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34-013-20506

Well Details

Well ID: 34-013-20506
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Country: United States
State: Ohio
County: Belmont
Municipality: York Township
Operator Name: KEROGEN RESOURCES
Well Pad ID:
Farm/Lease Name: CARPENTER RUSSELL
License Status: Producing
License Date: 1987-07-08
Spud Date: 1987-07-19
Spud Drilling Contractor: SWANK-ULLMAN
Final Drill Date: 1987-07-22
Well Total Depth: 2180.00 ft
Configuration: Vertical
Latitude: 39.870000
Longitude: -80.880000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1987-07-08 Issued Date 7/8/87 Expired Date 7/7/88 Acres 0020000 Tool Type RTA Proposed Formation GORDON Proposed Depth 02180 Proposed Drill Depth 02180
Original Spud 1987-07-19
Completed 1987-07-22
Reached Total Depth 1987-07-22
CO 1987-09-15 3054 KEROGEN RESOURCES GeoDate 7/8/87
Completion Report Received 1988-05-18
Construction Permit Expires 1988-07-07
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1983 2064 80
1985 2055 0
1997-06-29 1985 2055 0
1983 2064 80
1983 2064 80

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 99700 Gal 100000
ACID 15 600 Gal 0 FRAC: H2O,SAND,N2
N2 0 350 Mscf 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 PETRO DRILLING CORP 1118.00 17.00 105
1988 PETRO DRILLING CORP 6371.00 13.00 180
1989 PETRO DRILLING CORP 1998.00 22.00 150
1990 KEROGEN RESOURCES 1083.00 0.00 365
1991 KEROGEN RESOURCES 697.00 0.00 365
1992 KEROGEN RESOURCES 842.00 14.00 365
1993 KEROGEN RESOURCES 742.00 0.00 365
1994 KEROGEN RESOURCES 751.00 0.00 365
1995 KEROGEN RESOURCES 408.00 0.00 365
1996 KEROGEN RESOURCES 760.00 0.00 365
1997 KEROGEN RESOURCES 640.00 0.00 365
1998 KEROGEN RESOURCES 675.00 0.00 365
1999 KEROGEN RESOURCES 545.00 0.00 245
2000 KEROGEN RESOURCES 121.00 0.00 65
2001 KEROGEN RESOURCES 650.00 0.00 305
2002 KEROGEN RESOURCES 377.00 0.00 95
2003 KEROGEN RESOURCES 561.00 0.00 245
2004 KEROGEN RESOURCES 569.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 PETRO DRILLING CORP Brine 219 105
1988 PETRO DRILLING CORP Brine 253 180
1989 PETRO DRILLING CORP Brine 40 150
1990 KEROGEN RESOURCES Brine 11 365
1991 KEROGEN RESOURCES Brine 7 365
1992 KEROGEN RESOURCES Brine 8 365
1993 KEROGEN RESOURCES Brine 8 365
1994 KEROGEN RESOURCES Brine 8 365
1995 KEROGEN RESOURCES Brine 5 365
1996 KEROGEN RESOURCES Brine 8 365
1997 KEROGEN RESOURCES Brine 8 365
1998 KEROGEN RESOURCES Brine 11 365
1999 KEROGEN RESOURCES Brine 12 245
2000 KEROGEN RESOURCES Brine 11 65
2001 KEROGEN RESOURCES Brine 10 305
2002 KEROGEN RESOURCES Brine 10 95
2003 KEROGEN RESOURCES Brine 10 245
2004 KEROGEN RESOURCES Brine 11 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1173431353 2006-5-3 0:00:0 PW No Violations
-1478982654 2003-12-11 0:00 PW No Violations
-176027993 2018-11-16 0:00 PW No Violations 1.50
-1813418749 2017-5-31 0:00: PW No Violations 0.50
-1983691117 2010-6-22 0:00: PW No Violations 1.50
-1984118710 2008-11-19 0:00 PW No Violations
-386392560 2004-7-6 0:00:0 PW No Violations
-720640309 2016-4-20 0:00: PW No Violations 1.00
0011010729 2013-01-15 Production Wells No Violations I spoke with the owner and operator of this well Kim Cecil. He informed me that the well was being sold to Rice Energy and paperwork was being finalized. He also stated that his production records would be up to date very soon. All violations will be resolved at that time.
0130077772 2008-10-23 Production Wells No Violations WELL IS IN PRODUCTION. NO VIOLATIONS.
0174469517 2012-01-23 Production Wells Violations Noted On the day of my inspection the well was equipped with a pumping unit. The tank battery contents included one 110 barrel oil storage tank and one 50 barrel brine storage tank. Both of the tanks were rusted by the valves and had oil/brine deposits on the ground close by. The brine kill on the brine tank measured approximately 3 feet by 1.5 feet. The spill by the production tank measure approximately 1.5 feet by 1 foot. This well was capable of production, however no production report have been submitted since 2004. Photo documenting issues noted were taken on the day of my inspection.
