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34-031-21138

Well Details

Well ID: 34-031-21138
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Country: United States
State: Ohio
County: Coshocton
Municipality: Perry Township
Operator Name: VALLEY PETROLEUM MANAGEMENT
Well Pad ID:
Farm/Lease Name: MERCER MAX (MERCER FOREST)
License Status: Final Restoration
License Date: 2012-07-30
Spud Date: 2013-05-06
Spud Drilling Contractor:
Final Drill Date: 1971-12-08
Well Total Depth: 3274.00 ft
Configuration: Vertical
Latitude: 40.300000
Longitude: -82.170000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1958-02-03 P&A 6-4-13
CO 1966-11-18 28 CGAS EXPLORATION,INC GeoDate 11/18/66
Completed 1971-12-08 P&A 6-4-13
Reached Total Depth 1971-12-08 P&A 6-4-13
Change of Owner 2007-04-27 Operator changed from 28, CGAS EXPLORATION to 7578, ENERVEST OPERATING LLC
APP 2012-07-30 Proposed Formations:CLINTON, Issued Date:7/30/2012, Expired Date:7/30/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged/Abandoned 2013-06-04 P&A 6-4-13
Completion Report Received 2014-02-13 P&A 6-4-13
Construction Permit Expires 2014-07-30 P&A 6-4-13
Record Last Modified 2017-10-23 P&A 6-4-13

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
OIL 0 330 Bbl 14500
GEL 0 180 Bbl 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1497246561 2013-5-22 0:00: DD No Violations
-1857800714 2013-6-3 0:00:0 PB No Violations
-2045216530 2013-5-16 0:00: DD No Violations
-434036448 2014-4-14 0:00: FR No Violations
-929616330 2014-6-10 0:00: FR No Violations
0016285759 2013-06-04 Plug / Plug Back No Violations
0434036448 2014-04-14 Final Restoration No Violations FOLLOW UP TO CA #1384357022: On the day of my inspection I found that the site still needs to be seeded for erosion control.
0912756244 2013-06-20 Plug / Plug Back No Violations On the day of my inspection I found that the pit was still open. The fluid level was not in danger of breeching the liner and there were no sags or tears in the pit liner.
0929616330 2014-06-10 Final Restoration No Violations FOLLOW UP TO CA #1384357022: On the day of my inspection I found that the site was growing in weedy, grassy vegetation. The site is currently used as pasture for cattle.
1367332061 2013-04-30 Drill / Deepen / Reopen No Violations On the day of my inspection Kenny Rich was rigging up. I met with Denny Dugan to go over formation depths and proposed casing program.
1367847749 2013-05-06 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Kenny Rich had set 45 of 10.75 drive pipe. He was drilling at a depth of 580 with a 10 bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills.
1367951954 2013-05-06 Casing String Witnessed No Violations On the day of my inspection Kenny Rich had set 8.625 casing at 612. Formation pumped 30 barrels of water without establishing circulation. Then they pumped 400 lbs of gel mixed with cotton seed hull and celloflake. They displaced the slurry out of the casing and shut in for 15 minutes. Formation then pumped 112 sacks of class A cement mixed with cotton seed hulls. They established circulation while mixing cement. Good circulation was maintained throughout the remainder of the job. Cement returns were just starting to come back when Formation finished displacement.
1369759036 2013-05-28 Drill / Deepen / Reopen No Violations On the day of my inspection Kenny Rich was drilling at a depth of 2900 inside of the original 5.5 production casing. They continued to encounter metallic obstructions down hole. The permit was on location, the pit liner was in good shape and there were no leaks or spills.
1384357022 2013-11-12 Final Restoration Violations Noted ORC 1509.072(B): Within six months after a well that has produced oil or gas is plugged, or after the plugging of a dry hole, unless the chief approves a longer time period, the owner or the owners agent shall remove all production and storage structures, supplies, and equipment, and any oil, salt water, and debris, and fill any remaining excavations. Within that period the owner or the owners agent shall grade or terrace and plant, seed, or sod the area disturbed where necessary to bind the soil and prevent substantial erosion and sedimentation.
1387815220 2013-12-23 Final Restoration No Violations FOLLOW UP TO CA #1384357022: On the day of my inspection I found that the pit had been closed and the top soil was graded out. The site still needs to be seeded for erosion control.
1497246561 2013-05-22 Drill / Deepen / Reopen No Violations On the day of my inspection Kenny Rich was drilling at a depth of 2450 with a 6.5 bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills.
16285759 2013-6-4 0:00:0 PB No Violations
1705094901 2013-05-09 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Kenny Rich was drilling at a depth of 1000 with an 8 bit. The permit was on location, the pit liner was in good shape and there were no leaks or spills.
1784797006 2013-12-04 Final Restoration No Violations FOLLOW UP TO CA #1384357022: On the day of my inspection I found that nothing had been done to resolve this violation.
1827369838 2006-03-27 Field Inspected, Well Not Found No Violations Well not found , check of well records , shows plugged 1971 .
1857800714 2013-06-03 Plug / Plug Back No Violations

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2045216530 2013-05-16 Drill / Deepen / Reopen No Violations On the day of my inspection Kenny Rich was drilling at a depth of 1900 with a 6.5 bit. He reported that they were running into metallic obstructions down hole. The permit was on display, the pit liner was in good shape and there were no leaks or spills.
912756244 2013-6-20 0:00: PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1384357022 US-OH-111429 2014-06-16 Failure to complete final restoration within six months

For data sources see[4]

References