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Well ID: 34-007-21673 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashtabula | |
Municipality: Colebrook Township | |
Operator Name: BIG SKY ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: PERRY H | |
License Status: Active Injection | |
License Date: 1981-08-19 | |
Spud Date: 1981-03-06 | |
Spud Drilling Contractor: PEP DRLG | |
Final Drill Date: 1981-03-11 | |
Well Total Depth: 3860.00 ft | |
Configuration: Vertical | |
Latitude: 41.570000 | |
Longitude: -80.770000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1981-03-06 | CONVERT TO SWDW |
Completed | 1981-03-11 | CONVERT TO SWDW |
Reached Total Depth | 1981-03-11 | CONVERT TO SWDW |
Completion Report Received | 1981-06-22 | CONVERT TO SWDW |
CO | 1981-08-13 | 277 ATWOOD ENERGY INC GeoDate 8/13/81 |
Unknown | 1981-08-13 | Issued Date 8/13/81 Expired Date 8/13/82 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000 |
Conversion to Injector | 1981-08-19 | |
Plugged Back | 1981-08-19 | CONVERT TO SWDW |
First Injection | 1981-10-01 | CONVERT TO SWDW |
Construction Permit Expires | 1982-08-13 | CONVERT TO SWDW |
Annulus Pressure Monitoring Approved | 1991-05-02 | CONVERT TO SWDW |
CO | 1995-08-07 | 4205 TRANSFUEL RESOURCES CO GeoDate 8/13/81 |
CO | 1995-10-27 | 213 LOMAK OPERATING CO GeoDate 8/13/81 |
CO | 1996-09-13 | 4930 CANTON OIL & GAS COMPANY GeoDate 8/13/81 |
Change of Owner | 2004-07-14 | Operator changed from 4930, CANTON OIL & GAS COMPANY to 7666, ARVILLA OILFIELD SERVICES LLC |
Change of Owner | 2005-07-27 | Operator changed from 7666, ARVILLA OILFIELD SERVICES LLC to 1333, BIG SKY ENERGY INC |
Last Compliance Report | 2014-07-31 | CONVERT TO SWDW |
Record Last Modified | 2017-02-15 | CONVERT TO SWDW |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-04-27 | 3390 | 3418 | 2 |
2000-04-27 | 3658 | 3730 | 1 |
3390 | 3418 | 2 | |
3658 | 3730 | 1 | |
3390 | 3418 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 1000 Gal | 0 | |||
H2O | 0 | 82068 Gal | 60000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | ATWOOD ENERGY INC | 0.00 | 0.00 | 365 |
1988 | ATWOOD ENERGY INC | 0.00 | 0.00 | 365 |
1989 | ATWOOD ENERGY INC | 0.00 | 0.00 | 365 |
1990 | ATWOOD ENERGY INC | 0.00 | 0.00 | 365 |
1991 | ATWOOD ENERGY INC | 0.00 | 0.00 | 365 |
1992 | ATWOOD RESOURCES INC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | ATWOOD ENERGY INC | Brine | 1870 | 365 |
1988 | ATWOOD ENERGY INC | Brine | 1015 | 365 |
1989 | ATWOOD ENERGY INC | Brine | 620 | 365 |
1990 | ATWOOD ENERGY INC | Brine | 910 | 365 |
1991 | ATWOOD ENERGY INC | Brine | 415 | 365 |
1992 | ATWOOD RESOURCES INC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1044448876 | 2013-9-24 0:00: | SW | No Violations | |
-1082495966 | 2011-6-7 0:00:0 | SW | No Violations | |
-1090288849 | 2020-1-15 0:00: | SW | No Violations | 1.00 |
-1138986535 | 2020-3-3 0:00:0 | SW | No Violations | 1.20 |
-1147166741 | 2006-7-13 0:00: | SW | No Violations | |
-1175463793 | 2018-2-16 0:00: | SW | No Violations | |
-1177949407 | 2019-2-11 0:00: | SW | No Violations | |
-1226043144 | 2006-3-9 0:00:0 | SW | No Violations | |
-1305466377 | 2006-12-6 0:00: | SW | No Violations | |
-1306139932 | 2010-8-16 0:00: | SW | No Violations | |
-1346306909 | 2012-2-24 0:00: | SW | No Violations | |
-1371970122 | 2017-9-12 0:00: | SW | No Violations | |
-1497882048 | 2019-4-29 0:00: | SW | No Violations | |
-1523628507 | 2010-8-5 0:00:0 | SW | No Violations | |
-1530752211 | 2013-8-7 0:00:0 | SW | No Violations | |
-1544311648 | 2003-3-28 0:00: | SW | No Violations | |
-1568124325 | 2011-9-22 0:00: | SW | No Violations | |
-1581033009 | 2018-11-19 0:00 | SW | No Violations | 1.00 |
-1621831252 | 2015-10-7 0:00: | SW | No Violations | |
-1662707990 | 2004-8-27 0:00: | SW | No Violations | |
-1688828412 | 2006-7-7 0:00:0 | SW | No Violations | |
-1776093633 | 2003-8-26 0:00: | SW | No Violations | |
-179221887 | 2010-8-9 0:00:0 | SW | No Violations | |
-1815117813 | 2019-8-8 0:00:0 | SW | No Violations | 1.00 |
-1816264697 | 2005-8-10 0:00: | SW | No Violations | |
-1879316166 | 2005-1-28 0:00: | SW | No Violations | |
-1884515009 | 2007-6-19 0:00: | SW | No Violations | |
-1904920627 | 2009-10-15 0:00 | SW | No Violations | |
-1908657593 | 2018-2-27 0:00: | SW | No Violations | 0.70 |
-1920551655 | 2008-12-9 0:00: | SW | No Violations | |
-1949412315 | 2010-1-26 0:00: | SW | No Violations | |
-1971409939 | 2014-2-25 0:00: | SW | No Violations | |
-236818114 | 2006-5-18 0:00: | SW | No Violations | |
