X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-019-20564

Well Details

Well ID: 34-019-20564
Loading map...
Country: United States
State: Ohio
County: Carroll
Municipality: Rose Township
Operator Name: RANGE RESOURCES-APPALACHIA LLC
Well Pad ID:
Farm/Lease Name: HARSHA-JOHNSTONE UNIT
License Status: Final Restoration
License Date: 1971-08-27
Spud Date: 1971-08-29
Spud Drilling Contractor: FLANIGAN BROS
Final Drill Date: 1971-09-08
Well Total Depth: 5243.00 ft
Configuration: Vertical
Latitude: 40.600000
Longitude: -81.290000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1971-08-27 139 MB OPERATING CO INC GeoDate 8/27/71
Original Spud 1971-08-29 GL=1022.3, KB=1032.3
Completed 1971-09-08 GL=1022.3, KB=1032.3
Reached Total Depth 1971-09-08 GL=1022.3, KB=1032.3
Completion Report Received 1971-11-08 GL=1022.3, KB=1032.3
APP 1999-05-12 139 MB OPERATING CO INC Proposed Formation CLINTON SAND Issued Date 5/12/99 Expired Date 5/11/00 6:00:00 AM
Plugged/Abandoned 1999-07-23 GL=1022.3, KB=1032.3
Change of Owner 2000-06-30 Operator changed from 139, MB OPERATING CO INC to 6674, GREAT LAKES ENERGY PTNSHP LLC
Record Last Modified 2017-02-15 GL=1022.3, KB=1032.3

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1999-05-12 5088 5146 19
5088 5146 19
5088 5146 19

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 4620 Bbl 55000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 MB OPERATING CO INC 1571.00 251.00 0
1985 MB OPERATING CO INC 1085.00 226.00 365
1986 MB OPERATING CO INC 173.00 136.00 365
1987 MB OPERATING CO INC 26.00 96.00 365
1988 MB OPERATING CO INC 30.00 102.00 366
1989 MB OPERATING CO INC 9.00 86.00 365
1990 MB OPERATING CO INC 42.00 57.00 365
1991 MB OPERATING CO INC 24.00 157.00 365
1992 MB OPERATING CO INC 5.00 760.00 366
1993 MB OPERATING CO INC 0.00 505.00 365
1994 MB OPERATING CO INC 0.00 367.00 365
1995 MB OPERATING CO INC 0.00 332.00 365
1996 MB OPERATING CO INC 0.00 190.00 366
1997 MB OPERATING CO INC 0.00 134.00 365
1998 MB OPERATING CO INC 0.00 0.00 365
1999 MB OPERATING CO INC 0.00 0.00 273

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 MB OPERATING CO INC Brine 0 0
1985 MB OPERATING CO INC Brine 35 365
1986 MB OPERATING CO INC Brine 0 365
1987 MB OPERATING CO INC Brine 0 365
1988 MB OPERATING CO INC Brine 70 366
1989 MB OPERATING CO INC Brine 0 365
1990 MB OPERATING CO INC Brine 0 365
1991 MB OPERATING CO INC Brine 0 365
1992 MB OPERATING CO INC Brine 595 366
1993 MB OPERATING CO INC Brine 265 365
1994 MB OPERATING CO INC Brine 140 365
1995 MB OPERATING CO INC Brine 110 365
1996 MB OPERATING CO INC Brine 110 366
1997 MB OPERATING CO INC Brine 0 365
1998 MB OPERATING CO INC Brine 0 365
1999 MB OPERATING CO INC Brine 70 273

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1264954924 2011-08-02 Final Restoration No Violations According to our database, this well was plugged on 07-23-1999. No visual evidence of well or production equipment. Site is a private lake and campground. Final Restoration passed.

For data sources see[9]

References