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34-007-20841

Well Details

Well ID: 34-007-20841
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Country: United States
State: Ohio
County: Ashtabula
Municipality: Morgan Township
Operator Name: MFC DRILLING INC
Well Pad ID:
Farm/Lease Name: MULDER
License Status: Final Restoration
License Date: 2017-03-29
Spud Date: 1977-07-07
Spud Drilling Contractor:
Final Drill Date: 1977-07-25
Well Total Depth: 3338.00 ft
Configuration: Vertical
Latitude: 41.700000
Longitude: -80.850000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-06-29 4508 FOUR CITY PRODUCING GeoDate 6/29/77
Original Spud 1977-07-07
Completed 1977-07-25
Reached Total Depth 1977-07-25
CO 1993-07-14 12 TUSSELL CLARENCE JR GeoDate 6/29/77
Change of Owner 1998-11-12 Operator changed from 12, TUSSELL CLARENCE JR to 3059, MFC DRILLING INC
APP 2017-03-29 Proposed Formations:CLINTON, Issued Date:3/29/2017, Expired Date:3/29/2019 12:00:00 PM, Drilling unit acres:60, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-06-14
Record Last Modified 2017-10-20
Construction Permit Expires 2019-03-29

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3164 3214 25
3164 3214 25
3164 3214 25

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 108000 Gal 49000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1998 MFC DRILLING INC 0.00 0.00 365
1999 MFC DRILLING INC 2094.00 52.00 365
2000 MFC DRILLING INC 1319.00 89.00 365
2001 MFC DRILLING INC 1746.00 0.00 365
2002 MFC DRILLING INC 858.00 60.00 365
2003 MFC DRILLING INC 609.00 64.00 365
2004 MFC DRILLING INC 6.00 0.00 365
2005 MFC DRILLING INC 0.00 53.00 365
2006 MFC DRILLING INC 1337.00 0.00 365
2007 MFC DRILLING INC 1414.00 24.00 365
2008 MFC DRILLING INC 1278.00 0.00 365
2009 MFC DRILLING INC 1905.00 70.00 365
2010 MFC DRILLING INC 2180.00 0.00 365
2011 MFC DRILLING INC 750.00 0.00 365
2012 MFC DRILLING INC 398.00 45.00 366
2013 MFC DRILLING INC 954.00 0.00 365
2014 MFC DRILLING INC 730.00 53.00 365
2015 MFC DRILLING INC 1087.00 45.00 365
2016 MFC DRILLING INC 324.00 0.00 365
2017 MFC DRILLING INC 200.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1998 MFC DRILLING INC Brine 148 365
1999 MFC DRILLING INC Brine 643 365
2000 MFC DRILLING INC Brine 270 365
2001 MFC DRILLING INC Brine 413 365
2002 MFC DRILLING INC Brine 223 365
2003 MFC DRILLING INC Brine 349 365
2004 MFC DRILLING INC Brine 100 365
2005 MFC DRILLING INC Brine 306 365
2006 MFC DRILLING INC Brine 325 365
2007 MFC DRILLING INC Brine 194 365
2008 MFC DRILLING INC Brine 314 365
2009 MFC DRILLING INC Brine 410 365
2010 MFC DRILLING INC Brine 278 365
2011 MFC DRILLING INC Brine 190 365
2012 MFC DRILLING INC Brine 285 366
2013 MFC DRILLING INC Brine 218 365
2014 MFC DRILLING INC Brine 75 365
2015 MFC DRILLING INC Brine 278 365
2016 MFC DRILLING INC Brine 237 365
2017 MFC DRILLING INC Brine 297 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1405176159 2019-11-29 0:00 FR No Violations
-1979165370 2017-6-14 0:00: PB No Violations 7.30
0570028665 2017-06-13 Plug / Plug Back No Violations I was on location to witness plug and abandon operations at this Clinton Sandstone well. MFC Drilling (MFC) was on location with their service rig, Nicks Well Plugging (NWP) was the cement contractor, and Petrowater (UIC#52) was supplying brine and freshwater for operations. Jimmy Orr (MFC) suspects there is a hole in the 4.5 production casing due to the high fluid level (800) inside the casing. The Clinton plug was set through 1.5 (ID) tubing and the tubing was pulled. There is gas pressure in the annulus between the 8.625 casing and 4.5 casing and was blown down prior to ripping the 4.5 casing. MFC ripped the 4.5 casing at a depth of 1973 and pulled the casing from the hole. 62 Joints of 9.5lb/ft., Range-2 casing was recovered from the hole. I had Petrowater load the hole with brine before leaving location. The wellhead was packed in and operations were shut down for the day. No violations. See plugging report for more details on this job.
1979165370 2017-06-14 Plug / Plug Back No Violations I was on location to witness plug and abandon operations at this Clinton Sandstone well. MFC Drilling (MFC) was on location with their service rig, Nicks Well Plugging (NWP) was the cement contractor, and Petrowater (UIC#52) was supplying brine and freshwater for operations. The 1.5 tubing was spotted at a depth of 1920 and a 300 plug was spotted to isolate the top of the Big Lime. 45 joints of tubing were pulled to a depth of 400 and cement was mixed and pumped until good returns were achieved at the surface. The remainder of the tubing was pulled and the hole was topped off. The top of the plug will be checked tomorrow prior to cutting off the 8.625 casing and attaching the ID plate. No violations. See plugging report for more details on this job.
1997091653 2006-02-28 Production Wells No Violations no violations .
2146304884 2008-08-06 Production Wells No Violations no violations .
570028665 2017-6-13 0:00: PB No Violations 10.20

For data sources see[9]

References