-248533971 | 2009-3-25 0:00: | SW | No Violations | |
-283978563 | 2005-5-9 0:00:0 | SW | No Violations | |
-306145749 | 2013-10-18 0:00 | SW | No Violations | |
-320925670 | 2016-3-18 0:00: | SW | No Violations | |
-396217935 | 2020-4-23 0:00: | SW | No Violations | |
-449026714 | 2018-10-26 0:00 | SW | No Violations | 0.50 |
-451816085 | 2019-9-11 0:00: | SW | No Violations | |
-453931456 | 2007-9-4 0:00:0 | SW | No Violations | |
-597653662 | 2006-9-22 0:00: | SW | No Violations | |
-628340354 | 2019-1-2 0:00:0 | SW | No Violations | 1.00 |
-664642191 | 2010-9-14 0:00: | SW | No Violations | |
-736505289 | 2018-5-3 0:00:0 | SW | No Violations | |
-872939254 | 2012-12-7 0:00: | SW | No Violations | |
-910138782 | 2007-3-8 0:00:0 | SW | No Violations | |
-923296357 | 2008-3-18 0:00: | SW | No Violations | |
-941938367 | 2014-5-9 0:00:0 | SW | No Violations | |
-964344009 | 2018-5-15 0:00: | SW | No Violations | 1.00 |
-997564728 | 2003-7-11 0:00: | SW | No Violations | |
0000UIC875 | 1990-04-12 | Salt Water Injection Well | No Violations | 1501:9-3-05 (6) CONSTRUCTION & CONVE |
000UIC1007 | 1990-11-28 | Salt Water Injection Well | No Violations | 1509.22 A 1.2 C-STORAGE & DISPOSAL |
000UIC1008 | 1990-11-28 | Salt Water Injection Well | No Violations | 1501.9-3-04 |
000UIC1163 | 1991-09-18 | Salt Water Injection Well | No Violations | 1501: 9-3-07 (E)&(F) QUARTERLY REPORTS |
000UIC1310 | 1992-10-01 | Salt Water Injection Well | No Violations | 1509.03 RULES & REGULATIONS |
000UIC1311 | 1992-10-01 | Salt Water Injection Well | No Violations | 1501: 9-3-04 PREVENT CONTAMINAT. |
000UIC1312 | 1992-10-01 | Salt Water Injection Well | No Violations | 1501: 9-3-05 (B) (7) STORAGE FACILITIES |
001250i215 | 2002-04-23 | Salt Water Injection Well | No Violations | Check U.I.C. facility. |
001250i277 | 2002-09-25 | Salt Water Injection Well | No Violations | Inspection per request by Curtis Hill [ local resident ] . Inspection showed well pressures are within allowable limits. Conversation with Don Gooseman[field supervisor] by telephone he advised me they had recently replaced the injection line from pump house to wellhead. I then advised him a pressure test is required of new injection line. He scheduled a test for Friday [9-27-02]. |
001250i283 | 2002-09-27 | Salt Water Injection Well | No Violations | On site to pressure test injection line. Pressure injection line to 1100 P.S.I. And shut-in for 15 minutes with 0 P.S.I. Loss. Pressure test passed. |
0033033749 | 2015-03-05 | Salt Water Injection Well | No Violations | My inspection of the storage facility and the well pressures found no compliance issues. I was unable to get a pressure reading of the tubing annulus due to a frozen valve. |
0036016920 | 2013-04-26 | Salt Water Injection Well | No Violations | Inspection of injection well pressures and storage facility found no violations , |
0058326702 | 2010-08-10 | Salt Water Injection Well | No Violations | Company pumping fluid through tubing and circulating to surface with Duplex mud pump in a attempt release packer with no success . |
0124322948 | 2011-02-23 | Salt Water Injection Well | No Violations | check uic facility. |
0125260645 | 2018-06-11 | Salt Water Injection Well | No Violations | I found no evidence of recent activity. There are several inches of standing water inside the diked tank battery. The equipment in the green shed has a corroded appearance. I was unable to gauge the annulus due to fittings need replaced. Overgrown vegetation surrounds the entire facility. An identification sign is posted. |
0179221887 | 2010-08-09 | Salt Water Injection Well | No Violations | Company still trying to release packer with no success . |
0236818114 | 2006-05-18 | Salt Water Injection Well | No Violations | check uic facility . |
0248533971 | 2009-03-25 | Salt Water Injection Well | No Violations | check uic facility . |
0249319227 | 2016-11-07 | Salt Water Injection Well | No Violations | Inspection of this well found there has been no action to remediate the contamination issues at and around the storage facility. There was one foot of fluid inside the storage impoundment area. The buried sump tanks for the unloading pad and the pump house were full to point of overflowing. This well was not in operation at the time of my inspection. |
0283978563 | 2005-05-09 | Salt Water Injection Well | No Violations | no violations . |
