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34-029-20805

Well Details

Well ID: 34-029-20805
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Country: United States
State: Ohio
County: Columbiana
Municipality: Knox Township
Operator Name: QUALITY OIL & GAS CORP
Well Pad ID:
Farm/Lease Name: WALBORN
License Status: Plugged and Abandoned
License Date: 2019-03-13
Spud Date: 1980-09-22
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1980-09-28
Well Total Depth: 5734.00 ft
Configuration: Vertical
Latitude: 40.830000
Longitude: -81.010000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1980-09-22
Completed 1980-09-28
Reached Total Depth 1980-09-28
Completion Report Received 1981-01-09
CO 1982-09-10 648 QUALITY OIL & GAS GeoDate 9/10/82
APP 2019-03-13 Proposed Formations:CLINTON, Issued Date:3/13/2019, Expired Date:3/12/2021 12:00:00 PM, Drilling unit acres:40.5, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2019-03-20
Construction Permit Expires 2021-03-12

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2003-09-05 5483 5555 16
5483 5555 16
5483 5555 16

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 88020 Gal 30000
H2O 0 83000 Gal 30000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 QUALITY OIL & GAS CORP 1084.00 660.00 365
1993 QUALITY OIL & GAS CORP 335.00 266.00 365
1994 QUALITY OIL & GAS CORP 338.00 141.00 365
1995 QUALITY OIL & GAS CORP 340.00 142.00 365
1997 QUALITY OIL & GAS CORP 67.00 0.00 364
2000 QUALITY OIL & GAS CORP 0.00 0.00 0
2003 QUALITY OIL & GAS CORP 0.00 0.00 0
2007 QUALITY OIL & GAS CORP 0.00 0.00 0
2014 QUALITY OIL & GAS CORP 0.00 0.00 0
2016 QUALITY OIL & GAS CORP 115.00 0.00 0
2017 QUALITY OIL & GAS CORP 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 QUALITY OIL & GAS CORP Brine 0 365
1993 QUALITY OIL & GAS CORP Brine 67 365
1994 QUALITY OIL & GAS CORP Brine 48 365
1995 QUALITY OIL & GAS CORP Brine 95 365
1997 QUALITY OIL & GAS CORP Brine 0 364
2000 QUALITY OIL & GAS CORP Brine 0 0
2003 QUALITY OIL & GAS CORP Brine 0 0
2007 QUALITY OIL & GAS CORP Brine 0 0
2014 QUALITY OIL & GAS CORP Brine 0 0
2016 QUALITY OIL & GAS CORP Brine 0 0
2017 QUALITY OIL & GAS CORP Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1234013722 2019-6-26 0:00: PB No Violations
-1537936428 2018-1-31 0:00: PW No Violations 0.20
-165084795 2005-3-15 0:00: PW No Violations 0.50
-2120974682 2019-12-20 0:00 PW No Violations 2.00
-82603580 2017-12-26 0:00 PW No Violations 1.00
0082603580 2017-12-26 Production Wells No Violations The purpose of my inspection was to document the status of well #2-0805. A review of RBDMS indicated the owner reported production in 2016. Access to the well was through a residential driveway that lead to a back yard. The well location was stable. The 8.625 well head was below grade. The 4.5 production casing was equipped with tubing only that was plumbed to a sales line and domestic supply connection. No tank battery was present. No identification was present. While on location I called and spoke with Quality contract lease operator Dave Wittick. Mr. Wittick stated he was not familiar with the well and had never operated the well. He continued that he was in the area changing production charts and would drive to the location. Mr. Wittick later arrived on location and we walked back to the well. Mr. Wittick repeated that he was not familiar with the well and that this was the first time that he had been there. I witnessed Mr. Wittick open a valve on the domestic supply drip tank and the well had no pressure or gas was observed. The house in front of the well also had a large propane tank in the back yard. The house did not appear lived in, but the electric service was connected and operating. Mr. Wittick stated he would contact the office to learn more about the well and report back what would be planned for the well. I will plan a follow-up inspection to either witness the well in production or issue a compliance notice to plug and abandon the well.
0110140274 2018-11-02 Production Wells No Violations The purpose of my inspection was to follow-up on compliance notice # 1524246727. I spoke with Tim Lanzer of Quality Oil & Gas Corp. on 11/01/2018 to discuss the status of well #2-0805. Mr. Lanzer stated that he was continuing to work with the partner on this well, Abarta Oil & Gas, to get the well plugged. Mr. Lanzer requested additional time to get the details in place. During the conversation I stated that I would discuss an extension with ODNR-DOGRM Northeast Regional Manager Thomas Hill. On 11/02/2018 I spoke with Mr. Hill regarding the extension. Mr. Hill approved extending the date that well #2-0805 needs to be plugged by 180 days. At the time of my follow-up inspection correct identification remained in place at the well head. Production valves remained in the closed position. No production equipment was on location. The well was not supplying gas for domestic consumption. I will contact Mr. Lanzer to notify him of the extension date.
0165084795 2005-03-15 Production Wells Violations Noted There is no tank battery. The well is domestic use only. Identification missing.
0252883162 2005-04-04 Production Wells Violations Noted Identification has no been posted. Called the office on 04/07/2005. The sign is supposed to be up now. Will verify. Case pends.
110140274 2018-11-2 0:00: PW No Violations 0.30
1103313546 2005-05-27 Production Wells No Violations Identification posted. Recommend case be resolved.
1524246727 2018-04-20 Production Wells Violations Noted The purpose of my inspection was to document the status of well #2-0805. The well operator had posted correct identification. Production valves were in the closed position. Following the inspection I called and spoke with Tim Lanzer with Quality Oil & Gas Corp to discuss the well. Mr. Lanzer reported that the well was owned by Abarta Oil and Gas and Quality was the operator. Mr. Lanzer stated that the plan was to plug the well at some point in 2018, but did not have a date. I communicated to Mr. Lanzer that I would be issuing a compliance notice to plug and abandon the well. The well is currently incapable of production Quality Oil and Gas Corp. shall submit a written plugging plan to Inspector Kenneth Frye at the Ohio Department of Natural Resources, Division of Oil and Gas Resources Management, 3575 Forest Lake Drive, Suite 150, Uniontown, OH 44685, within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. Quality Oil and Gas Corp. will be notified if the plugging plan is approved or denied.
1537936428 2018-01-31 Production Wells No Violations The purpose of my inspection was to conduct a status check on well #2-0805. Northeast District Supervisor Stephen Ochs was present during the inspection. Lease operator Dave Wittick had posted correct identification. At the time inspection, a slight audible leak was observed from the well head. Production valves remained in the closed position. The primary domestic supply connection valve was in the closed position. While on location I called and spoke with Mr. Wittick concerning the status of the well. Mr. Wittick stated he planned to test the well for flow and pressure. I will follow up with Mr. Wittick to document the status of the well.
1561462169 2019-6-25 0:00: PB No Violations
252883162 2005-4-4 0:00:0 PW No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0165084795 US-OH-116288 2005-03-17 Failure to legibly identify well
0252883162 US-OH-122606 2005-04-07 Failure to legibly identify well
1524246727 US-OH-114554 2018-05-04 NONE Well shall be plugged

For data sources see[9]

References