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34-019-22504

Well Details

Well ID: 34-019-22504
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Country: United States
State: Ohio
County: Carroll
Municipality: Fox Township
Operator Name: CHESAPEAKE EXPLORATION LLC
Well Pad ID: US-OH-000802
Farm/Lease Name: LAFFERTY 17-13-4
License Status: Final Restoration
License Date: 2017-09-12
Spud Date: 2013-10-12
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Horizontal
Latitude: 40.610000
Longitude: -80.910000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-09-30 Proposed Formations:TRENTON-BLACK RIVER, Issued Date:9/30/2013, Expired Date:9/30/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2013-10-09 Proposed Formations:POINT PLEASANT, Issued Date:10/9/2013, Expired Date:10/9/2015 12:00:00 PM, Drilling unit acres:147.97, Proposed Well Type:OG, Proposed Well Class:EDPW
APP 2015-09-28 Proposed Formations:POINT PLEASANT, Issued Date:9/28/2015, Expired Date:9/27/2017 12:00:00 PM, Drilling unit acres:147.97, Proposed Well Type:OG, Proposed Well Class:POOL
APP 2017-09-12 Proposed Formations:TOP SOIL, Issued Date:9/12/2017, Expired Date:9/12/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-09-14
Record Last Modified 2018-08-17
Construction Permit Expires 2019-09-12

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-969727562 2017-9-18 0:00: FR No Violations 1.00
0969727562 2017-09-18 Final Restoration No Violations I conducted a final restoration of the well after the conductor hole was plugged by the operator on 09/14/2017. As per Chesapeake representative, cement was found to be at surface on 09/15/2017 and was then cut 34 below grade and capped with a steel plate. The tin horn of the cellar was removed, and the cellar was filled in with gravel. This well was never put in production, so no production equipped was placed on site. There is one other producing well (34-019-2-2506-00-00) on the pad with production equipment.
1382463770 2013-10-13 Drill / Deepen / Reopen No Violations I was on site to witness the cementing of the 20 inch conductor casing. My inspection revealed that Precision has drilled a 26 inch hole to a total depth of 120 feet and ran 120 feet of 20 inch casing (94 pound per foot/ inside diameter 19.124 inches) into the well bore. Allied cemented the casing with 250 sacks of ClassA 2% CaCl and 1/2 pound per sack flake. The cement had a density of 15.6, a yield of 1.2 cubic feet per sack, and they used 5.25 gallons of mix water per sack. They pumped 53.4 barrels of cement slurry, 39 barrels of freshwater displacement, and there was 11 barrels of cement returns to surface. My inspection revealed no violations at this time.
1505928873 2017-09-14 Plug / Plug Back No Violations

For data sources see[3]

References