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Well ID: 34-019-21273 | Loading map...
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Country: United States | |
State: Ohio | |
County: Carroll | |
Municipality: Orange Township | |
Operator Name: BELDEN & BLAKE CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: MILLER C | |
License Status: Plugged and Abandoned | |
License Date: 2004-12-09 | |
Spud Date: 1979-06-24 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1979-06-30 | |
Well Total Depth: 5751.00 ft | |
Configuration: Vertical | |
Latitude: 40.470000 | |
Longitude: -81.230000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-03-26 | 182 BELDEN & BLAKE CO GeoDate 3/26/79 |
Original Spud | 1979-06-24 | |
Completed | 1979-06-30 | |
Reached Total Depth | 1979-06-30 | |
APP | 2004-12-09 | Proposed Formations:CLINTON, Issued Date:12/9/2004, Expired Date:12/9/2005 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2005-09-12 | |
Construction Permit Expires | 2005-12-09 | |
Change of Owner | 2007-04-27 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC well was plugged prior to transfer |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2005-09-06 | 5596 | 5616 | 0 |
5596 | 5616 | 0 | |
5596 | 5616 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 755 Bbl | 90000 | |||
H2O | 0 | 775 Bbl | 90000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ENTERPRISE ENERGY CORP | 1650.00 | 604.00 | 0 |
1985 | OXFORD OIL | 1114.00 | 597.00 | 365 |
1986 | OXFORD OIL | 1028.00 | 411.00 | 365 |
1988 | OXFORD OIL | 1152.00 | 381.00 | 365 |
1990 | BELDEN & BLAKE CORPORATION | 903.00 | 98.00 | 306 |
1997 | BELDEN & BLAKE CORPORATION | 472.00 | 81.00 | 181 |
1998 | BELDEN & BLAKE CORPORATION | 610.00 | 164.00 | 286 |
1999 | BELDEN & BLAKE CORPORATION | 76.00 | 90.00 | 112 |
2000 | BELDEN & BLAKE CORPORATION | 679.00 | 87.00 | 345 |
2001 | BELDEN & BLAKE CORPORATION | 543.00 | 183.00 | 152 |
2002 | BELDEN & BLAKE CORPORATION | 0.00 | 0.00 | 201 |
2003 | BELDEN & BLAKE CORPORATION | 0.00 | 0.00 | 313 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ENTERPRISE ENERGY CORP | Brine | 150 | 0 |
1985 | OXFORD OIL | Brine | 0 | 365 |
1986 | OXFORD OIL | Brine | 0 | 365 |
1988 | OXFORD OIL | Brine | 0 | 365 |
1990 | BELDEN & BLAKE CORPORATION | Brine | 70 | 306 |
1997 | BELDEN & BLAKE CORPORATION | Brine | 153 | 181 |
1998 | BELDEN & BLAKE CORPORATION | Brine | 57 | 286 |
1999 | BELDEN & BLAKE CORPORATION | Brine | 36 | 112 |
2000 | BELDEN & BLAKE CORPORATION | Brine | 79 | 345 |
2001 | BELDEN & BLAKE CORPORATION | Brine | 75 | 152 |
2002 | BELDEN & BLAKE CORPORATION | Brine | 0 | 201 |
2003 | BELDEN & BLAKE CORPORATION | Brine | 0 | 313 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-11836733 | 2005-9-7 0:00:0 | PB | No Violations | 2.00 |
-206544204 | 2005-8-31 0:00: | PB | No Violations | 1.00 |
-295167734 | 2005-9-6 0:00:0 | PB | No Violations | 2.00 |
-657673559 | 2005-9-8 0:00:0 | DD | No Violations | 2.00 |
0011836733 | 2005-09-07 | Plug / Plug Back | No Violations | Inspection revealed that the service rig is still fishing for the 1 1/2 tubing . No violations at this time . |
0206544204 | 2005-08-31 | Plug / Plug Back | No Violations | Rig crew suppose to be on location with fishing tools this morning to fish out the 1 1/2 tubing . The rig crew never showed up today . I called Dennis Weiss later on in the day and he advised that they would be out tomorrow morning . |
0295167734 | 2005-09-06 | Plug / Plug Back | No Violations | Inspection revealed that the service rig is still fishing for the 1 1/2 tubing . No violations at this time . Note: the plugging pit has been lined . |
0657673559 | 2005-09-08 | Drill / Deepen / Reopen | No Violations | The service rig has tripped the 1 1/2 tubing out of the well and are ready to run the 2 3/8 upset tubing back into the well to pump the bottom hole plug on Friday . No violations at this time . |
1645860959 | 2005-08-30 | Plug / Plug Back | No Violations | On site to witness the bottom hole plug thru the 1 1/2 tubing . Goimg to have Omega break circulation and then pump the bottom plug . Interden service rig was pulling on the tubing because they found that the tubing was hung in the hole . While pulling on the tubing it parted app. 10 feet down hole . They went back in and tagged the top of it but didnt get screwed back onto the tubing . Rig operator (Phil) advised Omega that they might as well leave location because they wouldnt be doing any plugging today . |
2007962021 | 2005-09-01 | Plug / Plug Back | No Violations | Interden rig crew on site with fishing tools . Ran fishing tools into the well and got ahold of the 1 1/2 tubing . With the rig in 5th gear and idling , they pulled the tubing up and set it in the slips . John Hudson arrived on site to shoot off the tubing . He tried several times to get the shot tool down the tubing . The even tied a sucker rod on the bottom of the shot tool to give it more weight , but it still wouldnt go down the tubing . They tried until app. 7:30 pm to get down the tubing , but could only get to 1663. John advised that he wasnt going to try to get down the tubing anymore . I advised that they needed to get the tubing out of the well before they could pump the bottom hole plug . |
For data sources see[9]