X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-005-23601

Well Details

Well ID: 34-005-23601
Loading map...
Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: SMALLEY ELLEN
License Status: Active Injection
License Date: 1983-06-07
Spud Date: 1983-06-20
Spud Drilling Contractor: WALTZ BROS DRLG
Final Drill Date: 1983-06-22
Well Total Depth: 718.00 ft
Configuration: Vertical
Latitude: 40.880000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Enhanced Recovery 1983-06-07 Issued Date 6/7/83 Expired Date 12/4/83 Acres 0081510 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00718 Proposed Drill Depth 00718
Original Spud 1983-06-20 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
Completed 1983-06-22 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
Reached Total Depth 1983-06-22 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
CO 1983-10-07 133 QUAKER STATE OIL REF CORP GeoDate 6/7/83
First Injection 1983-10-07 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
Completion Report Received 1983-10-19 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
Construction Permit Expires 1983-12-04 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
Annulus Pressure Monitoring Approved 1994-10-13 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 6/7/83
Last Compliance Report 1999-12-16 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15 LAST INJECTION IN 1998 CHG IN TOOL 6-18-83 PERMIT EXPIRED.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-23 598 662 0
598 662 0
598 662 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 108 Qts 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1065194201 2017-1-9 0:00:0 ER No Violations
-1108021305 2008-2-20 0:00: ER No Violations 0.50
-1143315354 2018-1-8 0:00:0 ER No Violations
-1147436128 2009-4-23 0:00: ER No Violations 0.50
-1280596676 2004-4-22 0:00: ER No Violations
-1329781778 2017-7-13 0:00: ER No Violations
-1410217102 2019-7-2 0:00:0 ER No Violations
-1441805501 2005-11-29 0:00 ER No Violations 0.50
-1508340346 2017-4-13 0:00: ER No Violations
-1510854277 2016-7-8 0:00:0 ER No Violations
-1551496399 2007-10-26 0:00 ER No Violations 0.50
-1555793123 2015-5-20 0:00: ER No Violations
-1716055686 2014-5-6 0:00:0 ER No Violations
-1742028763 2007-4-3 0:00:0 ER No Violations 0.50
-2061390353 2011-2-1 0:00:0 ER No Violations 1.00
-2099654859 2017-11-14 0:00 ER No Violations
-21267004 2011-10-17 0:00 ER No Violations
-222250617 2016-1-5 0:00:0 ER No Violations
-292204169 2006-4-13 0:00: ER No Violations 0.50
-299118057 2008-11-26 0:00 ER No Violations 0.50
-299343543 2018-5-1 0:00:0 ER No Violations
-328860660 2013-3-4 0:00:0 ER No Violations
-419743991 2018-10-10 0:00 ER No Violations
-518762959 2016-4-19 0:00: ER No Violations
-564435075 2016-11-2 0:00: ER No Violations
-671047079 2006-12-13 0:00 ER No Violations 0.50
-696318318 2012-11-27 0:00 ER No Violations
-758772465 2014-10-29 0:00 ER No Violations
0016498865 2018-08-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0021267004 2011-10-17 Enhanced Recovery Project No Violations Inspect well.
0222250617 2016-01-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0292204169 2006-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap and 1 tubing on a packer used for injection.
0299118057 2008-11-26 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures equal. Reset packer and test.
0299343543 2018-05-01 Enhanced Recovery Project No Violations Inspect well with operator to preform monthly pressure test of the annulus on the well.
0328860660 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0401873504 2003-08-14 Enhanced Recovery Project No Violations
0419743991 2018-10-10 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0456522508 2011-07-12 Enhanced Recovery Project No Violations inspect well.
0518762959 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0564435075 2016-11-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0654773820 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head has a slight leak.
0671047079 2006-12-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0696318318 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Injector line has slow leak at nipple.
0758772465 2014-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0830675422 2018-04-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0833564665 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
0885235978 2011-04-12 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1033430420 2013-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pump shut down during inspection. A line leak had occurred near the well head and appears to have plugged itself. Operator will excavate line and make appropriate repairs.
1065194201 2017-01-09 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1108021305 2008-02-20 Enhanced Recovery Project No Violations Annulus and injection pressure test.
1138919076 2010-03-30 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1143315354 2018-01-08 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1147436128 2009-04-23 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1214647425 2005-04-27 Enhanced Recovery Project No Violations Injection well test.
1228250584 2008-12-02 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1235914788 2012-05-24 Enhanced Recovery Project No Violations Inspect Well.
1280596676 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test.
1308300743 2009-10-20 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1329781778 2017-07-13 Enhanced Recovery Project Violations Noted Upon arrival at location the operator located leak with the flexible injection line. The supply trunk line was shut off and a replacement flexible injection flow line was installed at the well head. The operator determined less than 42 gallons of water was released and incident notification was not required. The well was put back into operation. The well was inspected for integrity and pressure. 1501:9-5-06 Prevention of contamination and pollution.

