X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-007-22306

Well Details

Well ID: 34-007-22306
Loading map...
Country: United States
State: Ohio
County: Ashtabula
Municipality: New Lyme Township
Operator Name: C & D OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: LOVEY ANTHONY
License Status: Producing
License Date: 1983-08-10
Spud Date: 1983-09-15
Spud Drilling Contractor: PEP DRLG
Final Drill Date:
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 41.640000
Longitude: -80.760000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1983-08-10 3270 GROUP MAINTENANCE CORP GeoDate 8/10/83
Oil and Gas 1983-08-10 Issued Date 8/10/83 Expired Date 2/6/84 Acres 0028000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1983-09-15 PERMIT EXPIRED.
Construction Permit Expires 1984-02-06 PERMIT EXPIRED.
Change of Owner 2004-12-03 Operator changed from 3270, GROUP MAINTENANCE CORP to 5952, BELVOIR ENERGY INC.
Last Compliance Report 2015-03-30 PERMIT EXPIRED.
Change of Owner 2018-02-12 Operator changed from 5952, BELVOIR ENERGY INC. to 10067, C & D OIL & GAS LLC
Record Last Modified 2018-02-12 PERMIT EXPIRED.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1988 GROUP MAINTENANCE CORP 1394.00 98.00 365
1989 GROUP MAINTENANCE CORP 1656.00 87.00 365
1990 GROUP MAINTENANCE CORP 190.00 91.00 365
1991 GROUP MAINTENANCE CORP 1073.00 0.00 365
1992 GROUP MAINTENANCE CORP 1193.00 97.00 365
1994 GROUP MAINTENANCE CORP 712.00 0.00 360
1996 GROUP MAINTENANCE CORP 1785.00 0.00 330
1997 GROUP MAINTENANCE CORP 983.00 0.00 360
2006 GROUP MAINTENANCE CORP 619.00 0.00 365
2007 BELVOIR ENERGY INC. 463.00 43.00 365
2010 BELVOIR ENERGY INC. 265.00 0.00 365
2012 BELVOIR ENERGY INC. 233.00 0.00 366
2013 BELVOIR ENERGY INC. 430.00 82.00 365
2014 BELVOIR ENERGY INC. 495.00 27.00 365
2016 BELVOIR ENERGY INC. 0.00 0.00 365
2017 BELVOIR ENERGY INC. 0.00 0.00 365
2018 C & D OIL & GAS LLC 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1988 GROUP MAINTENANCE CORP Brine 66 365
1989 GROUP MAINTENANCE CORP Brine 130 365
1990 GROUP MAINTENANCE CORP Brine 130 365
1991 GROUP MAINTENANCE CORP Brine 243 365
1992 GROUP MAINTENANCE CORP Brine 95 365
1994 GROUP MAINTENANCE CORP Brine 149 360
1996 GROUP MAINTENANCE CORP Brine 197 330
1997 GROUP MAINTENANCE CORP Brine 0 360
2006 GROUP MAINTENANCE CORP Brine 33 365
2007 BELVOIR ENERGY INC. Brine 0 365
2010 BELVOIR ENERGY INC. Brine 0 365
2012 BELVOIR ENERGY INC. Brine 63 366
2013 BELVOIR ENERGY INC. Brine 41 365
2014 BELVOIR ENERGY INC. Brine 40 365
2016 BELVOIR ENERGY INC. Brine 0 365
2017 BELVOIR ENERGY INC. Brine 0 365
2018 C & D OIL & GAS LLC Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1915217114 2015-1-21 0:00: AD No Violations
-249546178 2015-5-26 0:00: PW No Violations
-274541650 2018-8-6 0:00:0 PW No Violations
0249546178 2015-05-26 Production Wells No Violations My inspection of this well found no compliance issues.
0274541650 2018-08-06 Production Wells No Violations At the time of this inspection, the well was equipped with a plunger lift assembly and the gate valve on the tubing was closed. The 2 inch flow line off of the tubing was closed. The tank battery consisted of one 210 BBL tank, one 50 BBL steel tank and a mechanical separator. Valves on the separator were closed. The tank battery was diked and had legible signage. Lease access was stable.
0484589249 2006-04-18 Production Wells No Violations no violations .
0608606167 2010-03-19 Annular Disposal No Violations no annular disposal .
0828623309 2003-12-17 Annular Disposal No Violations No annular disposal .
1106092000 2004-05-25 Production Wells No Violations Case# 04-003 , Larry Scholten . Inspection showed no gas leak . Follow-up / on site for approx. 45 min.s when well turned on causing a gas leak from seperator to sales line . I contacted Greg Harris , he arrived in approx. 20 min.s , he then shut-in we
1915217114 2015-01-21 Annular Disposal No Violations My inspection of this well found there is no annular disposal use at this well.
484589249 2006-4-18 0:00: PW No Violations
608606167 2010-3-19 0:00: AD No Violations
828623309 2003-12-17 0:00 AD No Violations

For data sources see[7]

References