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34-013-21051

Well Details

Well ID: 34-013-21051
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Country: United States
State: Ohio
County: Belmont
Municipality: Goshen Township
Operator Name: RICE DRILLING D LLC
Well Pad ID: US-OH-001394
Farm/Lease Name: TUNA NUT
License Status: Producing
License Date: 2016-09-09
Spud Date: 2016-08-21
Spud Drilling Contractor: PATTERSON DRILLING
Final Drill Date: 2016-11-24
Well Total Depth: 16624.00 ft
Configuration: Horizontal
Latitude: 39.950000
Longitude: -81.070000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2016-04-15 Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:4/15/2016, Expired Date:4/15/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2016-09-09 Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:9/9/2016, Expired Date:9/9/2018 12:00:00 PM, Drilling unit acres:534.7995, Proposed Well Type:OG, Proposed Well Class:NWC
Correction to Well 2016-11-04 UNIT SIZE DECREASED TO 327.4260 ACRES.
Reached Total Depth 2016-11-24
Correction to Well 2017-02-24 UPDATE TAKEPOINT/TARGET PER AS-DRILLED PLAT-ALE
Completion Report Received 2017-08-09
Correction to Well 2017-09-08 UPDATE TAKE/ACREAGE PER AS-DRILLED RCVD 8-10-17 ALE.
Record Last Modified 2018-07-24
Construction Permit Expires 2018-09-09

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2017-08-24 8974 9111 24
2017-08-24 16500 16540 30
16500 16540 30
8974 9111 24
8974 9111 24

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2017-03-29 H2O 15 9766 Bbl 455220 STINGRAY PRESSURE PUMPING LLC STAGE 1/45

STAGES 2-44 SEE IMAGES

2017-05-09 H2O 15 9632 Bbl 500680 STINGRAY PRESSURE PUMPING LLC STAGE 45/45

STAGES 2-44 SEE IMAGES

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2016 RICE DRILLING D LLC 0 0 0
2017 RICE DRILLING D LLC 2479615 0 188
2018 RICE DRILLING D LLC 3606864 0 332
2019 RICE DRILLING D LLC 567996 0 90

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2016 RICE DRILLING D LLC Brine 1821 0
2017 RICE DRILLING D LLC Brine 18576 188
2018 RICE DRILLING D LLC Brine 56515 332
2019 RICE DRILLING D LLC Brine 15668 90

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1384095310 2018-9-19 0:00: PW No Violations 0.50
0157529777 2016-10-12 Drill / Deepen / Reopen No Violations On location for a site inspection. The rig is currently troubleshooting pressure issues they are having when mist drilling in the 17.5 hole. There were no problems noted at the time of the inspection.
1384095310 2018-09-19 Production Wells No Violations On the day of my inspection I witnessed that the well was equipped with 5.5 inch diameter production casing, Annular pressure monitoring was in place on both the 9.625-inch diameter casing gauge read 840 pounds per square inch, the 13.375-inch diameter casing gauge read 160 pounds per square inch. Pressure release lines have been installed from the 9.625-inch diameter casing to the production fluid tanks, the 13.375-inch diameter casing had pressure release lines that vented to atmosphere. Production equipment included 2 sand traps for each well an individual Gas Processing unit, and 4- 400-barrel production fluid tanks shared with the other producing wells on the pad. The well pad and all equipment were within earthen containment with secondary containment around the production tanks. There was flow back equipment still on location including 4 additional sand traps and 8- 500-barrel mobile fluid storage tanks on location with secondary containment, flowback equipment was no longer attached to the well head. There were multiple Emergency Shutoff Devices on location, Identification tag were present, and production was current.
1534806175 2020-3-23 0:00: PW No Violations 0.20
1554612552 2019-03-21 Preliminary Restoration No Violations Preliminary Restoration status check inspection found the well site meets ORC 1509.072 with erosion control in place and vegetation established. The perimeter sediment control filter sock has been removed. The well pad and lease road surface is stone construction and in good repair. The well pad perimeter is protected by an earthen berm. 4 wells are present and producing on the well pad, the wells are equipped with production trees with emergency shut down devices in place. Annular pressure monitoring is also installed on the well head A&B sections. Proper identification is posted on the well heads with hazard warning labels on the production tanks. There are (4) 400 barrel tanks present inside a polymer lined steel containment dike area. 4 gas processing units are present on the pad. I contacted Bruce Gallick with the company and asked that he address the plugging and cutting off 30 below grade of the Mouse Holes.
157529777 2016-10-12 0:00 DD No Violations
1940233076 2016-08-22 Casing String Witnessed No Violations

For data sources see[9]

References