0306145749 | 2013-10-18 | Salt Water Injection Well | No Violations | Inspection found the underground tanks for the pump house and the unloading pad have been emptied . There is about 8 of fluid inside the impoundment walls around the storage tanks . There has been no action to clean-up oil stained gravel and soil or to clean the fresh oil from pump house floor . I spoke with Bob Barr Jr. and he told me they are repairing their high pressure steam cleaner to complete the remedial work . He gave me no certain time frame for completion of the remedial work . |
0320925670 | 2016-03-18 | Salt Water Injection Well | No Violations | I was accompanied by Jen Barret, Dan Martin, Mike Williams [ Attorney Generals Office ], Rick Anderson and Tom Hill [ ODNR Division of Oil & Gas ]. I took photos of the areas inside the impoundments for the storage tanks and the sump pump on the north side of the pump house. |
0338937131 | 2016-12-08 | Salt Water Injection Well | No Violations | Myself and Tom Hill inspected the storage facility to find the company has not performed any remediation to resolve the compliance issues with this well. Tom took photos of the storage facility and the buried collection tanks for the unloading pad and the pump house. |
0376250163 | 2014-11-26 | Salt Water Injection Well | No Violations | My inspection of the well pressures and the storage facility found no compliance issues. |
0449026714 | 2018-10-26 | Salt Water Injection Well | No Violations | I found no evidence of recent activity. There has been no remediation started. There are several inches of water in the diked tank battery. The side of the dike is oil stained. The pump house garage door is open and the equipment inside has a corroded appearance. There injection well has a rusty appearance. There is overgrown vegetation around the facility and well. A slightly faded identification sign is posted. Photos were taken and are available upon request. |
0453931456 | 2007-09-04 | Salt Water Injection Well | No Violations | check uic facility . |
0464796672 | 2011-11-16 | Salt Water Injection Well | No Violations | Status check of underground injection facility. |
0477451005 | 2015-05-28 | Salt Water Injection Well | No Violations | Myself, Tom Hill and Rick Anderson inspected the site. There has been no remedial work performed. |
0519389591 | 2003-11-07 | Preliminary Restoration | No Violations | Check U.I.C. facility . |
0547927144 | 2012-09-20 | Salt Water Injection Well | No Violations | My inspection of injection well pressures and the storage facility found no violations . |
0567464977 | 2006-07-18 | Salt Water Injection Well | No Violations | Company building dike around pumphouse . |
0597653662 | 2006-09-22 | Salt Water Injection Well | No Violations | check uic facility . |
0628340354 | 2019-01-02 | Salt Water Injection Well | No Violations | |
0664642191 | 2010-09-14 | Salt Water Injection Well | No Violations | Company attempting to fish seperated tubing from well with no success . |
0684767765 | 2004-10-28 | Salt Water Injection Well | No Violations | Check U.I.C. facility . |
0704045293 | 2017-02-17 | Salt Water Injection Well | No Violations | Myself, Tom Hill, Rick Anderson, Terry Whitehair and Gene Park with ODNR Division of Oil & Gas met with Bob Barr Sr., Charles Mosio and Gino Pulito with Big Sky Energy on site to discuss the required remedial work needed to comply with the compliance issues with this well. |
0736505289 | 2018-05-03 | Salt Water Injection Well | Violations Noted | Our records indicate that the Division has not received the 2017 Salt Water Injection Well Annual Report (Form 204) that was due to the Division by April 15, 2018. Please submit the requested report by June 4, 2018. Report received, 5/12/2018 |
0872939254 | 2012-12-07 | Salt Water Injection Well | No Violations | My inspection of injection well pressures and storage facility found no violations . |
0910138782 | 2007-03-08 | Salt Water Injection Well | No Violations | CHECK UIC FACILITY |
0912417490 | 2017-02-28 | Salt Water Injection Well | No Violations | Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd, & 4th quarters of 2016. Please submit the appropriate reports by March 14, 2017Reports received 3/15/2017 |
0923296357 | 2008-03-18 | Salt Water Injection Well | No Violations | no violations . |
0941938367 | 2014-05-09 | Salt Water Injection Well | No Violations | My inspection found there has been no further action to comply with the compliance notice issued on 8-7-2013 . The deadline was on 9-27-2013 . The well was not in operation at this time . |
0948207629 | 2008-06-13 | Salt Water Injection Well | No Violations | check uic facility . |
