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34-005-22184

Well Details

Well ID: 34-005-22184
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: BLAND R D
License Status: Active Injection
License Date: 1983-06-10
Spud Date: 1983-08-12
Spud Drilling Contractor: M&G OIL CO.
Final Drill Date: 1983-08-25
Well Total Depth: 663.00 ft
Configuration: Vertical
Latitude: 40.880000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Enhanced Recovery 1983-06-10 Issued Date 6/10/83 Expired Date 12/7/83 Acres 0080000 Tool Type CT Proposed Formation BEREA Proposed Depth 00663 Proposed Drill Depth 00663
Original Spud 1983-08-12 CONVERT 6-11-83
Completed 1983-08-25 CONVERT 6-11-83
Reached Total Depth 1983-08-25 CONVERT 6-11-83
Construction Permit Expires 1983-12-07 CONVERT 6-11-83
CO 1984-01-12 133 QUAKER STATE OIL REF CORP GeoDate 6/10/83
First Injection 1984-01-12 CONVERT 6-11-83
Completion Report Received 1984-02-24 CONVERT 6-11-83
Annulus Pressure Monitoring Approved 1994-11-18 CONVERT 6-11-83
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 6/10/83
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Last Compliance Report 2009-03-13 CONVERT 6-11-83
Record Last Modified 2017-02-15 CONVERT 6-11-83

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-23 576 634 0
2000-05-23 580 630 0
576 634 0
580 630 0
576 634 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 110 Qts 0 FOR PRODUCTION
NITR 0 50 Qts 0 FOR ERP

