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Well ID: 34-031-22034 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Tiverton Township | |
Operator Name: W H PATTEN DRILLING CO | |
Well Pad ID: | |
Farm/Lease Name: LLOYD HAWKINS | |
License Status: Final Restoration | |
License Date: 2012-08-09 | |
Spud Date: 1970-11-22 | |
Spud Drilling Contractor: | |
Final Drill Date: 1971-01-20 | |
Well Total Depth: 3374.00 ft | |
Configuration: Vertical | |
Latitude: 40.430000 | |
Longitude: -82.140000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-10-15 | 372 PATTEN W H DRLG CO GeoDate 10/15/70 |
Original Spud | 1970-11-22 | UPDATE LOCATION PER SURVYOR-ALE 03/29/2017. |
Completed | 1971-01-20 | UPDATE LOCATION PER SURVYOR-ALE 03/29/2017. |
Reached Total Depth | 1971-01-20 | UPDATE LOCATION PER SURVYOR-ALE 03/29/2017. |
APP | 2012-08-09 | Proposed Formations:CLINTON, Issued Date:8/9/2012, Expired Date:8/9/2014 12:00:00 PM, Drilling unit acres:106.75, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2013-01-25 | UPDATE LOCATION PER SURVYOR-ALE 03/29/2017. |
Construction Permit Expires | 2014-08-09 | UPDATE LOCATION PER SURVYOR-ALE 03/29/2017. |
Record Last Modified | 2017-03-29 | UPDATE LOCATION PER SURVYOR-ALE 03/29/2017. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1500 Bbl | 18000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | W H PATTEN DRILLING CO | 918.00 | 803.00 | 0 |
1985 | W H PATTEN DRILLING CO | 509.00 | 477.00 | 156 |
1986 | W H PATTEN DRILLING CO | 503.00 | 384.00 | 156 |
1987 | W H PATTEN DRILLING CO | 290.00 | 352.00 | 156 |
1988 | W H PATTEN DRILLING CO | 154.00 | 315.00 | 156 |
1989 | W H PATTEN DRILLING CO | 201.00 | 235.00 | 156 |
1990 | W H PATTEN DRILLING CO | 109.00 | 324.00 | 156 |
1991 | W H PATTEN DRILLING CO | 156.00 | 170.00 | 156 |
1992 | W H PATTEN DRILLING CO | 0.00 | 120.00 | 156 |
1993 | W H PATTEN DRILLING CO | 0.00 | 82.00 | 156 |
1994 | W H PATTEN DRILLING CO | 0.00 | 80.00 | 156 |
1995 | W H PATTEN DRILLING CO | 160.00 | 88.00 | 156 |
1996 | W H PATTEN DRILLING CO | 45.00 | 21.00 | 365 |
1997 | W H PATTEN DRILLING CO | 40.00 | 110.00 | 365 |
1998 | W H PATTEN DRILLING CO | 6.00 | 117.00 | 365 |
1999 | W H PATTEN DRILLING CO | 125.00 | 0.00 | 365 |
2000 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2001 | W H PATTEN DRILLING CO | 0.00 | 112.00 | 365 |
2002 | W H PATTEN DRILLING CO | 0.00 | 37.00 | 365 |
2003 | W H PATTEN DRILLING CO | 0.00 | 72.00 | 365 |
2004 | W H PATTEN DRILLING CO | 0.00 | 24.00 | 365 |
2005 | W H PATTEN DRILLING CO | 0.00 | 109.00 | 365 |
2006 | W H PATTEN DRILLING CO | 0.00 | 117.00 | 365 |
2007 | W H PATTEN DRILLING CO | 0.00 | 116.00 | 365 |
2008 | W H PATTEN DRILLING CO | 0.00 | 111.00 | 365 |
2009 | W H PATTEN DRILLING CO | 0.00 | 102.00 | 365 |
2010 | W H PATTEN DRILLING CO | 0.00 | 79.00 | 365 |
2011 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
2012 | W H PATTEN DRILLING CO | 0.00 | 73.00 | 366 |
2013 | W H PATTEN DRILLING CO | 0.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1022918820 | 2012-12-31 0:00 | PB | No Violations | |
-110026418 | 2013-2-7 0:00:0 | PB | No Violations | |
-1650469919 | 2013-1-8 0:00:0 | PB | No Violations | |
-175881751 | 2013-6-6 0:00:0 | FR | No Violations | |
0110026418 | 2013-02-07 | Plug / Plug Back | No Violations | On the day of my inspection I found that the service rig and all related equipment had been removed from the site. The pit was closed and the soil was graded out to the approximate original contour. The lease road will remain in place at this site, as it is used to access the tank battery for permit 4780. |
0175881751 | 2013-06-06 | Final Restoration | No Violations | On the day of my inspection I found that the former well site was graded out and plowed for agricultural crops. The tank battery and access road are currently in use for permit 4780. There were no leaks and there were no oilfield related materials or debris left at the location. This site passes final restoration. |
0264112941 | 2013-01-03 | Plug / Plug Back | No Violations | On the day of my inspection Timco Wireline Services ran in with a stem to 130 to make sure they could get their guns past the rotted 7 casing top at 86. They repeatedly got hung up when trying to run in with the shots, and eventually lost the weight from the bottom of the gun. The decision was made to run back in with the sewer camera before any further attempts at getting into the 7 casing. |
1022918820 | 2012-12-31 | Plug / Plug Back | No Violations | On the day of my inspection Collins and Rice Well Service pulled 86 of 7 casing from the well. They ran 4.5 casing equipped with an 8 swedge to 85 to hang just above the rotted off 7 casing. Then Billy Patten went in with a wire line sewer camera to determine the extent of the damage at the top of the 7 casing. The decision was made to run in to shoot holes in the 7 casing, shooting 10 holes every 100 from 1000 to 200. |