0964109548 | 2010-04-21 | Salt Water Injection Well | No Violations | CHECK UIC FACILITY |
0964344009 | 2018-05-15 | Salt Water Injection Well | No Violations | I inspected this well location as part of an evaluation of open compliance violations. As such, the following deficiencies had previously been noted: release of oilfield fluids (oil and brine) from the storage tanks, into the impoundment, and the fluid unloading areas requiring remediation. At the time of this inspection, I noted the following: the facility was inactive and in a state of disrepair, with a small pump house structure, a multi-tank battery with a receiving dock station, and a single well that had been utilized as a brine disposal injection location. The tank battery system was comprised of four 210-barrel steel tanks and one 100-barrel steel tank within a common, earthen, plastic-lined impoundment structure that formed a secondary containment system. The secondary containment was filled with several inches of rusty water and oily sludge, with oily staining on the sidewalls. The piping system and tanks were extensively corroded with numerous perforations. The tanks were full to within 2 feet of the top, with fluid. The unloading dock and associated collection sump was full of oily sludge. The pump house shed contained a sump collection system and associated pumping apparatus. The sump was full to grade with oily water, and the interior of the shed was coated with oily staining. Adjacent to the shed was an approximate ten thousand gallon portable steel storage tank, the contents of which were not ascertainable. 150 feet east of the impoundment and shed was the wellhead, in an open field. The wellhead was comprised of a 4.5-inch casing with 1-inch flexible flow-line fittings and connections. There was an approximate 15 by 15 earthen pad with shallow berm surrounding the well. There was no visible active leaking fluids or gas from any portions of the system. There was no evidence that any actions had been taken to remedy or mitigate the impacted areas. |
0997564728 | 2003-07-11 | Salt Water Injection Well | No Violations | Check U.I.C. facility . |
1044448876 | 2013-09-24 | Salt Water Injection Well | No Violations | The statis of any remedial work to comply with the compliance notice has not changed since my inspection on 9-11-2013 . No remedial action at all . |
1081633549 | 2004-04-06 | Salt Water Injection Well | No Violations | Check UIC facility . |
1082495966 | 2011-06-07 | Salt Water Injection Well | No Violations | no violations . |
1085297020 | 2013-07-15 | Salt Water Injection Well | No Violations | Inspection of injection well pressures and storage facility found no violations . |
1088338902 | 2015-12-02 | Production Wells | No Violations | I conducted an inspection of this well and found that the emptied 300 BBL frac tank was still on site and had not been removed. There was excessive fluid in the sump tanks and in the storage facility area. Stained soil around the sump tanks was also observed at the time of this inspection. |
1117584484 | 2005-04-05 | Salt Water Injection Well | No Violations | Complaintant ; Curtis Hill . Inspection of injection well showed no violations . Myself and suprv. Cheslock talked with Mr. Hill per complaint [ contaminated water well ] , we asked him to acquire water samples from his water well to dertermine if contamination was related to oil & gas well . He advised us he did not want us to collect any samples from his well . Mr. Hill told us even if we took a sample and it tested no contamination he still would not drink the water because he had it tested in 1985 and at that time the person testing the well told him the water could be safe to drink one day but the contaminate could reapear days later , not making it safe to drink . Myself and suprv. Cheslock left site without collecting a water sample . |
1147166741 | 2006-07-13 | Salt Water Injection Well | No Violations | Check oil spill clean-up progress . Some clean-up still needed . |
1152287950 | 2006-07-05 | Salt Water Injection Well | Violations Noted | Arrived on site to find a oil spill from pump house flowing west 100 to road culvert at route 46 , through culvert to west side of road into storm ditch . Oil then flowed approximately 350 into low area , then spread out approximately 50 to 75 wide in very thick grass . After oil spread out it traveled approximately 100 then stopped . Bob Barr with Big Sky Energy advised me they lost approximately 10-20 barrel of oil and 60 barrel of brine from facility . I contacted EPA and advised them of spill . Jim Urwin with EPA arrived on site and inspected spill . NOTE: Company was already cleaning oil spill up .I collected water sample from three homes north and south of spill . House numbers 6419,6375 and 6353 . Samples were taken to lab for analysis . |
