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Well ID: 34-029-21004 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Knox Township | |
Operator Name: QUALITY OIL & GAS CORP | |
Well Pad ID: | |
Farm/Lease Name: PIFER-CRANSTON UNIT | |
License Status: Producing | |
License Date: 1984-10-11 | |
Spud Date: 1984-01-14 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1984-11-18 | |
Well Total Depth: 5715.00 ft | |
Configuration: Vertical | |
Latitude: 40.820000 | |
Longitude: -81.010000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1983-12-23 | 648 QUALITY OIL & GAS GeoDate 12/23/83 |
Oil and Gas | 1983-12-23 | Issued Date 12/23/83 Expired Date 6/20/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1984-10-11 | 648 QUALITY OIL & GAS GeoDate 10/11/84 |
Oil and Gas | 1984-10-11 | Issued Date 10/11/84 Expired Date 4/9/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05715 Proposed Drill Depth 05715 |
Original Spud | 1984-11-13 | RI 10-13-84 PERMIT EXPIRED. |
Completed | 1984-11-18 | RI 10-13-84 PERMIT EXPIRED. |
Reached Total Depth | 1984-11-18 | RI 10-13-84 PERMIT EXPIRED. |
Construction Permit Expires | 1985-04-09 | RI 10-13-84 PERMIT EXPIRED. |
Completion Report Received | 1986-06-27 | RI 10-13-84 PERMIT EXPIRED. |
Record Last Modified | 2017-02-15 | RI 10-13-84 PERMIT EXPIRED. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5494 | 5603 | 42 |
5494 | 5603 | 42 | |
5494 | 5603 | 42 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 179000 Gal | 140000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | QUALITY OIL & GAS CORP | 529.00 | 413.00 | 365 |
1994 | QUALITY OIL & GAS CORP | 310.00 | 339.00 | 365 |
1995 | QUALITY OIL & GAS CORP | 190.00 | 200.00 | 365 |
1997 | QUALITY OIL & GAS CORP | 169.00 | 197.00 | 364 |
1998 | QUALITY OIL & GAS CORP | 109.00 | 146.00 | 365 |
2000 | QUALITY OIL & GAS CORP | 92.00 | 482.00 | 365 |
2001 | QUALITY OIL & GAS CORP | 252.00 | 252.00 | 365 |
2002 | QUALITY OIL & GAS CORP | 107.00 | 252.00 | 365 |
2003 | QUALITY OIL & GAS CORP | 20.00 | 121.00 | 365 |
2004 | QUALITY OIL & GAS CORP | 0.00 | 90.00 | 365 |
2005 | QUALITY OIL & GAS CORP | 0.00 | 0.00 | 0 |
2007 | QUALITY OIL & GAS CORP | 0.00 | 0.00 | 0 |
2008 | QUALITY OIL & GAS CORP | 0.00 | 0.00 | 0 |
2009 | QUALITY OIL & GAS CORP | 0.00 | 0.00 | 0 |
2011 | QUALITY OIL & GAS CORP | 0.00 | 118.00 | 365 |
2012 | QUALITY OIL & GAS CORP | 0.00 | 0.00 | 0 |
2013 | QUALITY OIL & GAS CORP | 40.00 | 235.00 | 365 |
2014 | QUALITY OIL & GAS CORP | 412.00 | 739.00 | 365 |
2015 | QUALITY OIL & GAS CORP | 333.00 | 121.00 | 365 |
2016 | QUALITY OIL & GAS CORP | 281.00 | 210.00 | 365 |
2017 | QUALITY OIL & GAS CORP | 234.00 | 183.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1993 | QUALITY OIL & GAS CORP | Brine | 130 | 365 |
1994 | QUALITY OIL & GAS CORP | Brine | 40 | 365 |
1995 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
1997 | QUALITY OIL & GAS CORP | Brine | 35 | 364 |
1998 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
2000 | QUALITY OIL & GAS CORP | Brine | 50 | 365 |
2001 | QUALITY OIL & GAS CORP | Brine | 80 | 365 |
2002 | QUALITY OIL & GAS CORP | Brine | 40 | 365 |
2003 | QUALITY OIL & GAS CORP | Brine | 40 | 365 |
2004 | QUALITY OIL & GAS CORP | Brine | 35 | 365 |
2005 | QUALITY OIL & GAS CORP | Brine | 0 | 0 |
2007 | QUALITY OIL & GAS CORP | Brine | 0 | 0 |
2008 | QUALITY OIL & GAS CORP | Brine | 0 | 0 |
2009 | QUALITY OIL & GAS CORP | Brine | 0 | 0 |
2011 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
2012 | QUALITY OIL & GAS CORP | Brine | 0 | 0 |
2013 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
2014 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
2015 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
2016 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
2017 | QUALITY OIL & GAS CORP | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1188694722 | 2004-6-2 0:00:0 | PW | No Violations | 0.50 |
-1571027072 | 2017-3-16 0:00: | PW | No Violations | 3.00 |
-248294349 | 2004-7-14 0:00: | PW | No Violations | 0.50 |
-849996267 | 2012-8-29 0:00: | PW | No Violations | |
0248294349 | 2004-07-14 | Production Wells | Violations Noted | The contamination has not been removed as yet. Will contact the company to remind them. Case pends. |
