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Well ID: 34-029-20654 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Knox Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: EGLI VERNON F UNIT | |
License Status: Producing | |
License Date: 1970-09-11 | |
Spud Date: 1970-10-06 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-10-20 | |
Well Total Depth: 5550.00 ft | |
Configuration: Vertical | |
Latitude: 40.820000 | |
Longitude: -81.050000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-09-11 | 9 EDC GeoDate 9/11/70 |
Original Spud | 1970-10-06 | |
Completed | 1970-10-20 | |
Reached Total Depth | 1970-10-20 | |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5423 | 5503 | 0 |
5423 | 5503 | 0 | |
5423 | 5503 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1500 Bbl | 45000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | POWER GAS MARKETING & TRANS | 1466.00 | 88.00 | 0 |
1985 | POWER GAS MARKETING & TRANS | 2374.00 | 187.00 | 365 |
1987 | POWER GAS MARKETING & TRANS | 2247.00 | 83.00 | 365 |
1988 | POWER GAS MARKETING & TRANS | 3593.00 | 269.00 | 365 |
1989 | POWER GAS MARKETING & TRANS | 3507.00 | 181.00 | 365 |
1990 | POWER GAS MARKETING & TRANS | 2950.00 | 178.00 | 365 |
1991 | POWER GAS MARKETING & TRANS | 1811.00 | 259.00 | 365 |
1992 | POWER GAS MARKETING & TRANS | 2342.00 | 184.00 | 365 |
1993 | POWER GAS MARKETING & TRANS | 2347.00 | 76.00 | 365 |
1994 | POWER GAS MARKETING & TRANS | 1556.00 | 185.00 | 0 |
1995 | POWER GAS MARKETING & TRANS | 1937.00 | 90.00 | 0 |
1996 | POWER GAS MARKETING & TRANS | 1612.00 | 162.00 | 0 |
1997 | POWER GAS MARKETING & TRANS | 945.00 | 88.00 | 365 |
1998 | POWER GAS MARKETING & TRANS | 835.00 | 121.00 | 365 |
1999 | POWER GAS MARKETING & TRANS | 798.00 | 124.00 | 365 |
2000 | POWER GAS MARKETING & TRANS | 738.00 | 119.00 | 365 |
2001 | POWER GAS MARKETING & TRANS | 501.00 | 0.00 | 365 |
2002 | POWER GAS MARKETING & TRANS | 113.00 | 0.00 | 365 |
2003 | POWER GAS MARKETING & TRANS | 188.00 | 84.00 | 365 |
2004 | POWER GAS MARKETING & TRANS | 0.00 | 0.00 | 0 |
2005 | POWER GAS MARKETING & TRANS | 0.00 | 0.00 | 0 |
2006 | EXCO - NORTH COAST ENERGY INC | 544.00 | 175.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 3539.00 | 189.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 2636.00 | 187.00 | 366 |
2009 | ENERVEST OPERATING LLC | 1952.00 | 0.00 | 92 |
2010 | ENERVEST OPERATING LLC | 1423.00 | 131.00 | 365 |
2011 | ENERVEST OPERATING LLC | 2004.00 | 99.00 | 0 |
2012 | ENERVEST OPERATING LLC | 2156.00 | 115.00 | 366 |
2013 | ENERVEST OPERATING LLC | 2294.00 | 129.00 | 365 |
2014 | ENERVEST OPERATING LLC | 1268.00 | 118.00 | 365 |
2015 | ENERVEST OPERATING LLC | 1685.00 | 84.00 | 363 |
2016 | ENERVEST OPERATING LLC | 1359.00 | 130.00 | 359 |
2017 | ENERVEST OPERATING LLC | 1626.00 | 82.00 | 365 |
2018 | ENERVEST OPERATING LLC | 1302.00 | 107.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1904486044 | 2017-10-24 0:00 | PW | No Violations | 0.50 |
-2145153864 | 2006-2-2 0:00:0 | PW | No Violations | 0.50 |
-820468644 | 2006-1-18 0:00: | PW | No Violations | 0.50 |
0820468644 | 2006-01-18 | Production Wells | Violations Noted | The well is now in operation but the tank battery dike has not been built. Case pends. |
1124116254 | 2005-11-21 | Production Wells | Violations Noted | Arrived on site and found the well to be idle. There is no sale chart and no production filed for the year 2004. Met with Mr. Ben Rosenburger who claims that the well has been idle for several years due to the company that owns the sale line will not permit them to produce into the line due to the separator malfunctioning too many times and filling the sale line. |
1904486044 | 2017-10-24 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-0654. A review of RBDMS indicated that the owner was current with production. The access and locations were stable. The 8.625 well head was below grade. The 4.5 production casing was equipped with a plunger lift assembly. Production valves were open. No leaks were observed. A domestic supply connection was present. A worn earthen dike that was free of fluid was constructed around the production equipment. Equipment inside the dike consisted of one (1) vertical separator and one (1) 100 bbl production tank The separator remained in good repair with no leaks. The production tank remained in good repair and contained correct identification. Valves were closed and plugged. A standalone meter set with a current 16 day production chart was located outside of the dike. No violations were observed during this inspection. |
2108705678 | 2004-07-16 | Production Wells | No Violations | The tank battery consists of 1-210 bbl storage tank and no dike. |
2145153864 | 2006-02-02 | Production Wells | No Violations | The well is in operation and a dike has been built around the tank battery. Recommend case be resolved. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0820468644 | US-OH-129356 | 2006-01-19 | No SPCC dike/or failure to keep dike free of water or oil | |
1124116254 | US-OH-103128 | 2005-08-15 | No SPCC dike/or failure to keep dike free of water or oil | |
1124116254 | US-OH-103129 | 2005-08-15 | Well shall be plugged |
For data sources see[9]