1153668682 | 2006-07-21 | Salt Water Injection Well | No Violations | Remedial work has been completed . No violations . RESOLVED . |
1162055440 | 2008-09-24 | Salt Water Injection Well | No Violations | check uic facility . |
1175463793 | 2018-02-16 | Salt Water Injection Well | Violations Noted | Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd, & 4th quarter of 2017 . Please submit the appropriate reports by March 17, 2018. REPORTS RECEIVED BY THE DIVISION FEBRUARY 26, 2018 |
1177949407 | 2019-02-11 | Salt Water Injection Well | Violations Noted | The Division has not received the 1st, 2nd, 3rd, & 4th quarter brine disposal fees for 2018. Please forward disposal fees and sheets to the Division by 3/12/2019. |
1185403714 | 2006-08-09 | Salt Water Injection Well | No Violations | On site to collect soil samples in oil spill area . After collection of soil samples , a field test of dilluted samples with 1176 quantab showed 0 chlorides . A lab test is not required at this time . |
1189255003 | 2014-08-29 | Salt Water Injection Well | No Violations | Inspection of the well pressures and the storage facility found no violations. |
1226043144 | 2006-03-09 | Salt Water Injection Well | No Violations | Case# 06-005 , Curtis Hill . Inspection showed no visible violations . While on site a brine truck from Petrowater unloaded brine causing a loud screeching noise . Conf. With brine hauler revealed the unloading valve was insufficient causing him to by-pa |
124322948 | 2011-2-23 0:00: | SW | No Violations | |
1250i215 | 2002-4-23 0:00: | SW | No Violations | 0.50 |
1250i277 | 2002-9-25 0:00: | SW | No Violations | 0.70 |
1250i283 | 2002-9-27 0:00: | SW | No Violations | 3.50 |
125260645 | 2018-6-11 0:00: | SW | No Violations | 0.50 |
1282532533 | 2015-12-31 | Salt Water Injection Well | No Violations | My inspection of this well found the well was not in operation, the excessive fluid in the sump tanks and the fluid in the containment area for the storage tanks has not been removed. |
1285863038 | 2010-08-02 | Salt Water Injection Well | No Violations | Company is blowing down well to pull tubing and packer . |
1288519977 | 2009-06-26 | Salt Water Injection Well | No Violations | check uic facility . |
1305466377 | 2006-12-06 | Salt Water Injection Well | No Violations | Check UIC facility . |
1306139932 | 2010-08-16 | Salt Water Injection Well | No Violations | Company still attempting to release packer . Rig pulled 93 thousand lbs on tubing when it seperated approx. 300 down hole . |
1333885140 | 2015-05-06 | Salt Water Injection Well | No Violations | My inspection of the well pressures no compliance issues. I found there was fluid inside the impoundment one and a half feet deep. The underground tanks for the unloading pad and the pump house were full of fluid to the point of running over. I contacted Don Goosman and told him of the excessive fluid in the impoundment and the underground tanks. He told me he would have them emptied within a few days. |
1339685128 | 2012-06-14 | Salt Water Injection Well | No Violations | My inspection of injection well pressures and the storage facility found no violations. |
1346306909 | 2012-02-24 | Salt Water Injection Well | No Violations | check uic facility . |
1350431454 | 2010-09-15 | Salt Water Injection Well | No Violations | Company run impression tool to determine statis of seperated tubing . |
1371970122 | 2017-09-12 | Salt Water Injection Well | No Violations | At the time of my inspection the operator had isolated the storage tanks by closing the valves at the bottom of the tanks. No action has been taken to remove free brine and oil from the containment. Scalding along the north side of the tank battery was evident (barren areas in the agricultural field and dead vegetation.) Sump behind the pump house was still full of fluid. The pump motor remained in disrepair. The sumps at the west end of the unloading pad remained full. |
1393430856 | 2014-02-25 | Salt Water Injection Well | No Violations | |
