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34-007-22666

Well Details

Well ID: 34-007-22666
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: VIKING RESOURCES LLC
Well Pad ID:
Farm/Lease Name: HUEY UNIT
License Status: Not Drilled
License Date: 1984-03-15
Spud Date: 1984-06-16
Spud Drilling Contractor:
Final Drill Date: 1984-06-19
Well Total Depth: 2919.00 ft
Configuration: Vertical
Latitude: 41.900000
Longitude: -80.700000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-03-15 198 VIKING RESOURCES CORP GeoDate 3/15/84
Oil and Gas 1984-03-15 Issued Date 3/15/84 Expired Date 9/11/84 Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1984-06-16
Completed 1984-06-19
Reached Total Depth 1984-06-19
Construction Permit Expires 1984-09-11
Record Last Modified 2009-12-11

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2759 2839 14
2759 2839 14
2759 2839 14

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1352 Bbl 50000

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2133058445 2015-8-26 0:00: PW No Violations
1440610170 2015-08-24 Production Wells No Violations I was on location at the request of the well company. The 4.5 production casing has rusted through just above the 8 5/8 surface casing. There is a tubing packer set at an unknown depth in the well. The company has hired Autumn Ridge to bring in their service rig and perform the work. The company plans to repair the 4.5 and replace the wellhead with a new one. I will check back on 8/26/15 to see if the work has been completed.
2133058445 2015-08-26 Production Wells No Violations My inspection found the 4.5 production casing has been repaired and the company has installed a new wellhead. Circle M is on location repairing the domestic gas supply that is plumbed into the well. The company is going to replace the existing flow line with a new 2 coated steel flow line before turning the well back on.

For data sources see[5]

References