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 DEEP RESOURCES LLC 0.00 180.00 365
2009 DEEP RESOURCES LLC 0.00 151.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 DEEP RESOURCES LLC Brine 0 365
2009 DEEP RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1050938084 2011-11-17 0:00 ER No Violations
-1067649632 2011-7-12 0:00: ER No Violations
-1077985550 2004-4-22 0:00: ER No Violations
-1086629621 2010-3-30 0:00: ER No Violations 0.50
-1119895437 2007-5-31 0:00: ER No Violations 0.50
-1134135772 2019-7-2 0:00:0 ER No Violations
-1226506260 2019-1-10 0:00: ER No Violations
-1228915754 2020-4-10 0:00: ER No Violations
-1285044654 2017-1-6 0:00:0 ER No Violations
-136198518 2008-2-20 0:00: ER No Violations 0.50
-1471689629 2012-2-27 0:00: ER No Violations
-175877468 2016-4-19 0:00: ER No Violations
-1802992674 2014-5-6 0:00:0 ER No Violations
-1918178391 2015-5-20 0:00: ER No Violations
-1976967508 2016-1-6 0:00:0 ER No Violations
-2002350871 2016-7-6 0:00:0 ER No Violations
-2017921102 2014-10-29 0:00 ER No Violations
-2047388950 2020-2-24 0:00: ER No Violations
-2130008163 2018-4-19 0:00: ER No Violations
-338107849 2009-4-23 0:00: ER No Violations 1.00
-354885517 2012-9-11 0:00: ER No Violations
-574079887 2004-11-18 0:00 ER No Violations
-679756636 2009-10-20 0:00 ER No Violations 0.50
-744305707 2007-10-26 0:00 ER No Violations 0.50
-84721502 2014-3-17 0:00: ER No Violations
-946002843 2017-7-19 0:00: ER No Violations
-970448579 2019-4-18 0:00: ER No Violations
-983383773 2013-12-4 0:00: ER No Violations
0052396312 2007-10-30 Enhanced Recovery Project No Violations Pumped annular side to 230psi and pressure dropped 5 psi in 15 minutes. NOV in compliance.
0084721502 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0136198518 2008-02-20 Enhanced Recovery Project No Violations Annulus and injection pressure test.
0175877468 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0329149435 2018-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0338107849 2009-04-23 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0354885517 2012-09-11 Enhanced Recovery Project No Violations Inspect Well. Injection valve stripped.
0357718328 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Injection valve is bad.
0415124570 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Injector valve failed during inspection and blew out. New valve installed.
0574079887 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
0645196895 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0679756636 2009-10-20 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0744305707 2007-10-26 Enhanced Recovery Project No Violations Injection and annulus pressure test. 0 psi on annular side.
0820470749 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0946002843 2017-07-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0955105361 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The annulus test valve is in poor condition.
0959722586 2009-02-26 Enhanced Recovery Project No Violations Pulled tubing and packer and replaced packer with a Butler Larkin compression packer. After several tests pressure remains equilized. Shut injection pressure down until well tests.
0983266799 2012-05-30 Enhanced Recovery Project No Violations Inspect Well.
0983383773 2013-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pump shut down during inspection.
1000210287 2017-11-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1046605082 2008-12-02 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures are equal.
1050938084 2011-11-17 Enhanced Recovery Project No Violations Inspect well.
1067649632 2011-07-12 Enhanced Recovery Project No Violations Inspect well.
1070301798 2015-05-15 Enhanced Recovery Project No Violations The well is an injection well in the waterflood enhanced recovery project. ID posted. The well is in use.
1077985550 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test.
1081466762 2009-01-27 Enhanced Recovery Project No Violations Rig over well setting packer. Fluid will flow thru annulus. Shut in annulus.
1086629621 2010-03-30 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1110743117 2005-11-29 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1119895437 2007-05-31 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1144333868 2006-04-06 Enhanced Recovery Project No Violations Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap. 1 tubing on a packer used for injection.
1183168374 2005-04-27 Enhanced Recovery Project No Violations Injection well test.
1228945328 2008-12-10 Enhanced Recovery Project No Violations Pressure dropped and equalizied in 5 minutes. Reset packer at a later date.
1233596210 2009-02-02 Enhanced Recovery Project No Violations Trouble releasing packer. Parted 1 tubing at 3. Packer needs replaced. Advised Len Rex to shut off water flow out of well.
1234286612 2006-12-29 Enhanced Recovery Project No Violations Annulus pressure was at 0 psi. Pressured up on annulus at 200 psi and pressure held for 15 minutes.
1235483835 2009-02-23 Enhanced Recovery Project No Violations Pulling injection tubing and found one joint collapsed at 500. Tripped out to check packer. Packer needs replaced.
1251484495 2016-02-03 Work Over Reconditioning No Violations The well is constructed with 2 3/8 inch tubing at a depth of 568 feet cemented to the surface. The well is open hole to the total depth of 663 feet. The packer was released and the top most five foot long joint was determined to have failed and was replaced. The entire tubing string and packer was not removed from the borehole. Total of 19 joints of 25 foot sections of PVC lined one Inch tubing with one five foot joint were run in the hole on 3/4/2009 with a Butler Larkin packer set in compression. Approximately 300 gallon of fresh water were pumped through the annulus and circulated to the surface throught the tubing prior to setting the packer. The packer was set and the annulus was pressured up to 368 psi. The pressure was monitored for 15 minutes with 5.4% pressure loss. The test was performed a second time pressuring the well up to 420 psi. The pressure was monitored for 15 minutes with a 2.3% loss. This is within the stated margin of 5% pressure loss. The well passes the Mechanical Integrity Test. The well head was reconstructed with new parts and put into production.
1285044654 2017-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1395118696 2015-03-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Main flow line valves shut off during inspection.
1443620635 2003-08-07 Enhanced Recovery Project No Violations
1464733866 2018-10-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1471689629 2012-02-27 Enhanced Recovery Project No Violations inspect well.
1484735193 2018-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1545831476 2018-12-18 Enhanced Recovery Project No Violations Inspect well for pressure and integrity.
1653647426 2020-1-27 0:00: ER No Violations
1659063752 2010-11-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1791325337 2013-05-22 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Valve for annulus leaks.
1802992674 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1813333572 2006-12-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1918178391 2015-05-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1976967508 2016-01-06 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. Well has equalized. Operator conducted pressure test and verified failure.
2002350871 2016-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2017921102 2014-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2063770954 2015-10-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in poor condition. The operator was notified the flow line shut off valve stem has a slow leak. The operator subsequently replaced fittings. No leaks.
2114206956 2019-11-18 0:00 ER No Violations
2130008163 2018-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
329149435 2018-1-4 0:00:0 ER No Violations
357718328 2012-11-27 0:00 ER No Violations
415124570 2013-3-4 0:00:0 ER No Violations
445285454 2020-7-8 0:00:0 ER No Violations
52396312 2007-10-30 0:00 ER No Violations 1.00
645196895 2014-7-17 0:00: ER No Violations
820470749 2017-4-13 0:00: ER No Violations
955105361 2016-10-19 0:00 ER No Violations
959722586 2009-2-26 0:00: ER No Violations 4.00
983266799 2012-5-30 0:00: ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1046605082 US-OH-100731 2008-11-26 Failure to conduct or pass mech. integrity test
1976967508 US-OH-119981 2016-02-12 Mechanical failure/contamination

For data sources see[9]

References