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Well ID: 34-031-20129 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Perry Township | |
Operator Name: DERRICK PETROLEUM INC | |
Well Pad ID: | |
Farm/Lease Name: MOSSHOLDER J W | |
License Status: Final Restoration | |
License Date: 2014-07-03 | |
Spud Date: 1936-08-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1936-10-09 | |
Well Total Depth: 3254.00 ft | |
Configuration: Vertical | |
Latitude: 40.280000 | |
Longitude: -82.180000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1936-08-20 | |
Completed | 1936-10-09 | |
Reached Total Depth | 1936-10-09 | |
Change of Owner | 2014-06-19 | Operator changed from 9998, HISTORIC OWNER to 296, DERRICK PETROLEUM INC |
APP | 2014-07-03 | Proposed Formations:CLINTON, Issued Date:7/3/2014, Expired Date:7/2/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2016-07-02 | |
Plugged/Abandoned | 2016-07-06 | |
Record Last Modified | 2017-05-02 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-144865887 | 2016-7-5 0:00:0 | PB | No Violations | 1.00 |
-1762254860 | 2017-4-25 0:00: | FR | No Violations | 1.00 |
-1962697325 | 2009-11-9 0:00: | PW | No Violations | |
-404419392 | 2008-1-18 0:00: | PW | No Violations | |
-738686624 | 2012-2-22 0:00: | PW | No Violations | |
0055739256 | 2016-06-30 | Plug / Plug Back | No Violations | On the day of my inspection I found that Phil shut down after starting to pull the 5.5 casing. The casing was hung when he started to pull again. He made many attempts to pull the casing with no success. Phil came up and ripped the casing again at 945. He still couldnt get it to pull. He then made two more attempts at 882 and 760 before he could get the casing to come free. He pulled the 760 of free casing from the well. Then he started washing clay down the well to fill it from the brush and stone bridge at 1034. Phil washed approximately 12 more tons of clay down the well, filling it to surface multiple times. The clay would settle and they would fill it again. Once the well was filled and the clay was not falling, Phil pushed the remaining clay pile over the open casing and the well was left to sit over the weekend. |
0144865887 | 2016-07-05 | Plug / Plug Back | No Violations | On the day of my inspection I found that the clay was still piled over the open conductor casing. The clay inside the well had not fallen. The well had been sitting open for 4 days. I told Phil that he was clear to cut the casing off and cap the well. |
0404419392 | 2008-01-18 | Production Wells | No Violations | Well capable of production . |
0738686624 | 2012-02-22 | Production Wells | Violations Noted | FOLLOW UP TO NOV # 1329929086 This well is equipped with a pumping unit (40) powered by an electric motor and is capable of production. The production casing is open to the atmosphere and I was unable to determine if the well is actually producing oil. There is no identification (ID) posted at the well site The well owner must affix a valid and legible ID as soon as possible. This well must be put into production or plugged. |
0984707975 | 2016-07-06 | Plug / Plug Back | No Violations | On the day of my inspection Phil Moran uncovered the open conductor casing and the clay was still sitting firm at the surface. He cut the casing off 36 below grade and capped the casing with a steel plate inscribed with the permit number. The soil was pushed back over the well and the site was rough graded. This violation is resolved. |
1329929086 | 2012-02-22 | Production Wells | Violations Noted | This well is equipped with a pumping unit (40) powered by an electric motor and is capable of production. The production casing is open to the atmosphere and I was unable to determine if the well is actually producing oil. There is no identification (ID) posted at the well site The well owner must affix a valid and legible ID as soon as possible. This well must be put into production or plugged. |
1467292339 | 2016-06-29 | Plug / Plug Back | No Violations | On the day of my inspection Phil Moran washed 5 tons of clay down the 5.5 casing, then he rigged up to rip the 5.5 casing. He could not get any stretch when he tried to pull on the casing. He could not get a telegraph until 995. The 10 conductor was open with the 5.5 on a casing hanger. There were no other visible casing strings in the hole. The well was drilled in 1936. The 8 and 6 casing strings were likely removed during the WWII era and never recorded as being pulled. The 10 casing has likely been open for decades, allowing water, soil and debris to wash down the annulus around the 5.5 casing. Phil set a brush and stone bridge in the 5.5 casing at 1034 and then he ripped the 5.5 casing at 995 and started to pull it. |
1762254860 | 2017-04-25 | Final Restoration | No Violations | On the day of my inspection I found that the well site and access road were 90% covered in grass. There are two areas along the old access road that are always wet with standing water, so the grass did not grow there. I did not find any materials or debris left at the well site. There were not any tanks for this well. This site passes final restoration. |
1962697325 | 2009-11-09 | Production Wells | No Violations | Well capable of production . |
55739256 | 2016-6-30 0:00: | PB | No Violations | 8.00 |
984707975 | 2016-7-6 0:00:0 | PB | No Violations | 1.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0738686624 | US-OH-128399 | 2016-07-25 | Well shall be plugged | |
1329929086 | US-OH-109438 | 2012-02-24 | Failure to legibly identify well |
For data sources see[3]