X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-005-23059

Well Details

Well ID: 34-005-23059
Loading map...
Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: AUSTIN CLARK & THELMA
License Status: Active Injection
License Date: 1976-02-05
Spud Date: 1976-03-23
Spud Drilling Contractor: SHORTS DRLG
Final Drill Date: 1976-04-19
Well Total Depth: 682.00 ft
Configuration: Vertical
Latitude: 40.890000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-02-05 133 QUAKER STATE OIL REF CORP GeoDate 2/5/76
Enhanced Recovery 1976-02-05 Issued Date 2/5/76 Expired Date Acres 0000000 Tool Type RTAF Proposed Formation BEDFORD Proposed Depth Proposed Drill Depth
Original Spud 1976-03-23 RE-ISSUE 4-23-75, R.I. -S.REC. 2-11-76
Completed 1976-04-19 RE-ISSUE 4-23-75, R.I. -S.REC. 2-11-76
Reached Total Depth 1976-04-19 RE-ISSUE 4-23-75, R.I. -S.REC. 2-11-76
Completion Report Received 1977-03-31 RE-ISSUE 4-23-75, R.I. -S.REC. 2-11-76
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 2/5/76
Annulus Pressure Monitoring Approved 1999-03-03 RE-ISSUE 4-23-75, R.I. -S.REC. 2-11-76
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Last Compliance Report 2011-02-09 RE-ISSUE 4-23-75, R.I. -S.REC. 2-11-76
Record Last Modified 2017-02-15 RE-ISSUE 4-23-75, R.I. -S.REC. 2-11-76

