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Well ID: 34-029-20642 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Knox Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: HE & ZE ECKERT UNIT | |
License Status: Producing | |
License Date: 1970-03-05 | |
Spud Date: 1979-04-19 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-05-03 | |
Well Total Depth: 5522.00 ft | |
Configuration: Vertical | |
Latitude: 40.830000 | |
Longitude: -81.050000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-03-05 | 9 EDC GeoDate 3/5/70 |
Completed | 1970-05-03 | |
Reached Total Depth | 1970-05-03 | |
Original Spud | 1979-04-19 | |
Change of Owner | 2008-07-21 | Operator changed from 9, POWER GAS MARKETING & TRANS to 1388, EXCO - NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5380 | 5451 | 0 |
5380 | 5451 | 0 | |
5380 | 5451 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 0 | 1000 Gal | 0 | MCA | ||
H2O | 0 | 1500 Bbl | 55000 | R.P. 48 HRS. |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1240133995 | 2017-10-24 0:00 | PW | No Violations | 0.50 |
-527491331 | 2004-7-16 0:00: | PW | No Violations | 0.50 |
0527491331 | 2004-07-16 | Production Wells | No Violations | The tank battery consists of 1-210 bbl storage tank and a low dike. |
1240133995 | 2017-10-24 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-0642. A review of RBDMS indicated that last reported production was 2014. The access and locations were stable. The 8.625 well head was below grade. The 4.5 production casing was equipped with a plunger lift assembly. The main gate valve was closed. No leaks were observed. A domestic supply connection was present and open. A worn earthen dike that was free of fluid was constructed around the production tank. The tank remained in good repair and contained correct identification. Valves were closed and plugged. A vertical separator was outside of the dike and not in use. The meter house did not contain a current production chart. While on location I called and left a voicemail with Enervest Superintendent Joe Teppert to determine the status of the well. |
1574105636 | 2019-11-18 0:00 | PW | No Violations | 1.00 |
For data sources see[9]