X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-013-20530

Well Details

Well ID: 34-013-20530
Loading map...
Country: United States
State: Ohio
County: Monroe
Municipality: Switzerland Township
Operator Name: KEROGEN RESOURCES
Well Pad ID:
Farm/Lease Name: CALDWELL CHAS
License Status: Producing
License Date: 1989-09-08
Spud Date: 1989-10-02
Spud Drilling Contractor: R WOLFE DRLG
Final Drill Date: 1989-10-04
Well Total Depth: 2325.00 ft
Configuration: Vertical
Latitude: 39.850000
Longitude: -80.950000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1988-06-22 Issued Date 6/22/88 Expired Date 6/22/89 Acres 0327280 Tool Type RTA Proposed Formation GORDON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1989-09-08 3054 KEROGEN RESOURCES GeoDate 9/8/89
Oil and Gas 1989-09-08 Issued Date 9/8/89 Expired Date 9/8/90 Acres 0327280 Tool Type RTA Proposed Formation GORDON Proposed Depth 02325 Proposed Drill Depth 02325
Original Spud 1989-10-02 RI 9-9-89
Completed 1989-10-04 RI 9-9-89
Reached Total Depth 1989-10-04 RI 9-9-89
CO 1989-11-01 1515 PETRO DRILLING CORP GeoDate 6/22/88
Completion Report Received 1989-11-16 RI 9-9-89
Construction Permit Expires 1990-09-08 RI 9-9-89
Record Last Modified 2017-02-15 RI 9-9-89

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2044 2060 0
2044 2060 0
2006-09-11 2045 2067 29
2045 2067 29
2044 2060 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 65 Qts 80000 N2 FOAM FRAC