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-22 578 622 0
578 622 0
578 622 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 88 Qts 0
Not Treated 0 88 Qts 0 WHT. WTR. TAMP.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC 0.00 61.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1087356809 2011-4-14 0:00: ER No Violations 1.00
-1116149005 2017-5-31 0:00: WR No Violations
-129444090 2005-4-27 0:00: ER No Violations 0.50
-1543912876 2014-3-18 0:00: ER No Violations
-1699302068 2013-3-4 0:00:0 ER No Violations
-1776830979 2012-9-11 0:00: ER No Violations
-1786051901 2008-12-11 0:00 ER No Violations 0.50
-1850819350 2011-7-11 0:00: ER No Violations
-1888180508 2014-10-28 0:00 ER No Violations
-1899597796 2008-4-7 0:00:0 ER No Violations 5.00
-1909181884 2019-1-14 0:00: ER No Violations
-1961717200 2014-5-6 0:00:0 ER No Violations
-1967674605 2018-4-23 0:00: ER No Violations
-244771842 2018-10-10 0:00 ER No Violations
-586379469 2013-5-22 0:00: ER No Violations
-73105475 2017-5-25 0:00: WR No Violations
-79291907 2011-10-18 0:00 ER No Violations
-956997988 2006-11-28 0:00 ER No Violations 0.50
-964485607 2012-5-24 0:00: ER No Violations
-986228033 2019-11-18 0:00 ER No Violations
0017240343 2012-02-27 Enhanced Recovery Project No Violations inspect well.
0024674618 2009-09-30 Enhanced Recovery Project Violations Noted Injection and annulus pressure test.
0073105475 2017-05-25 Work Over Reconditioning No Violations The operator is working on removing the packer and tubing. The tubing parted duing workover activities. The remainder of the tubing and packer will need to be retrived from the well bore.
0079291907 2011-10-18 Enhanced Recovery Project No Violations Inspect well.
0085929404 2017-04-27 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The annulus has equalized with the tubing. Compliance notice issued.
0103277364 2007-12-20 Enhanced Recovery Project No Violations Pressured up on annulus to 200psi and tested for 15 minutes. 5 psi decline. NOV in compliance.
0117835617 2010-04-05 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0129444090 2005-04-27 Enhanced Recovery Project No Violations Injection well test.
0194656844 2008-12-12 Enhanced Recovery Project Violations Noted Annulus side would not hold prssure. Pull tubing and packer to check status. Shut well in.
0244771842 2018-10-10 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0298313887 2014-08-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0354425590 2016-07-07 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0502720322 2007-11-01 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. 0 psi on annular side.
0581157499 2016-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0586379469 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0659106987 2003-11-13 Enhanced Recovery Project No Violations
0763495353 2018-08-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0790077112 2017-06-01 Enhanced Recovery Project Violations Noted Work on determining cause of monthly pressure test failure. Operator decided to trip the six new joints out of the hole and set and test at 350 feet; the annulus held pressure. The operator subsequently tripped in the hole and tested at 375 feet and 400 feet; the pressure test failed. The operator thought there was an issue with the used pipe and tripped out the entire string and ran in the hole with an entire string of 20 joints of new pipe to 500 feet. The test failed. Subsequently the operator tripped out the hole testing at each joint interval. After five joints had been removed, the packer briefly hung up at a depth of 368 feet. The packer was then set at 365 feet, and tested. The pressure held at 365 feet. The evaluation revealed the 2 3/8 inch casing that was cemented to the surface in 1992 had parted at 368 feet below grade. The packer was reset at 375 feet to isolate the injection zone from parted casing zone until time the well can be plugged.
0864504737 2017-05-22 Work Over Reconditioning No Violations The operator is attempting to pull the packer and tubing using the Simco hydraulic service rig. The rig does not have the power to pull the packer. The larger service rig will need to be setup on the well.
0872112316 2015-10-26 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head is in fair condition. The injector line shut off valve stem has a very slow leak.
0886653678 2010-12-02 Enhanced Recovery Project No Violations FOLLOW UP TO NOV # 1291305855 Injection and annulus pressure test. Annular side is at 0 psi. Pump up to 200 psi and test.
0956997988 2006-11-28 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0964485607 2012-05-24 Enhanced Recovery Project No Violations Inspect Well.
103277364 2007-12-20 0:00 ER No Violations 2.00
1087356809 2011-04-14 Enhanced Recovery Project No Violations Injectin and annulus pressure test.
1116149005 2017-05-31 Work Over Reconditioning No Violations Work on determining cause of monthly pressure test failure. The operator tripped the packer and tubing out of the hole to test individual joints for integrity. The packer was found to be leaking through the threads. Repairs were made and the Parmaco Packer and tubing were run in the hole. Tubing included six new joints and 14 used joints. The packer was set at 500 feet and pressure tested. The pressure was bleeding off, so a tie down was installed to verify the packer was properly set. The well was pressure tested, the test failed. Pulled one joint and tested well at 475 feet. Pressure test failed.
1134748683 2005-12-16 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1146146283 2006-04-27 Enhanced Recovery Project No Violations Injection and annulus pressure test.
117835617 2010-4-5 0:00:0 ER No Violations 0.50