1164726813 | 2011-01-05 | Production Wells | Violations Noted | Well in capable of production. PLUG OR PRODUCE. Failure to comply may result in bond forfeiture. |
1294247948 | 2011-01-05 | Production Wells | No Violations | Well equipped with separator, 1-100bl. Storage tank and pumping unit with no motor. Well isnt capable of production. |
1353440740 | 2012-11-20 | Plug / Plug Back | No Violations | On the day of my inspection Collins & Rice Well Services moved a service rig onto the location and started to pull rods. |
1354028825 | 2012-11-26 | Plug / Plug Back | No Violations | On the day of my inspection Formation Cementing pumped a 270 cement plug above the Clinton sandstone. The plug was spotted through 1.5 tubing. Circulation was established prior to pumping plug. |
1354200788 | 2012-11-27 | Plug / Plug Back | No Violations | On the day of my inspection Collins & Rice Well Service pulled the tubing and ripped the 5.5 casing at 2100. The knife broke off and they had to call in Timco to try to shoot the casing off. After multiple attempts the casing was shot off at 1800 |
1354566365 | 2012-12-03 | Plug / Plug Back | No Violations | On the day of my inspection Collins & Rice Well Service ran 1.5 tubing to 1650. Formation Cementing broke circulation and pumped a 250 isolation plug above the top of the Big Lime. A copy of the permit was on location, there were no sags or tears in the pit liner and there were no leaks or spills. |
1357672288 | 2013-01-07 | Plug / Plug Back | No Violations | On the day of my inspection Patten Drilling ran a sewer camera down to the top of the 7 casing. The image revealed jagged burrs of metal folded over blocking the opening at the top of the 7 casing. Collins & Rice Well Service ran in with 1.5 tubing coupled with a 3 string mill back down to 1.5. The set up eventually penetrated the burrs and, after working the mill in the tight spot, the top of the 7 casing was opened to approximately 3. |
1357919425 | 2013-01-10 | Plug / Plug Back | No Violations | On the day of my inspection Collins & Rice Well Service had 1.5 tubing set at 965 inside of the 7 casing. Formation Cementing pumped class A cement with 3% gel through the 1.5 tubing until the well was filled to surface. All the tubing was pulled from the well and the 85 of 4.5 casing was pulled from the well. At that point the cement had fallen approximately 50. Formation then filled the well from surface. The cement top was at 10 and falling slowly. We will return on 01/14/2013 to tag the top of the cement plug and determine if further action is needed. |
1358171959 | 2013-01-14 | Plug / Plug Back | No Violations | On the day of my inspection I found that the cement plug had fallen approximately 20 feet. I authorized Patten Drilling to top the well off with sack concrete. |
1358530113 | 2013-01-16 | Administrative Inspection | No Violations | I received a phone call from Billy Patten to report that Collins & Rice Well Services tagged the top of the cement plug at 30 feet. |
1359387363 | 2013-01-25 | Administrative Inspection | No Violations | FOLLOW UP TO CA # 1164726813: I received a phone call from Billy Patten to notify me that the well had been topped off with clay. They were cutting the casing off 36 below grade and capping it with a steel plate. The pit was closed and the rig was moved off location. |
1447302658 | 2011-01-05 | Production Wells | No Violations | FOLLOW UP TO NOV # 1164726813 Well in capable of production. PLUG OR PRODUCE. Failure to comply may result in bond forfeiture. |
1476376567 | 2016-10-12 | Final Restoration | No Violations | On the day of my inspection I escorted surveyor Tom Smith to the plugged well site in order to mark the location with a flagged stake at the final recorded GPS coordinates. I found that the vegetation was well established and there were no signs of erosion. There was no evidence that the plugged well was leaking. |
1650469919 | 2013-01-08 | Plug / Plug Back | No Violations | On the day of my inspection Timco Wireline Services perforated the 7 casing with 10 shots at 960, 875 and 800. Then they used 10 shots every 100 from 800 to 200. |
1804974475 | 2013-01-09 | Plug / Plug Back | No Violations | On the day of my inspection Collins & Rice Well Service was running 1.5 tubing into the well to set up for cement plugs. I met with Terry Rice to discuss the options for setting the cement plugs. |
264112941 | 2013-1-3 0:00:0 | PB | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1164726813 | US-OH-104377 | 2011-01-05 | Well shall be plugged |
For data sources see[8]