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34-013-20823

Well Details

Well ID: 34-013-20823
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Country: United States
State: Ohio
County: Belmont
Municipality: Somerset Township
Operator Name: GULFPORT APPALACHIA LLC
Well Pad ID: US-OH-001085
Farm/Lease Name: MCLAUGHLIN 210272
License Status: Producing
License Date: 2014-07-29
Spud Date: 2014-08-05
Spud Drilling Contractor: PATTERSON DRILLING
Final Drill Date: 2014-12-26
Well Total Depth: 15485.00 ft
Configuration: Horizontal
Latitude: 39.900000
Longitude: -81.200000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2014-07-29 Proposed Formations:UTICA/POINT PLEASANT, Issued Date:7/29/2014, Expired Date:7/28/2016 12:00:00 PM, Drilling unit acres:427.125, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2014-12-26
Completion Report Received 2015-12-01
Correction to Well 2015-12-18 TARGET/TAKEPOINT CHANGE PER AS-DRILLED PLAT-ALE
Construction Permit Expires 2016-07-28
Record Last Modified 2017-10-24

For data sources see[2]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 07/04/2015 08/01/2015 8721 7,263,900.0 0

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 B-84 X-Chem, LLC Biocide Glutaraldehyde 111-30-8 27 0.010032 0
n-Alkyl dimethyl benzyl ammonium chloride 68424-85-1 5.5 0.00204355 0
Water 7732-18-5 55.5 0.0206213 0
Didecyl dimethyl ammonium chloride 7173-51-5 8 0.00297244 0
Ethanol 64-17-5 4 0.00148622 0
Plexgel 907L-EB Chemplex SOLVAY Viscosifier Alcohol ethoxylate 34398-01-1 0.99 0.00003352 0
Guar Gum 9000-30-0 50 0.00169304 0
Cyrstalline Silica 14808-60-7 0.06 0.00000203 0
Organophylic Clay Proprietary 2 0.00006772 0
Distillate(petroleum), hydrotreated light 64742-47-8 50 0.00169304 0
FRA 409 Weatherford Friction Reducer Proprietary Proprietary 30 0.0333335 0
Ethanaminium, N,N,N-trimethyl-2-[(1-oxo-2-propenyl)oxy]-,

chloride, polymer with 2-propenamide

69418-26-4 70 0.0777782 0
Petroleum Distillate 64742-47-8 10 0.0111112 0
Alcohols, C12-14-secondary, ethoxylated 84133-50-6 5 0.00555559 0
Adipic acid 124-04-9 3 0.00333335 0
SC-30 X-Chem, LLC Scale Inhibitor Sodium Polyacrylate Proprietary 30 0.00341513 0
Water 7732-18-5 70 0.00796863 0
TCA 6038F X-Chem, LLC Corossion Inhibitor Water 7732-18-5 80 0.00234203 0
Methanol 67-56-1 20 0.000585507 0
Muriatic Acid Axiall, LLC Acid Water 7732-18-5 60 0.147672 0
Hydrogen chloride 7647-01-0 40 0.0984479 0
Fresh water Stingray Carrier Water 7732-18-5 100 87.1338 0
100 mesh Minerva/Cadiz Proppant Sand 14808-60-7 100 1.30298 0
40/70 White Steubenville/Cadiz Proppant Sand 14808-60-7 100 11.1506 0
Breaker 3l Weatherford Breaker Potassium Chloride 7447-40-7 10 0.00005918 0
Sodium Chlorite 7758-19-2 5 0.00002959 0
Sodium Chloride 7647-14-5 40 0.000236729 0
Water 7732-18-5 45 0.000266321 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2015-08-01 H2O 10 198786 Gal 275540 STINGRAY PRESSURE PUMPING LLC STAGE 33/33

50 SHOTS

2015-07-03 H2O 10 285222 Gal 275020 STINGRAY PRESSURE PUMPING LLC STAGE 1/33

50 SHOTS

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2015 GULFPORT ENERGY CORPORATION 944430 611 100
2016 GULFPORT ENERGY CORPORATION 2685713 24 361
2017 GULFPORT ENERGY CORPORATION 961216 1 365
2018 GULFPORT ENERGY CORPORATION 564958 1 360
2019 GULFPORT ENERGY CORPORATION 92513 0 90

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2015 GULFPORT ENERGY CORPORATION Brine 7662 100
2016 GULFPORT ENERGY CORPORATION Brine 18446 361
2017 GULFPORT ENERGY CORPORATION Brine 7625 365
2018 GULFPORT ENERGY CORPORATION Brine 4550 360
2019 GULFPORT ENERGY CORPORATION Brine 1055 90