0176027993 2018-11-16 Production Wells No Violations Follow up inspection to Orders # 2014-138 & 2017-356 and violation #-720640309. The landowner Tom Carpenter accompanied me on this day and the well was observed to be equipped with a 4.5 diameter production casing string along with a 1.900 diameter production tubing string. There is 2 diameter flow lines attached to the casing and tubing well heads with valves present in the closed position. There is a second 2 diameter line on the casing well head that is equipped with a valve that is also closed. The surface casing well head 2 outlet does not have a flow line or plug installed and is standing open. There is a polish rod liner and pumping rods inserted into the tubing well head but the pumping unit has been removed. The landowner indicated there was 2 production fluid storage areas present associated with the well and he had to have them removed and the areas restored due to the production tanks leaking, also at that time the pumping unit was removed. No domestic hook up is present. The registered owner Kerogen Resources has no Bond or Insurance in place with the Division. Photographs taken on this day.
0386392560 2004-07-06 Production Wells No Violations NO CHANGE IN STATUS OF WELL.NO PRODUCTION REPORTS SUBMITTED BY OPERATOR. REQUEST CHIEFS ORDER ON WELL.
0720640309 2016-04-20 Production Wells Violations Noted On the day of my inspection I was following up on Chiefs Order 2014-138. The status of the well appears to be the same. The well was equipped with a pumping unit, tubing, and rods. The tank battery consisted of a 100 barrel production fluid holding tank, a brine storage tank, and a mechanical separator. The valves at the tank battery were in the closed position. Production records have not been submitted since 2004 and the well is unable to produce in its current state. Photos were taken on the date of this inspection. The well owner/operator shall submit a written plugging schedule to Inspector Andrew Corder at 5880 Memory Road Zanesville, Ohio 43701 within 30 days, per OAC 1501:9-11-OS(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
11010729 2013-1-15 0:00: PW No Violations 0.50
1101953429 2004-12-15 Production Wells No Violations WELL IS IN PRODUCTION
1173431353 2006-05-03 Production Wells No Violations WELL INPRODUCTION
1197922380 2006-02-07 Production Wells No Violations STATUS CHECK. WELL PRODUCING.
1244924772 2005-05-12 Production Wells No Violations STATUS CHECK. WELL IN PRODUCTION
130077772 2008-10-23 0:00 PW No Violations
1478982654 2003-12-11 Production Wells No Violations STATUS CHECK
1526739586 2013-01-03 Production Wells No Violations Inspection due to previous NOV. Status of well has not changed. I attempted to call Mr. Cecil and the number listed in the system is disconnected. I will do more research to try and resolve this matter.
1580752786 2020-2-3 0:00:0 PW No Violations 1.50
1667640900 2004-06-29 Production Wells No Violations STATUS CHECK
174469517 2012-1-23 0:00: PW No Violations 0.50
1778124201 2016-06-24 Production Wells No Violations An inspection was conducted as a follow up for the bonding and surety section. According to the landowner, no one is currently receiving domestic gas from this well. The well status has changed from the previous inspection. The landowner has removed the tank battery area and reclaimed the area. All valves on the well are shut in.
1813418749 2017-05-31 Production Wells No Violations A follow up inspection was conducted and well remains in the same condition as it was in the last inspection. The landowner had removed all the tank battery contents and the pumping unit. The landowner has stated that he had this work done and the well has been shut in.
1983691117 2010-06-22 Production Wells No Violations On day of inspection well is supplied with pump jack and 8 5/8 casing,4.5cas,1.5tubing.There is a 100bbl tank and a 1550 plastic tank. Dike and id are in place. No production has been filed 2004.
1984118710 2008-11-19 Production Wells No Violations DIKE AREA WORKED OVER. WELL IS CAPABLE OF PRODUCTION.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0174469517 US-OH-117338 2014-04-10 Nonproduction; well shall be plugged or placed in temporary inactive status
0174469517 US-OH-117339 2014-04-10 Statement of annual production not filed
0720640309 US-OH-128194 2016-06-03 Well shall be plugged

For data sources see[9]

References