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34-009-23545

Well Details

Well ID: 34-009-23545
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Country: United States
State: Ohio
County: Athens
Municipality: Bern Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: WOGAN J
License Status: Producing
License Date: 2018-05-09
Spud Date: 1994-02-03
Spud Drilling Contractor: HIGHLAND DRLG
Final Drill Date: 1994-02-08
Well Total Depth: 5045.00 ft
Configuration: Vertical
Latitude: 39.440000
Longitude: -81.880000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1993-11-24 198 VIKING RESOURCES CORP GeoDate 11/24/93
Oil and Gas 1993-11-24 Issued Date 11/24/93 Expired Date 11/24/94 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05045 Proposed Drill Depth 05045
Original Spud 1994-02-03
Annular Disposal Well 1994-02-08
Completed 1994-02-08
Reached Total Depth 1994-02-08
Completion Report Received 1994-03-11
Change of Owner 1998-11-12 Operator changed from 198, VIKING RESOURCES CORP to 3793, ENERGY SEARCH INC
Revocation 1999-03-31
Last Compliance Report 2005-10-17
Change of Owner 2008-02-26 Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2018-05-09 Proposed Formations:MEDINA SAND, Issued Date:5/9/2018, Expired Date:5/8/2020 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2018-05-16
Construction Permit Expires 2020-05-08

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1998-01-09 4912 4918 2
4912 4918 2
4912 4918 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 48460 Gal 50000 FRAC W/48,460 GAL H20 & 50M# SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1994 VIKING RESOURCES LLC 34016.00 0.00 365
1995 VIKING RESOURCES LLC 35931.00 0.00 365
1996 VIKING RESOURCES LLC 29196.00 0.00 0
1997 VIKING RESOURCES LLC 14980.00 0.00 0
1998 VIKING RESOURCES LLC 3139.00 0.00 365
1999 ENERGY SEARCH INC 0.00 0.00 365
2000 ENERGY SEARCH INC 0.00 0.00 365
2008 EXCO - NORTH COAST ENERGY INC 0.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 1
2016 ENERVEST OPERATING LLC 0.00 0.00 0
2017 ENERVEST OPERATING LLC 0.00 0.00 0
2018 ENERVEST OPERATING LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1994 VIKING RESOURCES LLC Brine 2542 365
1995 VIKING RESOURCES LLC Brine 633 365
1996 VIKING RESOURCES LLC Brine 204 0
1997 VIKING RESOURCES LLC Brine 0
1998 VIKING RESOURCES LLC Brine 0 365
1999 ENERGY SEARCH INC Brine 0 365
2000 ENERGY SEARCH INC Brine 365
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0
2010 ENERVEST OPERATING LLC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 1
2016 ENERVEST OPERATING LLC Brine 0 0
2017 ENERVEST OPERATING LLC Brine 0 0
2018 ENERVEST OPERATING LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1087437835 2018-1-30 0:00: PW No Violations 1.00
-1319452902 2018-9-12 0:00: PW No Violations 0.80
-1528668751 2017-8-11 0:00: PW No Violations 1.50
-1554870470 2017-8-18 0:00: PW No Violations 2.00
-1888134611 2005-9-8 0:00:0 AD No Violations
-1895118757 2005-3-1 0:00:0 PW No Violations
-2075207265 2018-3-27 0:00: PW No Violations
-886618916 2020-4-10 0:00: PW No Violations 1.00
0000015651 Preliminary Restoration No Violations PASSED Y WITNESSED 11/22/94 INSPECTOR DAN GOINS DATE 11/2219/94 DATA FROM OLD VAX INFO
1087437835 2018-01-30 Production Wells No Violations Follow-up to inspection 1528668751 on 8/11/17. There were several violations cited in the report. The pollution and contamination has been addressed, the tank was removed so tank spacing and equipment pressure was addressed. The tank was removed and the dike was remediated so the failure to keep dike free and clear of contaminates was addressed. I still have received no plan to plug the well. The tubing was still behind the well and no flow lines were connected. The well is still in violation of 12b however the other violations are as of today cleared.
1115819277 Production Wells No Violations
1142804841 2004-01-21 Annular Disposal No Violations Well is not equipped for annular disposal.
1159238256 2017-08-11 Temporary Abandoned Annular Disposal No Violations Annular disposal is not in use. Well is not set up for annular disposal. Well is idle and incapable of production.
1319452902 2018-09-12 Production Wells No Violations I have received a plugging permit in the mail. I emailed Tim McConaha to ask what the plan was for this well. The well was found in the same state as last reported.
1350554162 2018-07-19 Production Wells No Violations I received the permit to plug the well a couple months back. The well is still not capable of production. The well is shut in with a bull plug and the valve is in the closed position. I called Tim McConoughey with Enervest and left a message. The well was originally written up for 12B.
1528668751 2017-08-11 Production Wells Violations Noted Inspection of this well revealed a swage nipple, valve reduced to 2 and a bull plug. A string on 1.5 inch tubing was laid out behind the well. The tank was correctly identified and was leaking. There were several 100 pound propane tanks laying around the dike. The dike was contaminated with an oily substance. The environmental contamination shall be properly remediated. The source of the contamination shall be dealt with in such a way as to prevent further contamination and releases. This well shall be plugged.
1554870470 2017-08-18 Production Wells No Violations Checked on status of cleanup. The dike was filled with rain water today. It did look as if someone had driven a four wheeler back to the location in the last week. It did not appear that clean up had begun.
15651 PL No Violations
1888134611 2005-09-08 Annular Disposal No Violations Well is not equipped for annular disposal.
1895118757 2005-03-01 Production Wells No Violations The well was found disconnected and incapable of production. The well was equipped with a 2 to 4 1/2 inch swage and valve. Apparently, a pump jack was removed from the well.
2075207265 2018-03-27 Production Wells No Violations Follow-up to inspection 1528668751 on 8/11/17. There were several violations cited in the report. The pollution and contamination has been addressed, the tank was removed so tank spacing and equipment pressure was addressed. The tank was removed and the dike was remediated so the failure to keep dike free and clear of contaminates was addressed. I still have received no plan to plug the well. The tubing was still behind the well and no flow lines were connected. The well is still in violation of 12b. I contacted the company and they said they would get started on the plugging permit paperwork.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1528668751 US-OH-114640 2017-08-21 9-1-07 Well operation causing pollution and contamination
1528668751 US-OH-114641 2017-08-21 9-9-05(A)2 Violation of tank spacing requirements
1528668751 US-OH-114642 2017-08-21 9-9-05(A)8 Equipment pressure rated below operating pressure
1528668751 US-OH-114643 2017-08-21 9-9-05(A)9 No SPCC dike/or failure to keep dike free of water or oil
1528668751 US-OH-114644 2017-08-21 NONE Well shall be plugged

For data sources see[9]

References