1413226684 | 2014-07-31 | Salt Water Injection Well | No Violations | Myself and supervisor Hill were on site to witness mechanical integrity test on annulus of production casing. Company pressured the annulus of the production casing to 1100 psi and then shut-in the annulus and held the pressure for 15 minutes with no drop in the pressure. The test passed. After further inspection of the remedial work required by the compliance notice issued on 8-7-2014. The remedial wok has been completed. The compliance notice has been resolved. |
1414422365 | 2004-05-07 | Salt Water Injection Well | No Violations | Check U.I.C. facility . |
1434458220 | 2015-05-27 | Salt Water Injection Well | No Violations | My inspection found the excessive fluid in the buried tanks and the facility has not been removed. |
1446939867 | 2010-08-06 | Salt Water Injection Well | No Violations | Company still unable to release packer. |
1451370259 | 2019-6-13 0:00: | SW | No Violations | 1.00 |
1497882048 | 2019-04-29 | Salt Water Injection Well | Violations Noted | Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on April 15th for 2018, Please submit the Form 204 to the Division by 5/29/2019. |
1506520065 | 2017-09-27 | Salt Water Injection Well | No Violations | |
1509564265 | 2017-11-01 | Salt Water Injection Well | No Violations | I inspected this well location as part of on-going enforcement proceedings. As such, the following deficiencies had been noted: release of oilfield fluids (oil and brine) from the storage tanks, into the impoundment, and the fluid unloading areas requiring remediation. At the time of this inspection, I noted the following: the facility appeared to have been inactive for an extended amount of time. The There was a tank battery system comprised of four 210-barrel steel tanks and one 100-barrel steel tank within a common, earthen, plastic-lined impoundment structure that formed a secondary containment system. The tanks were full to within 2 feet of the top, with fluid. The secondary containment was partially filled with water and substantial oily sheen and rust, and extensive oily staining along the sidewalls. There was an unloading dock with subsurface tanks for fluid collection which were full to ground surface with oily water. Adjacent to the tank impoundment was a small pump house shed with sump collection system and associated pumping apparatus. The sump was full to grade with oily water, and the interior of the shed was coated with oily staining. I tested the ponded water within the impoundment and found the pH to be 6-7, and the chloride level to be less than 400 ppm. Adjacent to the shed was an approximate ten thousand gallon portable steel storage tank, the contents of which were not ascertainable. 150 feet east of the impoundment and shed was the wellhead, in an open field. The wellhead was comprised of a 4.5-inch casing with 1-inch flexible flow-line fittings and connections. The flow-line valves were open. There was an approximate 15 by 15 earthen pad with shallow berm surrounding the well. The bermed area was full of water which I tested and found to be pH 6-7, and less than 400 ppm chlorides. There was no visible active leaking fluids or gas from any portions of the system. There was no evidence that any actions had been taken to remedy or mitigate the |
1509718505 | 2017-11-03 | Salt Water Injection Well | No Violations
-up line connecting the storage tanks is under water and has a rusty/corroded appearance. The unloading pad is surrounded by overgrown vegetation and has standing water. An identification sign is posted on the walkway along the storage tanks. Photos have been taken and are available upon request. | |
1521818587 | 2018-03-23 | Salt Water Injection Well | No Violations | I found no change from the previous inspection. Big Sky Energy has not begun any remediation. There is no evidence of recent activity. The injection well is not in operation. I was unable to gauge the annulus due to corroded fitting. The storage tanks are still surrounded by several inches of standing water with old oil residue. Photos were taken and available upon request. |
1523628507 | 2010-08-05 | Salt Water Injection Well | No Violations | Company pumping fresh water through tubing and circulating to surface in a attempt to release packer . They were still unable to release packer . |
