X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-029-21279

Well Details

Well ID: 34-029-21279
Loading map...
Country: United States
State: Ohio
County: Columbiana
Municipality: West Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: MILLER WALTER
License Status: Producing
License Date: 1986-07-12
Spud Date: 1986-12-26
Spud Drilling Contractor:
Final Drill Date: 1986-12-30
Well Total Depth: 5781.00 ft
Configuration: Vertical
Latitude: 40.760000
Longitude: -81.020000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1986-12-26
Completed 1986-12-30
Reached Total Depth 1986-12-30
Change of Owner 2004-03-12 Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC
Change of Owner 2011-01-27 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
Change of Owner 2011-02-08 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
Change of Owner 2017-10-17 Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2017-10-17

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5547 5598 28
5547 5598 28
5547 5598 28

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 123000 Gal 71000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 LANGASCO ENERGY CORP 381.00 383.00 308
1990 RESOURCE AMERICA INC 866.00 395.00 228
1991 RESOURCE AMERICA INC 1846.00 562.00 365
1993 RESOURCE AMERICA INC 1255.00 477.00 365
1994 RESOURCE AMERICA INC 1067.00 300.00 365
1995 RESOURCE AMERICA INC 1059.00 478.00 365
1996 RESOURCE AMERICA INC 845.00 4080.00 365
1997 RESOURCE AMERICA INC 750.00 349.00 365
1998 RESOURCE AMERICA INC 723.00 252.00 365
1999 RESOURCE AMERICA INC 623.00 113.00 321
2000 RESOURCE AMERICA INC 742.00 0.00 365
2001 RESOURCE AMERICA INC 680.00 247.00 207
2002 RESOURCE AMERICA INC 902.00 131.00 365
2003 RESOURCE AMERICA INC 814.00 101.00 365
2004 CHEVRON APPALACHIA LLC 813.00 407.00 365
2005 CHEVRON APPALACHIA LLC 708.00 0.00 365
2006 CHEVRON APPALACHIA LLC 516.00 0.00 365
2007 CHEVRON APPALACHIA LLC 726.00 591.00 365
2008 CHEVRON APPALACHIA LLC 930.00 539.00 366
2009 CHEVRON APPALACHIA LLC 725.00 284.00 365
2010 ATLAS NOBLE LLC 768.00 302.00 365
2011 CHEVRON APPALACHIA LLC 645.00 226.00 365
2012 ATLAS NOBLE LLC 887.00 189.00 366
2013 ATLAS NOBLE LLC 735.00 227.00 365
2014 ATLAS NOBLE LLC 815.00 217.00 365
2015 ATLAS NOBLE LLC 630.00 144.00 365
2016 ATLAS NOBLE LLC 279.00 0.00 70
2017 ATLAS NOBLE LLC 29.00 0.00 182
2018 M & R INVESTMENTS OHIO LLC 775.00 517.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 LANGASCO ENERGY CORP Brine 470 308
1990 RESOURCE AMERICA INC Brine 53 228
1991 RESOURCE AMERICA INC Brine 0 365
1993 RESOURCE AMERICA INC Brine 0 365
1994 RESOURCE AMERICA INC Brine 0 365
1995 RESOURCE AMERICA INC Brine 0 365
1996 RESOURCE AMERICA INC Brine 0 365
1997 RESOURCE AMERICA INC Brine 0 365
1998 RESOURCE AMERICA INC Brine 90 365
1999 RESOURCE AMERICA INC Brine 0 321
2000 RESOURCE AMERICA INC Brine 0 365
2001 RESOURCE AMERICA INC Brine 0 207
2002 RESOURCE AMERICA INC Brine 40 365
2003 RESOURCE AMERICA INC Brine 0 365
2004 CHEVRON APPALACHIA LLC Brine 20 365
2005 CHEVRON APPALACHIA LLC Brine 0 365
2006 CHEVRON APPALACHIA LLC Brine 0 365
2007 CHEVRON APPALACHIA LLC Brine 50 365
2008 CHEVRON APPALACHIA LLC Brine 16 366
2009 CHEVRON APPALACHIA LLC Brine 18 365
2010 ATLAS NOBLE LLC Brine 70 365
2011 CHEVRON APPALACHIA LLC Brine 9 365
2012 ATLAS NOBLE LLC Brine 56 366
2013 ATLAS NOBLE LLC Brine 73 365
2014 ATLAS NOBLE LLC Brine 69 365
2015 ATLAS NOBLE LLC Brine 24 365
2016 ATLAS NOBLE LLC Brine 0 70
2017 ATLAS NOBLE LLC Brine 0 182
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1719465349 2015-7-21 0:00: PW No Violations
-2126986986 2012-1-31 0:00: PW No Violations 1.00
-485498768 2018-4-12 0:00: WR No Violations
0000000737 2002-08-01 Production Wells No Violations Identification is now posted. Recommend case be resolved.
001216i638 2002-06-13 Production Wells Violations Noted Wellhead identification missing. Met on site with pumper Andy Smith.
0083277675 2002-08-12 Preliminary Restoration No Violations Meets requirements.
0485498768 2018-04-12 Work Over Reconditioning No Violations The purpose of my inspection was to witness work over activities on well #2-1279. I met with production foreman Chris Belch on location. Bishop Well Service was on location to perform the work over operation. Mr. Belch reported the 1.5 tubing had parted and was being replaced with 2.375 tubing and a new downhole pump. At the time of my inspection. Bishop was pulling the remaining 1.5 tubing from the well. I did not observe any evidence of spills or leaks. The well head was secured after the tubing was removed. Mr. Belch stated that activities would be completed and the well placed back in to production by the end of the following week (4/20/2018). I will schedule a follow-up inspection once the well is placed back into production.
1216i638 2002-6-13 0:00: PW No Violations 0.50
1225175393 2005-01-26 Production Wells No Violations The tank battery is shared with permits 1341 and 1274 and consists of 3-210 bbl storage tanks, 3-separators, 1-50 bbl salt water tank and a dike.
1719465349 2015-07-21 Production Wells No Violations I was on site to conduct a status check. The tank battery is shared between the W. Miller #1 (#21274), the W. Miller #2 (#21279), and the W. Miller #3 (#21341). Identification was posted on the tank battery. The tank battery consists of three 210 bbl production tanks, a 50 bbl steel brine tank, and three horizontal separators. The tanks valves are sealed with a plug. There is a meter box with a current seven day chart showing production. A dike is present and in good repair. The wellhead is equipped with an electric pumpjack and a domestic supply line. The access road and site are stable. No violations were observed.
2126986986 2012-01-31 Production Wells No Violations On 1/31/2012, I performed a status check on the above well site. No violations were noted at this time.
737 2002-8-1 0:00:0 PW No Violations 0.50
83277675 2002-8-12 0:00: PL No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
001216i638 US-OH-105804 2002-06-17 Failure to legibly identify well

For data sources see[9]

References