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34-019-20373

Well Details

Well ID: 34-019-20373
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Country: United States
State: Ohio
County: Carroll
Municipality: Rose Township
Operator Name: G & O RESOURCES LTD
Well Pad ID:
Farm/Lease Name: SHIRLEY ET AL UNIT
License Status: Plugged and Abandoned
License Date: 2019-09-06
Spud Date: 1968-08-27
Spud Drilling Contractor:
Final Drill Date: 1968-09-09
Well Total Depth: 5400.00 ft
Configuration: Vertical
Latitude: 40.610000
Longitude: -81.260000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1968-08-08 311 STOCKER & SITLER INC GeoDate 8/8/68
Original Spud 1968-08-27 IP. GAS = 50.3 MCFG
Completed 1968-09-09 IP. GAS = 50.3 MCFG
Reached Total Depth 1968-09-09 IP. GAS = 50.3 MCFG
Change of Owner 1999-07-20 Operator changed from 311, STOCKER & SITLER INC to 5785, M-J OIL COMPANY INC.
Change of Owner 2001-03-13 Operator changed from 5785, M-J OIL COMPANY INC. to 5894, G & O RESOURCES LTD
Record Last Modified 2013-12-31 IP. GAS = 50.3 MCFG

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5239 5279 2
5239 5279 2
5239 5279 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1310 Bbl 75000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 STOCKER & SITLER INC 598.00 529.00 365
1985 STOCKER & SITLER INC 795.00 301.00 0
1986 STOCKER & SITLER INC 2193.00 820.00 365
1987 STOCKER & SITLER INC 454.00 190.00 365
1988 STOCKER & SITLER INC 569.00 354.00 0
1989 STOCKER & SITLER INC 525.00 378.00 365
1990 STOCKER & SITLER INC 908.00 592.00 365
1991 STOCKER & SITLER INC 438.00 285.00 365
1992 STOCKER & SITLER INC 495.00 240.00 365
1993 STOCKER & SITLER INC 433.00 146.00 365
1994 STOCKER & SITLER INC 734.00 163.00 0
1995 STOCKER & SITLER INC 24.00 265.00 0
1996 STOCKER & SITLER INC 0.00 126.00 0
1997 STOCKER & SITLER INC 0.00 105.00 365
1998 STOCKER & SITLER INC 28.00 240.00 365
1999 M-J OIL COMPANY INC. 0.00 117.00 100
2000 M-J OIL COMPANY INC. 158.00 350.00 365
2001 M-J OIL COMPANY INC. 0.00 44.00 49
2002 G & O RESOURCES LTD 0.00 198.00 365
2003 G & O RESOURCES LTD 0.00 141.00 365
2004 G & O RESOURCES LTD 0.00 152.00 365
2005 G & O RESOURCES LTD 63.00 128.00 365
2006 G & O RESOURCES LTD 256.00 68.00 365
2007 G & O RESOURCES LTD 282.00 105.00 365
2008 G & O RESOURCES LTD 188.00 34.00 366
2009 G & O RESOURCES LTD 264.00 53.00 365
2010 G & O RESOURCES LTD 206.00 0.00 365
2011 G & O RESOURCES LTD 161.00 0.00 365
2012 G & O RESOURCES LTD 132.00 0.00 366
2013 G & O RESOURCES LTD 0.00 0.00 0
2014 G & O RESOURCES LTD 0.00 0.00 0
2015 G & O RESOURCES LTD 0.00 0.00 0
2016 G & O RESOURCES LTD 0.00 0.00 0
2017 G & O RESOURCES LTD 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 STOCKER & SITLER INC Brine 0 365
1985 STOCKER & SITLER INC Brine 0 0
1986 STOCKER & SITLER INC Brine 0 365
1987 STOCKER & SITLER INC Brine 0 365
1988 STOCKER & SITLER INC Brine 0 0
1989 STOCKER & SITLER INC Brine 0 365
1990 STOCKER & SITLER INC Brine 0 365
1991 STOCKER & SITLER INC Brine 0 365
1992 STOCKER & SITLER INC Brine 0 365
1993 STOCKER & SITLER INC Brine 0 365
1994 STOCKER & SITLER INC Brine 0 0
1995 STOCKER & SITLER INC Brine 0 0
1996 STOCKER & SITLER INC Brine 0 0
1997 STOCKER & SITLER INC Brine 38 365
1998 STOCKER & SITLER INC Brine 36 365
1999 STOCKER & SITLER INC Brine 0 365
2000 M-J OIL COMPANY INC. Brine 157 365
2001 M-J OIL COMPANY INC. Brine 30 49
2002 G & O RESOURCES LTD Brine 177 365
2003 G & O RESOURCES LTD Brine 108 365
2004 G & O RESOURCES LTD Brine 55 365
2005 G & O RESOURCES LTD Brine 49 365