1530752211 | 2013-08-07 | Salt Water Injection Well | Violations Noted | Inspection of the storage facility I found a fresh oil stained area 10 X 3 located between the pump house and the impoundment area . Further inspection I found the fluid level inside the dike walls was 2 deep , also the underground sump tank for the unloading pad was full of fluid to the point of overflowing . The underground sump tank for the pump house located on the north side of the pump house was full of fluid to the point of overflowing . Inspection of the interior of the pump house I found fresh oil lying over the entire area of the pump house floor . There was a new electric motor installed to run the injection pump but it had no belts installed to operate the injection pump . The well was not in operation at the time of my inspection . REMEDIAL WORK REQUIRED TO RESOLVE THE COMPLIANCE NOTICE : REMOVE ALL THE OIL STAINED MATERIAL AND DISPOSE OF IN AN APPROVED MANNER , REMOVE ALL THE EXCESSIVE FLUIDS FROM THE IMPOUNDMENT AREA AND THE UNDERGROUND TANKS FOR THE UNLOADING PAD AND THE PUMP HOUSE , CLEAN ALL THE FREE OIL FROM THE PUMP HOUSE FLOOR . NOTE: I contacted Bob Barr Jr. and told him of the compliance notice and the remedial action needed to resolve the compliance notice . |
1544311648 | 2003-03-28 | Salt Water Injection Well | No Violations | Check U.I.C. facility. |
1555681811 | 2019-04-19 | Salt Water Injection Well | No Violations | |
1568124325 | 2011-09-22 | Salt Water Injection Well | No Violations | Status check of underground injection facility. |
1572437128 | 2007-12-27 | Salt Water Injection Well | No Violations | check uic facility . |
1576157943 | 2019-12-11 0:00 | SW | No Violations | 4.00 |
1577191662 | 2019-12-23 0:00 | SW | No Violations | 8.00 |
1581033009 | 2018-11-19 | Salt Water Injection Well | No Violations | I found no evidence of recent activity. The facility equipment and injection well are highly corroded and rusty in appearance. The garage door on the pump house is open. There are several inches of water in the diked tank battery and around the injection well. A partially faded identification sign is posted. |
1588783729 | 2020-5-6 0:00:0 | SW | No Violations | |
1596639800 | 2020-8-5 0:00:0 | SW | No Violations | 1.10 |
1597928583 | 2020-8-20 0:00: | SW | No Violations | |
1601021558 | 2003-05-30 | Salt Water Injection Well | No Violations | Check U.I.C. facility . |
1621831252 | 2015-10-07 | Salt Water Injection Well | No Violations | Inspection of this well found the well is not in operation at this time. The sump tanks for the pump house and the unloading pad are full of fluid to the point of overflowing. There was 1.5 feet of fluid inside the storage facility impoundment for the storage tanks. |
1662707990 | 2004-08-27 | Salt Water Injection Well | No Violations | Check UIC facility . |
1674930927 | 2006-07-06 | Salt Water Injection Well | No Violations | On site for oil spill clean-up . |
1679810575 | 2005-11-18 | Salt Water Injection Well | No Violations | Check U.I.C. facility . |
1688828412 | 2006-07-07 | Salt Water Injection Well | No Violations | On site for oil spill clean-up . |
1714747071 | 2013-09-11 | Salt Water Injection Well | No Violations | Inspection found there is over a foot of water inside the impoundment around the storage tanks and the underground tanks for the pump house and the unloading pad are still full of fluid to the point of overflowing . There has been no action from the company to clean-up the fresh oil lying over the pump house floor or to remove oil saturated gravel and soil on west side of pump house . |
1738689943 | 2016-06-22 | Salt Water Injection Well | No Violations | My inspection found the sump tanks for the pump house and the unloading pad were full of fluid to point of overflowing. There was 4-6 inches of fluid inside the storage impoundment for the brine storage tanks. This well was not in operation at the time of my inspection. |
1753780672 | 2003-09-17 | Salt Water Injection Well | No Violations | Check U.I.C. facility per request from Curtis Hill . |
1753925101 | 2015-07-21 | Salt Water Injection Well | No Violations | My inspection found the leaking 300 bbl frac tank has been emptied. There is still excessive fluid in the sump tanks and in the storage facility. |
1765786079 | 2018-07-18 | Salt Water Injection Well | No Violations | I found no evidence that Big Sky Energy has performed any remediation or clean-up operations. The ball valve on the tubing at the injection well is in the open position. The fittings on the annulus are corroded. There is crystalized salt on the wellhead. Overgrown vegetation surrounds the facility. There are several inches of water in the diked tank battery with oil residue. A faded identification sign is posted. The equipment inside of the pump house has a corroded appearance. Photos were taken and are available upon request. |
