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Well ID: 34-029-21025 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Knox Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: STRYFELLER-STOFFER | |
License Status: Producing | |
License Date: 1984-04-27 | |
Spud Date: 1984-05-25 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1984-05-31 | |
Well Total Depth: 5441.00 ft | |
Configuration: Vertical | |
Latitude: 40.880000 | |
Longitude: -81.010000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-04-27 | Issued Date 4/27/84 Expired Date 10/24/84 Acres 0086350 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05441 Proposed Drill Depth 05441 |
Original Spud | 1984-05-25 | |
Completed | 1984-05-31 | |
Reached Total Depth | 1984-05-31 | |
CO | 1984-09-21 | 8 BLAIR BILL INC GeoDate 4/27/84 |
Completion Report Received | 1984-10-11 | |
Construction Permit Expires | 1984-10-24 | |
CO | 1993-04-13 | 28 CGAS EXPLORATION,INC GeoDate 4/27/84 |
Change of Owner | 2007-04-27 | Operator changed from 28, CGAS EXPLORATION to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5201 | 5358 | 0 |
5201 | 5358 | 0 | |
2006-09-11 | 5250 | 5330 | 48 |
5250 | 5330 | 48 | |
5201 | 5358 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 59140 Gal | 55000 | FRAC: H2O,SAND | ||
ACID | 0 | 500 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BLAIR BILL INC | 9614.00 | 842.00 | 365 |
1985 | BLAIR BILL INC | 23361.00 | 860.00 | 365 |
1986 | BLAIR BILL INC | 20690.00 | 502.00 | 365 |
1987 | BLAIR BILL INC | 14906.00 | 307.00 | 365 |
1988 | BLAIR BILL INC | 13160.00 | 354.00 | 365 |
1989 | BLAIR BILL INC | 11348.00 | 220.00 | 365 |
1990 | BLAIR BILL INC | 10202.00 | 218.00 | 365 |
1991 | BLAIR BILL INC | 7553.00 | 146.00 | 365 |
1992 | BLAIR BILL INC | 6383.00 | 142.00 | 365 |
1993 | BLAIR BILL INC | 1000.00 | 67.00 | 90 |
1994 | CGAS EXPLORATION | 6018.00 | 139.00 | 365 |
1995 | CGAS EXPLORATION | 5156.00 | 85.00 | 365 |
1996 | CGAS EXPLORATION | 4185.00 | 96.00 | 365 |
1997 | CGAS EXPLORATION | 4958.00 | 136.00 | 365 |
1998 | CGAS EXPLORATION | 4860.00 | 95.00 | 365 |
1999 | CGAS EXPLORATION | 3044.00 | 97.00 | 365 |
2000 | CGAS EXPLORATION | 2842.00 | 138.00 | 365 |
2001 | CGAS EXPLORATION | 3086.00 | 164.00 | 365 |
2002 | CGAS EXPLORATION | 2202.00 | 72.00 | 365 |
2003 | CGAS EXPLORATION | 2068.00 | 128.00 | 365 |
2004 | CGAS EXPLORATION | 5373.00 | 71.00 | 365 |
2005 | CGAS EXPLORATION | 1417.00 | 84.00 | 365 |
2006 | CGAS EXPLORATION | 1715.00 | 66.00 | 365 |
2007 | ENERVEST OPERATING LLC | 1452.00 | 0.00 | 365 |
2008 | ENERVEST OPERATING LLC | 1960.00 | 0.00 | 365 |
2009 | ENERVEST OPERATING LLC | 1946.00 | 89.00 | 365 |
2010 | ENERVEST OPERATING LLC | 1912.00 | 73.00 | 365 |
2011 | ENERVEST OPERATING LLC | 2093.00 | 76.00 | 0 |
2012 | ENERVEST OPERATING LLC | 2101.00 | 87.00 | 366 |
2013 | ENERVEST OPERATING LLC | 1787.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 1030.00 | 83.00 | 365 |
2015 | ENERVEST OPERATING LLC | 925.00 | 18.00 | 365 |
2016 | ENERVEST OPERATING LLC | 1186.00 | 19.00 | 366 |
2017 | ENERVEST OPERATING LLC | 1187.00 | 18.00 | 365 |
2018 | ENERVEST OPERATING LLC | 965.00 | 0.00 | 355 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BLAIR BILL INC | Brine | 0 | 365 |
1985 | BLAIR BILL INC | Brine | 120 | 365 |
1986 | BLAIR BILL INC | Brine | 60 | 365 |
1987 | BLAIR BILL INC | Brine | 0 | 365 |
1988 | BLAIR BILL INC | Brine | 38 | 365 |
1989 | BLAIR BILL INC | Brine | 30 | 365 |
1990 | BLAIR BILL INC | Brine | 25 | 365 |
1991 | BLAIR BILL INC | Brine | 15 | 365 |
1992 | BLAIR BILL INC | Brine | 25 | 365 |
1993 | BLAIR BILL INC | Brine | 0 | 90 |
1994 | CGAS EXPLORATION | Brine | 17 | 365 |
1995 | CGAS EXPLORATION | Brine | 0 | 365 |