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 KEROGEN RESOURCES 0.00 0.00 0
1990 KEROGEN RESOURCES 4085.00 0.00 363
1991 KEROGEN RESOURCES 1059.00 0.00 358
1992 KEROGEN RESOURCES 924.00 6.00 365
1993 KEROGEN RESOURCES 639.00 0.00 365
1994 KEROGEN RESOURCES 557.00 0.00 365
1995 KEROGEN RESOURCES 377.00 0.00 335
1996 KEROGEN RESOURCES 460.00 0.00 365
1997 KEROGEN RESOURCES 448.00 0.00 365
1998 KEROGEN RESOURCES 469.00 0.00 365
1999 KEROGEN RESOURCES 525.00 0.00 275
2000 KEROGEN RESOURCES 33.00 0.00 65
2001 KEROGEN RESOURCES 114.00 0.00 155
2002 KEROGEN RESOURCES 94.00 0.00 185
2003 KEROGEN RESOURCES 9.00 0.00 60
2004 KEROGEN RESOURCES 258.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 KEROGEN RESOURCES Brine 0 0
1990 KEROGEN RESOURCES Brine 16 363
1991 KEROGEN RESOURCES Brine 11 358
1992 KEROGEN RESOURCES Brine 10 365
1993 KEROGEN RESOURCES Brine 6 365
1994 KEROGEN RESOURCES Brine 6 365
1995 KEROGEN RESOURCES Brine 5 335
1996 KEROGEN RESOURCES Brine 5 365
1997 KEROGEN RESOURCES Brine 5 365
1998 KEROGEN RESOURCES Brine 5 365
1999 KEROGEN RESOURCES Brine 6 275
2000 KEROGEN RESOURCES Brine 3 65
2001 KEROGEN RESOURCES Brine 6 155
2002 KEROGEN RESOURCES Brine 5 185
2003 KEROGEN RESOURCES Brine 5 60
2004 KEROGEN RESOURCES Brine 6 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-102958043 2006-4-19 0:00: PW No Violations
-1186385815 2017-6-1 0:00:0 PW No Violations 1.00
-1340260283 2008-7-30 0:00: PW No Violations
-1401940209 2004-7-28 0:00: PW No Violations
-1455036828 2004-4-8 0:00:0 PW No Violations
-2036232062 2006-4-19 0:00: PW No Violations
0102958043 2006-04-19 Production Wells No Violations STATUS CHECK. NO PRODUCTION REPORTS SINCE 2004.
0223825313 2013-01-15 Production Wells No Violations I spoke with the owner and operator of this well Kim Cecil. He informed me that the well was being sold to Rice Energy and paperwork was being finalized. He also stated that his production records would be up to date very soon. All violations will be resolved at that time.
0496886760 2005-01-11 Production Wells No Violations STATUS CHECK
1186385815 2017-06-01 Production Wells No Violations A follow up inspection was conducted and well remains in the same condition as it was in the last inspection. The well is equipped with a pumping unit, tubing, and rods. The tank battery consisted of a 100 barrel production fluid holding tank, a brine storage tank, and a mechanical separator. Production records have still not been submitted since 2004.
1205931376 2008-03-18 Production Wells No Violations PRODUCING WELL
1340260283 2008-07-30 Production Wells No Violations NO PRODUCTION REPORTS SINCE YR. 2004. SHOULD BE BROUGHT TO MCCORMACS ATTENTION.
1401940209 2004-07-28 Production Wells No Violations STATUS CHECK, WELL APPEARS TO BE IN PRODUCTION
1455036828 2004-04-08 Production Wells No Violations STATUS CHECK
1470925231 2016-08-02 Production Wells No Violations An inspection was conducted as a follow up for the bonding and surety section. Landowner was not available on this day and the electric fencing with no gate found made access to the well unfeasible. Domestic production has not been confirmed at this time. A follow up inspection will ensue.
1663452297 2016-03-22 Production Wells Violations Noted Chiefs order # 2014-138 follow up inspection found the following equipment present at the well head-4.5 production casing-1.5 production tubing with a production tree on the tubing and pumping rods in the tubing with the production valves in the closed position and the well set up to be produced by the means of a pumping unit. The electric service is severed at the meter and a gas powered drive motor has been installed on the unit with no current signs of production at the well head. At the production area a single 100 barrel steel tank is present along with a 1,200 gallon plastic storage tank and a mechanical separator and a gas sales meter with no current sales chart present in the meter and no reported production shown to the Division in the State RBDMS database since 2004. Also noted is both production tanks are leaking fluid inside the dike and no identification is present. Instructions are as follows -The well owner/operator shall address the pollution and contamination at the production area by remediating the affected area and removing the fluid from the leaking production tank, post proper well identification within 30 days, also submit a written plugging schedule to (Bill Stolarik) at (5880 Memory Road Zanesville Ohio 43701) within 30 days, per OAC 1501:9-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
2003171171 2018-11-21 Production Wells No Violations Follow up inspection to Chief Orders # 2017-356 & 2014-138 along with violation # 1663452297. Upon inspection the well was observed to be equipped with 4.5 diameter production casing along with 1.900 production tubing with casing and tubing well heads present. Attached to the casing and tubing well head sections are 2 diameter flow lines with check and shut off valves installed in the 2 flow lines, the valves are in the closed position and conjoin into one 2 diameter sales line that is severed at ground level near the well head. The electrical service has been removed along with the electrical motor on the pumping unit. A gasoline engine has been installed on the pumping unit along with new valves and gauges on the service side of the casing and tubing well head sections. The production facility is located on the property next to the County Road and consists of a single 100 barrel steel tank along with a 2,100 gallon plastic tank along with a mechanical separator and gas sales meter. The valve on the separator is closed and the production flow line was reported previously to of been severed by a contractor when a house was built between the well head and tank battery by the landowner. The 2,100 gallon tank is 1/2 full with product and is leaking from a split in the side. There is also product on the ground below the 100 barrel steel tank 3 outlet valve that appears of been present for a period of time. The 100 barrel tank appeared empty. The last reported commercial production to the Division was in 2004.
2036232062 2006-04-19 Production Wells No Violations STATUS CHECK. NO PRODUCTION REPORTS SINCE 2004.
223825313 2013-1-15 0:00: PW No Violations 0.50
496886760 2005-1-11 0:00: PW No Violations
812173520 2020-2-4 0:00:0 PW No Violations 0.80

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1663452297 US-OH-116452 2016-03-24 Well operation causing pollution and contamination
1663452297 US-OH-116453 2016-03-24 Failure to legibly identify well
1663452297 US-OH-116454 2016-03-24 Well shall be plugged
1663452297 US-OH-116455 2016-03-24 Statement of annual production not filed

For data sources see[9]

References