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34-013-20587

Well Details

Well ID: 34-013-20587
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Country: United States
State: Ohio
County: Belmont
Municipality: Pultney Township
Operator Name: EQUITY OIL & GAS FUNDS INC
Well Pad ID:
Farm/Lease Name: GIFFIN D
License Status: Final Restoration
License Date: 2007-01-12
Spud Date: 2007-02-01
Spud Drilling Contractor: WARREN DRLG
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 40.030000
Longitude: -80.770000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2007-01-12 Proposed Formations:BEREA THRU ORISKANY, Issued Date:1/12/2007, Expired Date:1/12/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW
Construction Permit Expires 2008-01-12
Record Last Modified 2018-11-06

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1559403113 2007-2-4 0:00:0 DD No Violations
-46964772 2007-2-6 0:00:0 DD No Violations
-765468845 2007-2-21 0:00: PW No Violations
-992656808 2011-2-9 0:00:0 FR No Violations 0.50
0046964772 2007-02-06 Drill / Deepen / Reopen No Violations 7 PILLS OF MUD CIRCULATED. NO RETURNS TO SURFACE. RAN DOWNHOLE CAMERA.FLUID LEVEL AT 495 SAW SEVERAL PLACES WHERE WATER WAS COMING IN HOLE AT 366 AND AT 402. DECIDED TO REAM HOLE WITH 17.75 BIT TO 615 AND RUN 11.75 CONDUCTOR AND CEMENT IN HOLE. STARTING TO REAM HOLE.
0409395899 2007-02-01 Drill / Deepen / Reopen No Violations WARREN DRILLING. DRILLING SURFACE HOLE AT 300
0765468845 2007-02-21 Production Wells No Violations PIT MTD CLOSED LOCATION ROUGHED IN. TO FRAC WELL NEXT MONTH OR SOONER.
0992656808 2011-02-09 Final Restoration No Violations On day of inspection well was plugged due to lost surface hole per conversation withJohn Murphy. Mike Kavage let them use a cement mixer and grout off.Vegetation back 100%.Final Restoration passed.
1170289852 2007-01-31 Drill / Deepen / Reopen No Violations WARREN DRILLING. MOVE ON RIG UP
1170940673 2007-02-08 Drill / Deepen / Reopen No Violations WARREN DRILLING. REAMING HOLE WITH 14.75 BIT. STARTE TO RUN 11.75 PIPE 4 JOINTS IN RIG CONTROL BANK MALFUNCTIONED. FLEXED HOURS AT HOUSE FROM 3-8 P.M. FINISHED RUNNING 11.75 IN HOLE. UNIVERSAL CEMENT 525SX.IN HOLE BASKET SET AT 125. BALANCED PLUG ON BOTTOM 380
1559403113 2007-02-04 Drill / Deepen / Reopen No Violations WARREN DRILLING. STILL MIXING MUD AND PUMPING DOWNHOLE. NO CIRCULATION YET. 700BBLS. PUMPED AWAY DOWNHOLE.SHOULD HAVE HAD CIRCULATION AT 270 BBLS.
1700824460 2007-02-05 Drill / Deepen / Reopen No Violations WARREN DRILLING.STILL MIXING MUD AND PUMPING DOWNHOLE. FLUID LEVEL AT 360
409395899 2007-2-1 0:00:0 DD No Violations

For data sources see[3]

References