1996 | CGAS EXPLORATION | Brine | 40 | 365 |
1997 | CGAS EXPLORATION | Brine | 0 | 365 |
1998 | CGAS EXPLORATION | Brine | 0 | 365 |
1999 | CGAS EXPLORATION | Brine | 52 | 365 |
2000 | CGAS EXPLORATION | Brine | 20 | 365 |
2001 | CGAS EXPLORATION | Brine | 20 | 365 |
2002 | CGAS EXPLORATION | Brine | 20 | 365 |
2003 | CGAS EXPLORATION | Brine | 17 | 365 |
2004 | CGAS EXPLORATION | Brine | 0 | 365 |
2005 | CGAS EXPLORATION | Brine | 40 | 365 |
2006 | CGAS EXPLORATION | Brine | 0 | 365 |
2007 | ENERVEST OPERATING LLC | Brine | 10 | 365 |
2008 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2009 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 366 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2016 | ENERVEST OPERATING LLC | Brine | 0 | 366 |
2017 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2018 | ENERVEST OPERATING LLC | Brine | 0 | 355 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1670917143 | 2018-10-15 0:00 | PW | No Violations | 0.10 |
-168254439 | 2005-2-10 0:00: | PW | No Violations | 0.50 |
-464993520 | 2019-8-14 0:00: | PW | No Violations | 1.00 |
-718311044 | 2018-8-27 0:00: | PW | No Violations | 0.20 |
0168254439 | 2005-02-10 | Production Wells | No Violations | The tank battery is shared with permit 1026 and consists of 1-210 bbl storage tank, 1-buried concrete salt water tank and a dike. |
0718311044 | 2018-08-27 | Production Wells | Violations Noted | The purpose of my inspection was to document the status of the leaking tubing head packing assembly on well #2-1025. At the time of my follow-up inspection gas was witnessed leaking from the tubing head assembly. On 9/5/2018 I notified Enervest Field Superintendent Joe Teppert that the well was insufficiently equipped to prevent the escape of gas. Mr. Teppert reported that he would have a contractor scheduled to investigate the leak and make any necessary repairs within two weeks. I will schedule a follow-up inspection after 9/19/2018 to document the status of the well. |
1536146650 | 2018-08-16 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check inspection on well #2-1025. RBDMS indicated reported production was current. Access to the well remained stable and drivable. The 8.625 well head was plumbed above grade and closed to atmosphere. The 4.5 production casing was equipped with a plunger lift assembly. Production valves were in the open position. Staining consistent with a legacy operation was present. At the time of my inspection I witnessed gas leaking from the packing on the tubing head assembly. A stable earthen dike that was free of fluid was present around the production tanks. A horizontal separator was on located outside of the dike. The separator remained in good repair and contained a current 16 day chart. One (1) 210 bbl production tank and one (1) concrete brine vault were present inside of the dike. The production tank remained in good repair and contained correct identification. Valves were closed and plugged. The brine vault remained in good repair above grade. The vault was holding fluid with freeboard. Following the inspection I spoke with lease operator Don Pahovey to notify him of the leak observed at the tubing head. Mr. Pahovey stated he would investigate the leak and make any necessary repairs. I will schedule a follow-up inspection to document the status of repairs. |
1670917143 | 2018-10-15 | Production Wells | No Violations | The purpose of my inspection was to follow-up on compliance notice #718311044. At the time of my follow-up inspection the gas leak at the well head was repaired. No further action is necessary. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0718311044 | US-OH-128160 | 2018-11-16 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]