1776093633 | 2003-08-26 | Salt Water Injection Well | No Violations | Check U.I.C. facility . |
178325877 | 2020-1-3 0:00:0 | SW | No Violations | |
1816264697 | 2005-08-10 | Salt Water Injection Well | No Violations | Check uic facility . |
1879316166 | 2005-01-28 | Salt Water Injection Well | No Violations | check uic facility . |
1884515009 | 2007-06-19 | Salt Water Injection Well | No Violations | CHECK UIC FACILITY . |
1904920627 | 2009-10-15 | Salt Water Injection Well | No Violations | check uic facility . |
1908657593 | 2018-02-27 | Salt Water Injection Well | No Violations | |
1920551655 | 2008-12-09 | Salt Water Injection Well | No Violations | check uic facility . |
1949412315 | 2010-01-26 | Salt Water Injection Well | No Violations | no violations . |
1961004348 | 2013-08-28 | Salt Water Injection Well | No Violations | Inspection found there has been no remedial work done to comply with the compliance notice issued on 8-07-2013 . NOTE: There is one foot of fluid inside dike walls , also the underground sump tanks for the pump house and the unloading pad are full of fluid to point of overflowing . |
1971409939 | 2014-02-25 | Salt Water Injection Well | No Violations | I checked this well for remedial work in accordance with the compliance notice issued on 8-7-2013 and to determine if the company is in compliance with the chiefs order #2014-43 . Upon my inspection I found there is still oil saturated soil and gravel on the west side of the pump house and the pump house floor is still covered with wet oil . The injection pump motor has been installed and the injection line is hooked-up to the injection pump . There was not a pressure release switch installed on the pressure side of the injection pump . The injection pump was not operating at the time of my inspection . Upon further inspection of the well pressures I found the tubing had 400 psi and the annulus had 490 psi . There has been 0 psi on the tubing and the annulus for the last 3 inspections dating back to 7-15-2013 . There is a indication that a mechanical integrity test should be performed before any further injection of fluid is done . I will address the integrity test and the pressure release switch when the chiefs order # 2014-43 is resolved . |
2006787765 | 2006-07-11 | Salt Water Injection Well | No Violations | On site for oil spill clean-up . |
2086502563 | 2010-08-04 | Salt Water Injection Well | No Violations | Company attemting to release packer with no success . |
2116064473 | 2015-06-02 | Salt Water Injection Well | No Violations | I was on site to assist Kyle Tharp in collecting water samples. The company has not removed the excessive fluid from the storage facility. |
249319227 | 2016-11-7 0:00: | SW | No Violations | |
33033749 | 2015-3-5 0:00:0 | SW | No Violations | |
338937131 | 2016-12-8 0:00: | SW | No Violations | |
36016920 | 2013-4-26 0:00: | SW | No Violations | |
376250163 | 2014-11-26 0:00 | SW | No Violations | |
464796672 | 2011-11-16 0:00 | SW | No Violations | |
477451005 | 2015-5-28 0:00: | SW | No Violations | |
519389591 | 2003-11-7 0:00: | PL | No Violations | |
547927144 | 2012-9-20 0:00: | SW | No Violations | |
567464977 | 2006-7-18 0:00: | SW | No Violations | |
58326702 | 2010-8-10 0:00: | SW | No Violations | |
627558330 | 2020-3-5 0:00:0 | SW | No Violations | |
684767765 | 2004-10-28 0:00 | SW | No Violations | |
704045293 | 2017-2-17 0:00: | SW | No Violations | |
912417490 | 2017-2-28 0:00: | SW | No Violations | |
948207629 | 2008-6-13 0:00: | SW | No Violations | |
964109548 | 2010-4-21 0:00: | SW | No Violations | |
UIC1007 | 1990-11-28 0:00 | SW | No Violations | |
UIC1008 | 1990-11-28 0:00 | SW | No Violations | |
UIC1163 | 1991-9-18 0:00: | SW | No Violations | |
UIC1310 | 1992-10-1 0:00: | SW | No Violations | |
UIC1311 | 1992-10-1 0:00: | SW | No Violations | |
UIC1312 | 1992-10-1 0:00: | SW | No Violations | |
UIC875 | 1990-4-12 0:00: | SW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0736505289 | US-OH-128370 | 2018-07-17 | 9-3-04B | Failure to file salt water injection annual report |
1152287950 | US-OH-103961 | 2006-07-07 | Pollution/Contamination | |
1175463793 | US-OH-104651 | 2018-03-21 | NONE | Failure to report disposal fees |
1177949407 | US-OH-104729 | 2019-04-08 | NONE | Failure to report disposal fees |
1497882048 | US-OH-114043 | 2019-06-06 | 9-3-04B | Failure to file salt water injection annual report |
1530752211 | US-OH-114688 | 2013-09-19 | Pollution/Contamination |
For data sources see[9]