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34-007-21579

Well Details

Well ID: 34-007-21579
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Country: United States
State: Ohio
County: Ashtabula
Municipality: Hartsgrove Township
Operator Name: BIG SKY ENERGY INC
Well Pad ID:
Farm/Lease Name: BOYCE DK
License Status: Producing
License Date: 1980-12-31
Spud Date: 1981-02-18
Spud Drilling Contractor:
Final Drill Date: 1981-02-24
Well Total Depth: 3678.00 ft
Configuration: Vertical
Latitude: 41.630000
Longitude: -80.940000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-12-31 300 PETROLEUM ENERGY PROD COR GeoDate 12/31/80
Oil and Gas 1980-12-31 Issued Date 12/31/80 Expired Date Acres 0031200 Tool Type RTF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1981-02-18 LOG TYPE- LASSER LOG
Completed 1981-02-24 LOG TYPE- LASSER LOG
Reached Total Depth 1981-02-24 LOG TYPE- LASSER LOG
Completion Report Received 1981-04-29 LOG TYPE- LASSER LOG
CO 1991-10-09 201 GREEN GAS CO GeoDate 12/31/80
CO 1992-04-07 1453 GREEN ENERGY INC GeoDate 12/31/80
Change of Owner 2001-02-06 Operator changed from 1453, GREEN ENERGY INC to 1333, BARR ROBT/dba BIG SKY PET
Record Last Modified 2013-10-03 LOG TYPE- LASSER LOG

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 GREEN ENERGY INC 844.00 0.00 165
1994 GREEN ENERGY INC 771.00 0.00 365
1995 GREEN ENERGY INC 522.00 0.00 365
1996 GREEN ENERGY INC 739.00 31.00 365
1997 GREEN ENERGY INC 424.00 0.00 365
1998 GREEN ENERGY INC 560.00 0.00 245
1999 GREEN ENERGY INC 424.00 0.00 242
2000 GREEN ENERGY INC 751.00 0.00 365
2001 BIG SKY ENERGY INC 897.00 0.00 365
2002 BIG SKY ENERGY INC 24.00 0.00 365
2003 BIG SKY ENERGY INC 5.00 0.00 365
2004 BIG SKY ENERGY INC 1067.00 0.00 365
2005 BIG SKY ENERGY INC 545.00 20.00 365
2006 BIG SKY ENERGY INC 650.00 0.00 365
2007 BIG SKY ENERGY INC 195.00 0.00 365
2008 BIG SKY ENERGY INC 60.00 0.00 365
2009 BIG SKY ENERGY INC 281.00 0.00 365
2010 BIG SKY ENERGY INC 281.00 0.00 365
2011 BIG SKY ENERGY INC 1410.00 0.00 365
2012 BIG SKY ENERGY INC 1529.00 0.00 366
2013 BIG SKY ENERGY INC 225.00 18.00 280
2014 BIG SKY ENERGY INC 116.00 8.00 365
2016 BIG SKY ENERGY INC 0.00 0.00 0
2017 BIG SKY ENERGY INC 0.00 0.00 0

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 GREEN ENERGY INC Brine 1462 165
1994 GREEN ENERGY INC Brine 193 365
1995 GREEN ENERGY INC Brine 567 365
1996 GREEN ENERGY INC Brine 273 365
1997 GREEN ENERGY INC Brine 76 365
1998 GREEN ENERGY INC Brine 282 245
1999 GREEN ENERGY INC Brine 50 242
2000 GREEN ENERGY INC Brine 343 365
2001 BIG SKY ENERGY INC Brine 0 365
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 365
2004 BIG SKY ENERGY INC Brine 0 365
2005 BIG SKY ENERGY INC Brine 0 365
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 365
2008 BIG SKY ENERGY INC Brine 0 365
2009 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0 365
2011 BIG SKY ENERGY INC Brine 0 365
2012 BIG SKY ENERGY INC Brine 0 366
2013 BIG SKY ENERGY INC Brine 0 280
2014 BIG SKY ENERGY INC Brine 0 365
2016 BIG SKY ENERGY INC Brine 0 0
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-899386314 2018-3-6 0:00:0 PW No Violations
0039094647 2016-05-03 Production Wells Violations Noted My inspection found the tank battery was equipped with one separator. There was a 210 barrel steel tank outside the earthen dike area on the east side. The tank was not connected to anything. There was no identification posted at the tank battery location. There was a oil saturated area at the base of the tank in an area 1.5 x 4 on the south side of the tank. I took one photo of the oil saturated area by the tank. There was a steel tank ladder lying on the ground outside the tank battery area on the south side. While traveling to the well location I observed a plastic flow line on the surface in several areas. The well was equipped with a pumping unit. There was a gas leak from a pressure release valve on the line supplying gas to the pump-jack motor. The valves from the well to the flow line were closed. This well was not in production at the time of my inspection. REQUIRED REMEDIAL WORK: Remove the oil saturated soil from the base of the tank, post identification at the tank battery location for this well, bury the flow line from the tank battery area to the well location and repair the gas leak at the well.
0599243902 2016-12-27 Production Wells No Violations My inspection of this well found there has been no remedial work done to resolve the compliance issues with this well.
0899386314 2018-03-06 Production Wells No Violations I conducted a compliance notice follow-up inspection for compliance notice 39094647. At the time of this inspection, the well was equipped with a pumpjack and the annulus and flow line valves were closed. No leak was observed at the well location. There was a 210 BBL production tank, a mechanical separator, and sales line on site at the tank battery. The 210 BBL tank was outside of the diked battery and disconnected from the other production equipment. The oil impacted area at the base of the 210 BBL tank has not been cleaned up. The flow line from the well to the tank battery location was still above ground and no signage has been added at the well or tank battery location.
0900193444 2005-11-18 Production Wells No Violations Remedial completed . No violations , RESOLVED .
0905902941 2005-11-09 Production Wells Violations Noted Complaintant - Beth Sacerich . Inspection showed a very small gas leak from tubing head packing .
1474304230 2016-09-13 Production Wells No Violations My inspection of this well found the oil saturated area at the base of the production tank has not been removed. Identification has not been posted at the tank battery location. The flow line from the tank battery to the well has not been buried. There was still gas leaking from the supply line to the pump jack motor.
39094647 2016-5-3 0:00:0 PW No Violations
599243902 2016-12-27 0:00 PW No Violations
900193444 2005-11-18 0:00 PW No Violations
905902941 2005-11-9 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0039094647 US-OH-124153 2016-09-14 Failure to properly bury pipeline
0039094647 US-OH-124154 2016-09-14 Well operation causing pollution and contamination
0039094647 US-OH-124155 2016-09-14 Well insufficiently equipped to prevent escape of oil and gas
0039094647 US-OH-124156 2016-09-14 Failure to legibly identify well
0905902941 US-OH-130339 2005-12-11 Well insufficiently equipped to prevent escape of oil and gas

For data sources see[7]

References