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Well ID: 34-029-20646 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Knox Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: KITZMILLER E & V | |
License Status: Producing | |
License Date: 1970-04-14 | |
Spud Date: 1970-06-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-06-24 | |
Well Total Depth: 5570.00 ft | |
Configuration: Vertical | |
Latitude: 40.820000 | |
Longitude: -81.040000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-04-14 | 9 EDC GeoDate 4/14/70 |
Original Spud | 1970-06-03 | GL=1265.9 |
Completed | 1970-06-24 | GL=1265.9 |
Reached Total Depth | 1970-06-24 | GL=1265.9 |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2019-06-04 | GL=1265.9 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5438 | 5466 | 0 |
5438 | 5466 | 0 | |
5438 | 5466 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 0 | 1000 Gal | 0 | MCA | ||
H2O | 0 | 1500 Bbl | 50000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1022964107 | 2005-3-22 0:00: | PW | No Violations | 0.50 |
-1848083487 | 2005-3-15 0:00: | PW | No Violations | 1.00 |
-256869416 | 2017-10-24 0:00 | PW | No Violations | 0.40 |
0256869416 | 2017-10-24 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-0646. A review of RBDMS indicated that the owner was current with production. The access and locations were stable. Correct identification was present at the production tank. The 8.625 well head was above grade and open to atmosphere. The 4.5 production casing was equipped with a plunger lift assembly. Production valves were open. No leaks were observed. A stable earthen dike that was free of fluid was constructed around the production equipment. Equipment consisted of one (1) vertical separator and one (1) 100 bbl production tank. The separator remained in good repair with no leaks. The production tank remained in good repair and contained correct identification. Valves were closed and plugged. No violations were observed during this inspection. |
1022964107 | 2005-03-22 | Production Wells | No Violations | Separator repaired. Contamination removed. Recommend case be resolved. |
1090240096 | 2004-07-16 | Production Wells | Violations Noted | The tank battery consists of 1-210 bbl storage tank and no dike. |
1563293769 | 2019-7-16 0:00: | PW | No Violations | |
1848083487 | 2005-03-15 | Production Wells | Violations Noted | The problems under the load line have been resolved. The problem at the separator has worsened to the point that the separator is failing and sending fluid into the sales line and onto the ground. Called Paul Kramer and met him on site. The well was shut in. The problem will be corrected tomorrow. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1090240096 | US-OH-102089 | 2004-07-19 | Well operation causing pollution and contamination | |
1848083487 | US-OH-118484 | 2005-03-17 | Well operation causing pollution and contamination |
For data sources see[9]