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34-013-21081

Well Details

Well ID: 34-013-21081
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Country: United States
State: Ohio
County: Belmont
Municipality: Colerain Township
Operator Name: ASCENT RESOURCES UTICA LLC
Well Pad ID: US-OH-001392
Farm/Lease Name: SEABRIGHT CLR BL
License Status: Final Restoration
License Date: 2016-07-14
Spud Date: 2016-10-28
Spud Drilling Contractor: FALCON DRLG
Final Drill Date:
Well Total Depth: 1769.00 ft
Configuration: Horizontal
Latitude: 40.100000
Longitude: -80.800000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2016-07-14 Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:7/14/2016, Expired Date:7/14/2018 12:00:00 PM, Drilling unit acres:604.313, Proposed Well Type:OG, Proposed Well Class:FWC
Plugged/Abandoned 2016-11-12
Completion Report Received 2017-03-28
Construction Permit Expires 2018-07-14
Record Last Modified 2018-07-24

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-489058202 2016-11-8 0:00: DD No Violations 3.00
-496960189 2017-5-4 0:00:0 FR No Violations 1.00
-704501536 2016-11-9 0:00: DD No Violations 2.00
0489058202 2016-11-08 Drill / Deepen / Reopen No Violations The casing run was unsuccessful and the company had elected to remove the casing from the well bore and attempt a ream and clean out cycle to begin attempts to run the 13.375 casing again.
0496960189 2017-05-04 Final Restoration No Violations The final restoration for this well is complete as the well has been plugged. The restoration for the well site pad disturbance area is required to be remediated once all other wells on this pad are plugged. Final restoration passed.
0704501536 2016-11-09 Drill / Deepen / Reopen No Violations Falcon Rig 26 has pulled that casing and begun drilling again to condition the hole and attempt to run the 13.375 casing string again.
1146871483 2016-11-09 Drill / Deepen / Reopen No Violations Falcon Rig 26 is attempting to run the 13.375 casing with little success. They will continue their attempt. I will check back in the later today.
1281565814 2016-11-03 Drill / Deepen / Reopen No Violations Falcon Rig 26 was drilling the 17.5 open hole section of the well bore. The 13.375 casing is anticipated to be set tomorrow.
1472480317 2016-08-26 Casing String Witnessed No Violations
1478700569 2016-11-08 Drill / Deepen / Reopen No Violations Falcon 26 was on attempting to run the 13.375 surface casing to total depth and O-Tex was on site to cement the casing.
1479132936 2016-11-12 Plug / Plug Back No Violations
1729785697 2016-11-10 Plug / Plug Back No Violations The operator has decided to deem this well a lost hole and begin plugging operations. They will attempt to go into the hole with open ended drill string and cement through the same. If that does not work they will put a bit on, drill back to total depth and cement through the bit.

For data sources see[3]

References