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34-013-20381

Well Details

Well ID: 34-013-20381
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Country: United States
State: Ohio
County: Belmont
Municipality: Somerset Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: JEFFERIS
License Status: Producing
License Date: 1990-06-07
Spud Date: 1981-06-10
Spud Drilling Contractor:
Final Drill Date: 1981-06-18
Well Total Depth: 2915.00 ft
Configuration: Vertical
Latitude: 39.900000
Longitude: -81.160000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1981-06-10
Completed 1981-06-18
Reached Total Depth 1981-06-18
CO 1981-07-02 1362 BW RESOURCES INC GeoDate 7/2/81
Oil and Gas 1981-07-02 Issued Date 7/2/81 Expired Date Acres 0020000 Tool Type RTA Proposed Formation GORDON Proposed Depth 00000 Proposed Drill Depth 00000
Completion Report Received 1982-01-07
CO 1983-09-21 1515 PETRO DRILLING CORP GeoDate 9/21/83
Unknown 1983-09-21 Issued Date 9/21/83 Expired Date 3/19/84 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
CO 1990-06-07 1515 PETRO DRILLING CORP GeoDate 6/7/90
Unknown 1990-06-07 Issued Date 6/7/90 Expired Date 6/7/91 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Construction Permit Expires 1991-06-07
CO 1993-05-05 952 G-R CONTRACTING INC GeoDate 6/7/90
Change of Owner 2006-05-22 Operator changed from 952, G-R CONTRACTING INC to 1634, NORTHWOOD ENERGY CORP
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1909 1919 11
1909 1919 11
1909 1919 11

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1065 Bbl 60000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2005 NORTHWOOD ENERGY CORP 0.00 0.00 0
2006 NORTHWOOD ENERGY CORP 0.00 0.00 0
2007 NORTHWOOD ENERGY CORP 0.00 0.00 0
2008 NORTHWOOD ENERGY CORP 0.00 0.00 0
2009 NORTHWOOD ENERGY CORP 0.00 0.00 0
2010 NORTHWOOD ENERGY CORP 0.00 0.00 0
2011 NORTHWOOD ENERGY CORP 0.00 0.00 0
2012 NORTHWOOD ENERGY CORP 275.00 0.00 366
2013 NORTHWOOD ENERGY CORP 187.00 0.00 365
2014 NORTHWOOD ENERGY CORP 100.00 0.00 365
2015 NORTHWOOD ENERGY CORP 52.00 0.00 365
2016 NORTHWOOD ENERGY CORP 49.00 0.00 365
2017 NORTHWOOD ENERGY CORP 0.00 0.00 0
2018 NORTHWOOD ENERGY CORP 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2005 NORTHWOOD ENERGY CORP Brine 0 0
2006 NORTHWOOD ENERGY CORP Brine 0 0
2007 NORTHWOOD ENERGY CORP Brine 0 0
2008 NORTHWOOD ENERGY CORP Brine 0 0
2009 NORTHWOOD ENERGY CORP Brine 0 0
2010 NORTHWOOD ENERGY CORP Brine 0 0
2011 NORTHWOOD ENERGY CORP Brine 20
2012 NORTHWOOD ENERGY CORP Brine 0 366
2013 NORTHWOOD ENERGY CORP Brine 26 365
2014 NORTHWOOD ENERGY CORP Brine 0 365
2015 NORTHWOOD ENERGY CORP Brine 0 365
2016 NORTHWOOD ENERGY CORP Brine 0 365
2017 NORTHWOOD ENERGY CORP Brine 0 0
2018 NORTHWOOD ENERGY CORP Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-769870956 2018-6-25 0:00: PW No Violations 0.50
0758888700 2006-01-23 Production Wells No Violations CAPABLE OF PRODUCING.
0769870956 2018-06-25 Production Wells No Violations On the day of my inspection I witnessed production equipment included a 100 barrel stock tank, vertical separator, and 2 inch diameter meter run with a .250 inch orifice plate that was disconnected. The mechanical dump valve on the separator had a slight leak. After testing standing water near separator the chlorides were at 72 parts per million. Production equipment is shared with 34013203810000. The well was equipped with 4.5 inch diameter production casing, 2.375 inch diameter upset tubing, with rods and an Alten pumping unit with natural gas motor, supply line for the natural gas motor was no longer hooked up. All valves were closed at the time of my inspection, and well appeared to be shut in. Identification tags were present but illegible and production was reported as zero for gas, oil, and brine for 2017. I contacted Mike Corp with Northwood and explained that the leak needs to be fixed and Identification tags need to be addressed. He informed me that they would remediate the problems right away. There will be a follow up inspection later in the week to make sure problems have been remediated.
1831996130 2017-07-24 Production Wells No Violations This well is equipped with 4.5-inch diameter production casing. It also has tubing and rods installed in the well. Attached to the rods was a pumping unit. The pumping unit had a motor on it that appeared to be powered by natural gas. The motor had belts that were attached from it to the pumping unit. The production area contained one 100 barrel production fluid holding tank and a vertical mechanical separator. Production records within the RBDMS system are current up to 2016.
758888700 2006-1-23 0:00: PW No Violations

For data sources see[9]

References