1179860375 2007-05-24 Enhanced Recovery Project No Violations Injection and annulus pressure test. Advised Len Rex to pressure up on annulus to 200 psi and report. 0 psi on annular side. 5-24-2007 Pressured up on annular side to 230 psi and pressure held at 225 psi for 15 minutes.
1240574813 2009-04-24 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1291305855 2010-12-02 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Annular side is at 0 psi. Pump up to 200 psi and test.
1370915078 2010-12-02 Enhanced Recovery Project No Violations FOLLOW UP TO NOV # 1291305855 Injection and annulus pressure test. Annular side is at 0 psi. Pump up to 200 psi and test. Follow up. Subsequent inspections show pressure on annulus. Release CA.
1386189613 2013-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pump shut down during inspection.
1419383270 2016-05-09 Enhanced Recovery Project No Violations Follow up inspection from April 19, 2016. The operator has replaced the fitting that were in poor condition including the flexible flow line from the main flowline.
1427889725 2015-03-31 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1461852256 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head valves are in poor condition.
1477927615 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head fittings have been repaired and replaced.
1484057942 2017-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1496669309 2017-05-30 Work Over Reconditioning No Violations Work on determining cause of monthly pressure test failure. The old packer with the tubing was tripped out of the hole. The packer was ruined in the process. A new home made Parmaco type packer was run in the on 20 one inch PVC lined tubing at 25 feet each to 500 feet. Six of the joints are new and 14 were existing joints. Circulated borehole with about 250 gallons of fresh water and inhibitor for 30 minutes. Set packer and pressured up annulus. Pressure drifted off; test failed. Removed one joint and set packer at 475 feet, pressured up, shut in well. Pressure drifted off: test failed. The operator will trip out of the hole and test tubing and packer for integrity.
1500639524 2017-07-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well is shut in and disconnected. The packer is currently set below where the hole is in the casing to isolate formation water. Compliance notice issued; 6/1/17 & 4/27/17.
1543912876 2014-03-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1555958709 2019-4-22 0:00: ER No Violations
1563195610 2019-7-10 0:00: ER No Violations
1620885880 2018-01-08 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well is shut in and disconnected. The packer is currently set below where the hole is in the casing to isolate formation water. Compliance notice issued; 6/1/17 & 4/27/17.
1650353786 2012-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1699302068 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
17240343 2012-2-27 0:00: ER No Violations
1776830979 2012-09-11 Enhanced Recovery Project No Violations Inspect Well. Site ok.
1786051901 2008-12-11 Enhanced Recovery Project No Violations Injection and annulus pressure test. Pump up to 200 psi on annulus side.
1850819350 2011-07-11 Enhanced Recovery Project No Violations inspect well.
1888180508 2014-10-28 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1888564163 2015-05-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1899597796 2008-04-07 Enhanced Recovery Project No Violations Annulus and injection pressure test.
1909181884 2019-01-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well is shut in and disconnected from the flow line. The integrity of the casing has failed and a compliance notice was issued June 1, 2017. There is no change from the previous inspections.
1943659093 2017-11-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well is shut in and disconnected. Compliance notice issued; 6/1/17 & 4/27/17.
194656844 2008-12-12 0:00 ER No Violations 1.00
1956684216 2009-10-06 Enhanced Recovery Project No Violations Pumped up annulus to 210 psi and 0Psi decline in 15 minutes. NOV in compliance.
1961615226 2011-10-18 Enhanced Recovery Project No Violations Inspect well.
1961717200 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1967674605 2018-04-23 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well is shut in and disconnected. The packer is currently set below where the hole is in the casing to isolate formation water. Compliance notice issued; 6/1/17 & 4/27/17.
2063553413 2006-12-29 Enhanced Recovery Project No Violations Annulus pressure was at 0 psi. Pumped up annulus pressure to 200 psi. Pressure held at 200 for 15 minutes.
2113437748 2004-11-17 Enhanced Recovery Project No Violations Injection pressure test.
24674618 2009-9-30 0:00: ER No Violations 1.00
298313887 2014-8-18 0:00: ER No Violations
354425590 2016-7-7 0:00:0 ER No Violations
502720322 2007-11-1 0:00: ER No Violations 0.50
581157499 2016-1-4 0:00:0 ER No Violations
659106987 2003-11-13 0:00 ER No Violations
763495353 2018-8-13 0:00: ER No Violations
790077112 2017-6-1 0:00:0 ER No Violations
85929404 2017-4-27 0:00: ER No Violations
864504737 2017-5-22 0:00: WR No Violations
872112316 2015-10-26 0:00 ER No Violations
886653678 2010-12-2 0:00: ER No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0024674618 US-OH-122515 2009-09-30 Failure to conduct or pass mech. integrity test
0085929404 US-OH-129794 2018-03-06 9-5-10(H) Mechanical failure/contamination
0194656844 US-OH-119615 2008-12-12 Failure to conduct or pass mech. integrity test
0502720322 US-OH-125496 2007-11-01 Failure to conduct or pass mech. integrity test
0790077112 US-OH-128996 2017-06-29 9-5-10(J) Well incapable of inj./production
1291305855 US-OH-108219 2010-12-02 Failure to conduct or pass mech. integrity test

For data sources see[9]

References