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Well ID: 34-029-20292 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: West Township | |
Operator Name: FOLTZ & FOLTZ LTD PARTNERSHIP | |
Well Pad ID: | |
Farm/Lease Name: SANOR | |
License Status: Final Restoration | |
License Date: 2017-09-15 | |
Spud Date: 1948-10-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1948-11-13 | |
Well Total Depth: 814.00 ft | |
Configuration: Vertical | |
Latitude: 40.780000 | |
Longitude: -81.020000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1948-10-21 | |
Completed | 1948-11-13 | |
Reached Total Depth | 1948-11-13 | |
APP | 2017-09-15 | Proposed Formations:BEREA, Issued Date:9/15/2017, Expired Date:9/15/2019 12:00:00 PM, Drilling unit acres:123, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-10-03 | |
Record Last Modified | 2018-06-16 | |
Construction Permit Expires | 2019-09-15 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | BLAIR BILL INC | 1652.00 | 485.00 | 365 |
1986 | BLAIR BILL INC | 1365.00 | 449.00 | 365 |
1987 | BLAIR BILL INC | 1284.00 | 381.00 | 365 |
1988 | BLAIR BILL INC | 1424.00 | 511.00 | 365 |
1989 | BLAIR BILL INC | 1427.00 | 306.00 | 365 |
1990 | BLAIR BILL INC | 1350.00 | 317.00 | 365 |
1991 | BLAIR BILL INC | 1262.00 | 301.00 | 365 |
1992 | BLAIR BILL INC | 1549.00 | 358.00 | 365 |
1993 | BLAIR BILL INC | 277.00 | 53.00 | 90 |
2017 | FOLTZ & FOLTZ LTD PARTNERSHIP | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | BLAIR BILL INC | Brine | 106 | 365 |
1986 | BLAIR BILL INC | Brine | 60 | 365 |
1987 | BLAIR BILL INC | Brine | 80 | 365 |
1988 | BLAIR BILL INC | Brine | 120 | 365 |
1989 | BLAIR BILL INC | Brine | 80 | 365 |
1990 | BLAIR BILL INC | Brine | 60 | 365 |
1991 | BLAIR BILL INC | Brine | 90 | 365 |
1992 | BLAIR BILL INC | Brine | 45 | 365 |
1993 | BLAIR BILL INC | Brine | 20 | 90 |
2017 | FOLTZ & FOLTZ LTD PARTNERSHIP | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0338106409 | 2017-10-03 | Plug / Plug Back | No Violations | The purpose of my inspection was to witness plug and abandonment activities on well #2-0292. I witnessed owner Bob Foltz pulled 62,000 pounds of weight against the 5 production/intermediate casing without observing any movement. In a further attempt to recover 5 casing from the well, Mr. Foltz attached a lifting joint onto the casing in an attempt to unscrew the casing. This attempt to recover failed also. Mr. Foltz bailed the well dry prior to pouring in the top plug of 9 sack grout. The well was dead prior to pouring in the grout. R.W. Sidley delivered 5 yards of 9 sack grout. The grout was poured into the open well and brought to surface. The lined earthen pit dug was holding fluid and maintained freeboard. The location remained stable. I will schedule to document the status of the surface plug prior to attaching a monument plate and backfill. No violations were observed during this inspection. |
0702931208 | 2018-06-12 | Final Restoration | No Violations | The purpose of my inspection was to determine the status of final restoration on well #2-0292. At the time of my inspection, the working pit was backfilled and the location graded to local contour. Vegetation was established. No signs of erosion or sedimentation were observed. All equipment and debris utilized in plug and abandonment was removed. The access road was utilized by the landowner for commercial purposes and well #2-1231. The location has passed the requirements for final restoration. |
0710595515 | 2017-10-03 | Plug / Plug Back | No Violations | The purpose of my inspection was to witness plug and abandonment activities on well #2-0292. Owner Bob Foltz had placed the bottom plug on 10/02/2017 and reported that he was unable to pull the 5 intermediate/production casing. I arrived on location and witnessed Mr. Foltz make a second attempt to pull the intermediate/production casing. The weight indicator indicated 62,000 lbs and no casing movement was observed. Mr. Foltz continued to attempt to recover casing by attempting to unscrew the casing at the surface and was unsuccessful in his attempt. The top of the previous cement plug was measured at 608 below surface. R.W. Sidley delivered 3.0 yards of 9 sack grout. The grout was poured into the well bore and was brought to surface. The earthen pit remained holding fluid and maintained free board. No violations were observed this inspection. |
338106409 | 2017-10-3 0:00: | PB | No Violations | |
702931208 | 2018-6-12 0:00: | FR | No Violations | 0.20 |
710595515 | 2017-10-3 0:00: | PB | No Violations | 2.50 |
For data sources see[7]