0849996267 | 2012-08-29 | Production Wells | No Violations | I received a call from John Chenevey on 07/26/12 regarding the well being idle. Mr. Chenevey indicated that the well hadnt produced in years, but some oil that had been in the tank was sold in 2011. Upon inspection, I found that the well was not producing. The tank battery was overgrown with vegetation. There is no separator. The lease road is overgrown and rutted. The pump jack was overgrown with vegetation. The electric box breaker was off, and everything inside appeared to be corroding. |
1093009125 | 2004-08-19 | Production Wells | Violations Noted | |
1098358299 | 2004-10-20 | Production Wells | No Violations | The contamination has now been removed. Recommend case be resolved. |
1188694722 | 2004-06-02 | Production Wells | Violations Noted | The tank battery consists of 1-210 bbl storage tank, 1-buried concrete salt water tank, and a dike. |
1278787506 | 2012-12-11 | Production Wells | Violations Noted | The tank pad had been cleared of the vegetative overgrowth observed in August. The well is still not in production. There is neither a separator nor meter. The lease road is overgrown and rutted. The pump jack was overgrown with vegetation, and there were no signs of operation. There was a tag on the piping at the well head indicating that solvent had been put into the well by B&E Well Treating in November 2012. The well must be put into production within 30 days (02/02/13) of the date of this notice, or plugged within 90 days (04/03/13) of the date of this notice. |
1385399085 | 2013-01-09 | Administrative Inspection | No Violations | I spoke with Kathy at Quality Oil & Gas. She referred me to Brian, the pumper for the well. I called Brian and discussed the status of the well. He indicated that they could not sell any gas off the well, but did operate the pump jack about once a month to produce oil. Pumping once a month helped keep the electric bill down. He indicated that he had approximately 7 to 8 feet of oil in the oil storage tank. Since the company is producing the well, the Compliance Notice requesting produce the well or plug or plug the well is closed. |
1571027072 | 2017-03-16 | Production Wells | No Violations | The purpose of my inspection was to respond to a reported spill at well #2-1004. I received a phone call from Scott Miller who stated he was substituting for Dave Widdick while on vacation. Mr. Miller continued that on the morning of 3/16/2017 he had discovered a well head failure caused crude oil to leak onto and migrate adjacent to and down grade from the well location. Due to a recent snow event, the entire area was covered with snow and Mr. Miller was in the process of determining the volume and extent of the release. I confirmed with Mr. Miller that the pumping unit had been shut down to prevent further contamination. Mr. Miller reported that he was unsure of the exact volume of the release, but estimated the volume around 5 bbls. He continued that he had equipment arriving on site to begin containing and cleaning up the impacted soil. I communicated to Mr. Miller that I would be on location as soon as possible. Following the call with Mr. Miller, I spoke with ODNR-DOGRM Emergency Response Coordinator Fred Romeo. ERC Romeo reported to begin grading the contaminated area and store the material in an impervious containment (either lined roll off boxes or lined pit) until disposal can be arranged. I arrived on location to find Mr. Miller grading off the top layer of impacted soil and stockpiling it near the well head. Mr. Miller delineated the extent of the spill and determined that the spill had been contained to the Unit and no production fluid had migrated off of the property or into a surface water body. I walked the designated area and confirmed the delineated area of contamination. Mr. Miller constructed an earthen dike near the lease entrance road and lined it with an impervious pit liner to contain the stockpiled material until a manifest could be obtained. I will follow up with Dave Widdick to confirm the material has been removed from the location and disturbed areas regraded and stabilized. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0248294349 | US-OH-122424 | 2004-07-15 | Well operation causing pollution and contamination | |
1093009125 | US-OH-102181 | 2004-08-20 | Well operation causing pollution and contamination | |
1188694722 | US-OH-105012 | 2004-06-03 | Well operation causing pollution and contamination | |
1278787506 | US-OH-107751 | 2014-04-23 | Well shall be plugged |
For data sources see[9]