All persons engaged in any phase of enhanced recovery operations shall conduct such operations in a manner which will not contaminate the surface of the land, or water on the surface or in the subsurface.

1335462194 2012-02-27 Enhanced Recovery Project No Violations Inspect Well.
1409055532 2020-7-8 0:00:0 ER No Violations
1434966692 2019-4-11 0:00: ER No Violations
1441805501 2005-11-29 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1455629763 2016-02-12 Work Over Reconditioning No Violations In January 19, 2011 a total of 20 joints of PVC lined tubing were installed in the well at a depth of 500 feet with a Larkin packer set in compression. During the October 30, 2015 inspection of the well the tubing was observed to be deteriorated above the well head and the PVC line was visible. In February of 2016 the operator rigged up the service rig on the well and pulled the Larkin packer up-hole, 16 inches, without releasing the packer. The deteriorated tubing was cut off and the remaining tubing was threaded and the well head reconstructed. The packer is set at 498.6 feet. The well was loaded with fresh water and corrosion inhibitor and pressure tested by the operator. At the time the MIT was conducted the annulus pressure was at 305 psi. The operator was requested to pressure up the annulus above 350 psi. The annulus was pressured up to 395 psi and the pressure monitored for a period of 15 minutes with zero loss in pressure. The well passed the Mechanical Integrity test. The operator was notified that the well can be put into production.
1508340346 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1510854277 2016-07-08 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1551496399 2007-10-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1555793123 2015-05-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The annulus riser nipple is corroded.
1610858382 2020-4-21 0:00: ER No Violations
1629990026 2010-11-26 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures are equal at 320 psi. Reset packer and test.
16498865 2018-8-13 0:00: ER No Violations
1714546829 2020-1-23 0:00: ER No Violations
1716055686 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1742028763 2007-04-03 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1893402429 2013-04-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test.
1992859859 2012-09-20 Enhanced Recovery Project No Violations Inspect Well. Site ok.
2044688293 2015-03-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2048839956 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2061390353 2011-02-01 Enhanced Recovery Project No Violations Injection and annulus pressure test. Replaced packer. Pumped up annulus at 415 psi. 10 psi decline in 15 minutes. Topped off annulus between 2 3/8 tubing and surface casing with 35 sacks Class A cement.120 - 0, 1-17-2011.
2072778746 2019-1-10 0:00: ER No Violations
2083189440 2015-10-30 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in poor condition. The operator was notified the tubing has a slow leak.
2099654859 2017-11-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
401873504 2003-8-14 0:00: ER No Violations
456522508 2011-7-12 0:00: ER No Violations
654773820 2014-7-17 0:00: ER No Violations
681653235 2019-11-18 0:00 ER No Violations
830675422 2018-4-27 0:00: ER No Violations
833564665 2004-11-18 0:00 ER No Violations
885235978 2011-4-12 0:00: ER No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0299118057 US-OH-123111 2008-11-26 Failure to conduct or pass mech. integrity test
1329781778 US-OH-109434 2017-08-18 9-5-06 Pollution/Contamination
1629990026 US-OH-116020 2010-11-26 Failure to conduct or pass mech. integrity test

For data sources see[5]

References