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34-019-20620

Well Details

Well ID: 34-019-20620
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Country: United States
State: Ohio
County: Carroll
Municipality: Rose Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: SILVIS UNIT
License Status: Final Restoration
License Date: 1980-10-26
Spud Date: 1972-09-07
Spud Drilling Contractor:
Final Drill Date: 1972-10-10
Well Total Depth: 5553.00 ft
Configuration: Vertical
Latitude: 40.590000
Longitude: -81.240000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1972-09-07
Completed 1972-10-10
Reached Total Depth 1972-10-10
CO 1980-10-26 311 STOCKER & SITLER INC GeoDate 10/26/80
Change of Owner 2003-09-08 Operator changed from 311, STOCKER & SITLER INC to 28, CGAS EXPLORATION
Change of Owner 2007-04-27 Operator changed from 28, CGAS EXPLORATION to 7578, ENERVEST OPERATING LLC
Record Last Modified 2016-09-26

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5382 5412 0
5382 5412 0
5382 5412 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 3700 Bbl 70000

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1330518409 2012-02-28 Final Restoration No Violations I could not locate the well during this production well status check. The site now has a pole barn and a camping trailer on it. When I checked the records in our database I found a plugging report dated 11-18-1980. I contacted the Steve Opritza in the DNR Permitting Department (614-265-6442) and he advised me to do a final restoration and he would amend the database to reflect this Plug and Abandon. I checked for flow lines and a tank battery and neither could be found. The Final Restoration can be passed and no violations are noted at this time.

For data sources see[5]

References