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1027933599 2014-10-3 0:00: CS No Violations 8.00
-1424938738 2014-10-19 0:00 CS No Violations 8.00
-1525088983 2017-9-26 0:00: PW No Violations 1.00
-1770088206 2014-9-30 0:00: DD No Violations 2.00
-2143562587 2017-12-19 0:00 PW No Violations 1.00
-45982972 2014-8-6 0:00:0 CS No Violations 5.50
0045982972 2014-08-06 Casing String Witnessed No Violations On the date of inspection I accompanied ODNR Inspector Andrew Corder to witness the cementing of the conductor string. Refer to Andrew Corders report for further details.
0364034504 2016-03-14 Preliminary Restoration No Violations On this day I visited this pad to perform a preliminary restoration inspection. The pad appeared to be in satisfactory condition. Vegetation has been established and the erosion and sediment controls appear to be functioning properly. Preliminary restoration for this site has passed.
0415856132 2014-11-04 Drill / Deepen / Reopen No Violations
0516866016 2014-08-06 Casing String Witnessed No Violations On the day of my inspection the 30 conductor casing was ran and cemented. See casing ticket for details. No violations noted.
0853072160 2014-12-17 Drill / Deepen / Reopen No Violations Company plans to fish drill pipe out of the hole to approx. 20 degrees into the lateral and set a cement plug. Then they will kick off and sidetrack around the previous drilled hole where the drill string remains. No violations noted.
0965597055 2018-06-19 Production Wells No Violations On the day of my inspection I witnessed that the well was equipped with 5.5 inch diameter production casing that was open flowing. Annular pressure monitoring was in place, the intermediate casing gauge read 50 pounds per square inch, the surface casing gauge read 125 pounds per square inch. Production equipment included a Sand Separator, Gas Processing unit, 4- 400 barrel purge tanks, and a 50 barrel produced water tank shared with 34013208240000, 34013208250000, 34013208850000. Identification tags were present, and production was up to date. No violations were found at the time of my inspection.
1027933599 2014-10-03 Casing String Witnessed No Violations On the day of my inspection the 18.625 surface casing was ran and cemented. See cement ticket for details. No violations noted.
1412346744 2014-09-30 Drill / Deepen / Reopen No Violations Arrived onsite to witness the cementing of a surface casing. Rig cannot get passed a depth of 250 in the hole. Operator is going to pull casing and try to ream the hole. Will return when job is going to occur.
1415191279 2014-11-03 Drill / Deepen / Reopen No Violations I visited the McLaughlin 3-A well in response to a spill incident that took place 11/01/2014. Dave Ball was first responder on the day of the incident. There was an estimated amount of 75 bbl of SOBM dispersed onto the location. A majority of the dispersal was on the rig. There was a portion of the pad area that was affected as well as an area off the pad that had a light mist of SOBM that needed remediation as well. The well pressure was 270 # at the time of my inspection and killing operations were commencing. We developed a plan of remediation while I was on site and I will continue to monitor the process as it progresses.
1415223910 2014-11-02 Drill / Deepen / Reopen No Violations Inspection revealed that drilling rig lost approximately 75 bbl of oil based drilling fluid after well unloaded fluid during fishing operation with wash over pipe. The driller estimated they have recovered approximately 35 bbl of fluid so far and it was noted that there was evidence that material left site as a mist and it had traveled approximately 100 south of the drill pad and I told company rep to remove all contaminated material from site and the county inspector would need run tickets from them stating where material was properly disposed of.
1415224954 2014-11-03 Drill / Deepen / Reopen No Violations Follow up inspection with county inspector Andrew Corder to go over clean up plan with operator and check on well control issues they have mixed 1000 bbl of 16#fluid and presently the pressure is 270 psi and they are mixing more fluid too attempt to kill well so they can go in to the well and retrieve lost wash over pipe .
1424938738 2014-10-19 Casing String Witnessed No Violations On the day of my inspection the 13.375 intermediate casing was ran and cemented. See casing ticket for details. No violations noted.
1525088983 2017-09-26 Production Wells No Violations This well is equipped with 5.5-inch diameter production casing. The well appears to be free flowing without any artificial lift technology present at this time. The well is piped to a gas processing unit and then to the production area. The production area contains four 400-barrel production fluid storage tank. The production records within the RBDMS system are current to 2017.
1770088206 2014-09-30 Drill / Deepen / Reopen No Violations On the day my inspection the surface hole was being drilled and casing will be set soon. No violations noted.
1798367905 2014-12-19 Drill / Deepen / Reopen No Violations The rig will attempt to retrieve the last section of drill pipe from the curve section of this hole. They will then circulate two bottoms up and set a 600 cement plug on top of the fish to 100 inside the 9.625 casing. Following a wait time of 24 hours the rig will dress off the top of the cement and rig up a directional motor to start the new curve and lateral. No violations noted
2143562587 2017-12-19 Production Wells No Violations This well is equipped with 5.5-inch diameter production casing. The well appears to be free flowing without any artificial lift technology present at this time. The well is piped to a gas processing unit and then to the production area. The production area contains four 400-barrel production fluid storage tank. The production records within the RBDMS system are current to 2017.
364034504 2016-3-14 0:00: PL No Violations 1.00
415856132 2014-11-4 0:00: DD No Violations 2.50
516866016 2014-8-6 0:00:0 CS No Violations 4.00
853072160 2014-12-17 0:00 DD No Violations 2.50
965597055 2018-6-19 0:00: PW No Violations 0.50

For data sources see[9]

References