If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-031-21138 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.3,"lon":-82.17,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Perry Township | |
Operator Name: VALLEY PETROLEUM MANAGEMENT | |
Well Pad ID: | |
Farm/Lease Name: MERCER MAX (MERCER FOREST) | |
License Status: Final Restoration | |
License Date: 2012-07-30 | |
Spud Date: 2013-05-06 | |
Spud Drilling Contractor: | |
Final Drill Date: 1971-12-08 | |
Well Total Depth: 3274.00 ft | |
Configuration: Vertical | |
Latitude: 40.300000 | |
Longitude: -82.170000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1958-02-03 | P&A 6-4-13 |
CO | 1966-11-18 | 28 CGAS EXPLORATION,INC GeoDate 11/18/66 |
Completed | 1971-12-08 | P&A 6-4-13 |
Reached Total Depth | 1971-12-08 | P&A 6-4-13 |
Change of Owner | 2007-04-27 | Operator changed from 28, CGAS EXPLORATION to 7578, ENERVEST OPERATING LLC |
APP | 2012-07-30 | Proposed Formations:CLINTON, Issued Date:7/30/2012, Expired Date:7/30/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2013-06-04 | P&A 6-4-13 |
Completion Report Received | 2014-02-13 | P&A 6-4-13 |
Construction Permit Expires | 2014-07-30 | P&A 6-4-13 |
Record Last Modified | 2017-10-23 | P&A 6-4-13 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
OIL | 0 | 330 Bbl | 14500 | |||
GEL | 0 | 180 Bbl | 0 |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1497246561 | 2013-5-22 0:00: | DD | No Violations | |
-1857800714 | 2013-6-3 0:00:0 | PB | No Violations | |
-2045216530 | 2013-5-16 0:00: | DD | No Violations | |
-434036448 | 2014-4-14 0:00: | FR | No Violations | |
-929616330 | 2014-6-10 0:00: | FR | No Violations | |
0016285759 | 2013-06-04 | Plug / Plug Back | No Violations | |
0434036448 | 2014-04-14 | Final Restoration | No Violations | FOLLOW UP TO CA #1384357022: On the day of my inspection I found that the site still needs to be seeded for erosion control. |
0912756244 | 2013-06-20 | Plug / Plug Back | No Violations | On the day of my inspection I found that the pit was still open. The fluid level was not in danger of breeching the liner and there were no sags or tears in the pit liner. |
0929616330 | 2014-06-10 | Final Restoration | No Violations | FOLLOW UP TO CA #1384357022: On the day of my inspection I found that the site was growing in weedy, grassy vegetation. The site is currently used as pasture for cattle. |
1367332061 | 2013-04-30 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Kenny Rich was rigging up. I met with Denny Dugan to go over formation depths and proposed casing program. |
1367847749 | 2013-05-06 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found that Kenny Rich had set 45 of 10.75 drive pipe. He was drilling at a depth of 580 with a 10 bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills. |
1367951954 | 2013-05-06 | Casing String Witnessed | No Violations | On the day of my inspection Kenny Rich had set 8.625 casing at 612. Formation pumped 30 barrels of water without establishing circulation. Then they pumped 400 lbs of gel mixed with cotton seed hull and celloflake. They displaced the slurry out of the casing and shut in for 15 minutes. Formation then pumped 112 sacks of class A cement mixed with cotton seed hulls. They established circulation while mixing cement. Good circulation was maintained throughout the remainder of the job. Cement returns were just starting to come back when Formation finished displacement. |
1369759036 | 2013-05-28 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Kenny Rich was drilling at a depth of 2900 inside of the original 5.5 production casing. They continued to encounter metallic obstructions down hole. The permit was on location, the pit liner was in good shape and there were no leaks or spills. |
1384357022 | 2013-11-12 | Final Restoration | Violations Noted | ORC 1509.072(B): Within six months after a well that has produced oil or gas is plugged, or after the plugging of a dry hole, unless the chief approves a longer time period, the owner or the owners agent shall remove all production and storage structures, supplies, and equipment, and any oil, salt water, and debris, and fill any remaining excavations. Within that period the owner or the owners agent shall grade or terrace and plant, seed, or sod the area disturbed where necessary to bind the soil and prevent substantial erosion and sedimentation. |
1387815220 | 2013-12-23 | Final Restoration | No Violations | FOLLOW UP TO CA #1384357022: On the day of my inspection I found that the pit had been closed and the top soil was graded out. The site still needs to be seeded for erosion control. |
1497246561 | 2013-05-22 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Kenny Rich was drilling at a depth of 2450 with a 6.5 bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills. |
16285759 | 2013-6-4 0:00:0 | PB | No Violations | |
1705094901 | 2013-05-09 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found that Kenny Rich was drilling at a depth of 1000 with an 8 bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills. |
1784797006 | 2013-12-04 | Final Restoration | No Violations | FOLLOW UP TO CA #1384357022: On the day of my inspection I found that nothing had been done to resolve this violation. |
1827369838 | 2006-03-27 | Field Inspected, Well Not Found | No Violations | Well not found , check of well records , shows plugged 1971 . |
1857800714 | 2013-06-03 | Plug / Plug Back | No Violations
- | |
2045216530 | 2013-05-16 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Kenny Rich was drilling at a depth of 1900 with a 6.5 bit. He reported that they were running into metallic obstructions down hole. The permit was on display, the pit liner was in good shape and there were no leaks or spills. |
912756244 | 2013-6-20 0:00: | PB | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1384357022 | US-OH-111429 | 2014-06-16 | Failure to complete final restoration within six months |
For data sources see[4]