the casing that was open back to the tubing. The gate valve to the flow line back to the separator was closed. The tubing was rusted just above the wellhead and there was gas leaking from that general area. I found no fluid leaks from the wellhead and no contamination on the ground around the wellhead. The production equipment consisted of one 210 barrel steel tank, one 100 barrel steel tank and one horizontal separator in an earthen dike. The 100 barrel tank was corroded with several large holes in the side. It was empty and not in use. I did not find any fluid leaks from the tanks or contamination on the ground around the production equipment. Correct, legible identification was posted on the 210 tank. The chart at the separator was dated 5/23/15. The access road back to the well and tanks did not show any signs of recent use. The annual production report for 2016 shows zero (0) cubic feet of gas and zero (0) barrels of oil. The 2017 annual production report was not listed. There is no visible evidence that this well is currently being produced. The valve from the wellhead to the production equipment was closed and the chart has not been changed in years. The tubing is so rusted that it is starting to leak gas. There are no signs of any recent vehicle traffic back to the well and tanks. The well owner/operator shall submit a written plugging schedule to Chris Grimm at 5880 Memory Rd, Zanesville, OH 43701 within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/op
1578583819 2020-1-9 0:00:0 PW No Violations 0.70
1673902954 2018-07-12 Production Wells No Violations I received a phone call from the landowner Allen Yoder to let me know that M&R had put a new chart on the separator, and he thought the well was still leaking gas. On the day of my inspection I found that there was a line clamp on the tubing, just above the hammer union on the casing head. I did not hear any hissing or smell any gas at the time of my inspection. The Demco valve on the tubing was open, but the tubing valve back to the production equipment was closed. The casing line was plumbed in a loop back to the tubing. Both of the valves in the loop were partially opened. The chart showed 20 percent line pressure and there was a 1.000 inch orifice plate installed. The production line on the chart showed no gas production. I called Allen to report what I had found.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1135267879 US-OH-103426 2005-12-22 Failure to legibly identify well
1135267879 US-OH-103427 2005-12-22 Well shall be plugged
1523634133 US-OH-114539 2018-04-16 Well insufficiently equipped to prevent escape of oil and gas
1523634133 US-OH-114540 2018-04-16 Well shall be plugged

For data sources see[8]

References