2006 G & O RESOURCES LTD Brine 18 365
2007 G & O RESOURCES LTD Brine 39 365
2008 G & O RESOURCES LTD Brine 0 366
2009 G & O RESOURCES LTD Brine 0 365
2010 G & O RESOURCES LTD Brine 0 365
2011 G & O RESOURCES LTD Brine 0 365
2012 G & O RESOURCES LTD Brine 0 366
2013 G & O RESOURCES LTD Brine 0 0
2014 G & O RESOURCES LTD Brine 0 0
2015 G & O RESOURCES LTD Brine 9 0
2016 G & O RESOURCES LTD Brine 0 0
2017 G & O RESOURCES LTD Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1974656953 2019-10-30 0:00 PB No Violations 1.50
-1991346564 2019-10-31 0:00 PB No Violations 6.50
-273465258 2019-9-24 0:00: PW No Violations 1.00
-353718006 2019-11-3 0:00: PW No Violations 8.50
-456313649 2018-9-20 0:00: PW No Violations
-579454337 2012-4-13 0:00: PW No Violations
-734118963 2019-11-1 0:00: PB No Violations 7.50
0579454337 2012-04-13 Production Wells No Violations The well has reported production and no violations are noted athis time.
1428947082 2015-03-24 Production Wells Violations Noted I conducted a status check of this well with DOGRM inspector Heidi Scott. During our inspection, we found the well to be equipped with an electrically-driven pumpjack. The valves appeared to be open. The polish rod appeared to be lubricated. The guard for the drive belts on the pumpjack was not installed, and lay on the ground next to the pumpjack. About a gallon of oil lay pooled around the wellhead casing. The tank battery is equipped with two-210 bbl production tanks, an oil and gas heater treater separator, a vertical separator, and meter run with a drip bottle. There was a plug in the valve for the oil pick-up line. Oil staining was observed at the base of the oil pickup line for the production tanks. An identification sign is present on one of the production tanks, but the writing was not legible. The dike surrounding the tank battery is in poor repair. The lease road is stable and drivable. A review of production records in the state database indicates that the last reported production for the well was in 2012. Due to failure to keep the dike area free of oil and water, lack of proper identification, the uninstalled belt guard, and worn dike, a Compliance Notice is being issued. The oil around the wellhead must be removed and the casing leak repaired, proper identification must be installed, the belt guard must be installed, the oil-impacted soil within the dike removed, and the dike upgraded by May 13, 2015.
1536562697 2015-05-07 Production Wells No Violations I conducted a compliance follow-up inspection of the tank battery. At time of inspection, the heater treater tank had been removed. The production tanks had been emptied and steam-cleaned, and were on site pending removal. The contaminated soil inside the tank battery had been removed.
1921149815 2019-04-24 Production Wells No Violations The well was equipped with a pumping unit. The production valves appeared in the closed position. the last reported production for the well was 132 mcf of gas in 2012. I will speak to the operator regarding the plugging/producing status of the well. I spoke to the operator regarding low electrical lines on the property leading to the well, and was informed they will have an electrician move the lines to a safe position.
2097450863 2019-7-23 0:00: PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1428947082 US-OH-112525 2018-10-15 General Safety
1428947082 US-OH-112526 2018-10-15 Failure to legibly identify well
1428947082 US-OH-112527 2018-10-15 No SPCC dike/or failure to keep dike free of water or oil

For data sources see[9]

References