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34-005-22135

Well Details

Well ID: 34-005-22135
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: BLAND R D
License Status: Active Injection
License Date: 1983-06-10
Spud Date: 1983-08-26
Spud Drilling Contractor: M&G OIL CO.
Final Drill Date: 1983-09-06
Well Total Depth: 635.00 ft
Configuration: Vertical
Latitude: 40.880000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Enhanced Recovery 1983-06-10 Issued Date 6/10/83 Expired Date 12/7/83 Acres 0080000 Tool Type CT Proposed Formation BEREA Proposed Depth 00635 Proposed Drill Depth 00635
Original Spud 1983-08-26 CONVERT 6-11-83,SWIW
Completed 1983-09-06 CONVERT 6-11-83,SWIW
Reached Total Depth 1983-09-06 CONVERT 6-11-83,SWIW
Construction Permit Expires 1983-12-07 CONVERT 6-11-83,SWIW
CO 1984-01-12 133 QUAKER STATE OIL REF CORP GeoDate 6/10/83
First Injection 1984-01-12 CONVERT 6-11-83,SWIW
Completion Report Received 1984-02-24 CONVERT 6-11-83,SWIW
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 6/10/83
Annulus Pressure Monitoring Approved 1995-10-26 CONVERT 6-11-83,SWIW
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Last Compliance Report 2009-07-20 CONVERT 6-11-83,SWIW
Record Last Modified 2018-12-19 CONVERT 6-11-83,SWIW

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-23 564 0
2006-09-11 580 604 0
564 0
582 606 0
580 604 0
564 0
2000-05-23 582 606 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 24 Qts 0 FOR ERP
NITR 0 36 Qts 0 FOR PRODUCTION

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1113927055 2014-5-6 0:00:0 ER No Violations
-1354518112 2016-1-5 0:00:0 ER No Violations
-141141495 2016-11-7 0:00: ER No Violations
-1433665861 2008-2-21 0:00: ER No Violations 1.00
-1451405245 2010-11-26 0:00 ER No Violations 0.50
-1561114708 2019-4-18 0:00: ER No Violations
-1614329016 2015-5-20 0:00: ER No Violations
-1642419334 2007-5-31 0:00: ER No Violations 1.00
-164885855 2020-7-8 0:00:0 ER No Violations
-1701887985 2009-10-20 0:00 ER No Violations 1.00
-1877645203 2018-5-1 0:00:0 ER No Violations
-1903735574 2013-12-4 0:00: ER No Violations
-1923723377 2019-7-2 0:00:0 ER No Violations
-1967981771 2017-1-6 0:00:0 ER No Violations
-313950739 2018-10-2 0:00: ER No Violations
-34845830 2012-9-11 0:00: ER No Violations
-423404971 2004-4-22 0:00: ER No Violations
-436038962 2009-4-23 0:00: ER No Violations
-683956873 2019-1-10 0:00: ER No Violations
-685138061 2012-11-27 0:00 ER No Violations
-797391984 2016-10-19 0:00 ER No Violations
-803152526 2010-3-30 0:00: ER No Violations 0.50
-963433160 2018-7-6 0:00:0 ER No Violations
-969019889 2016-4-19 0:00: ER No Violations
0030408130 2003-08-07 Enhanced Recovery Project No Violations
0034845830 2012-09-11 Enhanced Recovery Project No Violations Inspect Well. Site ok.
0133075958 2008-03-13 Enhanced Recovery Project No Violations Tested annulus and injection pressure. NOV in compliance.
0141141495 2016-11-07 Enhanced Recovery Project No Violations Operator performed repairs on well and replaced fittings that were in poor condition.
0313950739 2018-10-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0373331196 2005-11-29 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0423404971 2004-04-22 Enhanced Recovery Project No Violations Injection pressure test.
0436038962 2009-04-23 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Pressures are equalized at 350 psi.
0522032175 2006-12-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0679387333 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The valve for the annulus was frozen at time of inspection.
0685138061 2012-11-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0720934733 2008-02-20 Enhanced Recovery Project Violations Noted Annulus and ijection pressure test. Annular side is 0 psi. Pump up to 200 psi and test.
0748631443 2018-12-18 Work Over Reconditioning No Violations The well is constructed with 2 3/8 inch tubing at a depth of 570 feet cemented to the surface with 40 sacks of cement in 1983. The well is open hole from 570 feet to the total depth of 635 feet. The wellhead was removed and the tubing and packer were pulled up 11 inches without releasing the packer. New parts were used to reconstruct the wellhead. The annulus was pressured up to 410 psi. The valve stem packing was tightened and the test continued for 15 minutes with a total loss of 5 psi over 15 minutes, with less than one percent in pressure loss. This is within the stated margin of 5% pressure loss. The well passes the Mechanical Integrity Test. Authorization to put the well into operation was granted.
0797391984 2016-10-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The nipple on the injection line is in poor condition.
0803152526 2010-03-30 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0805316189 2013-03-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0818339814 2017-11-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0832372216 2013-04-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test.
0869892637 2008-12-02 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0915459370 2012-02-27 Enhanced Recovery Project No Violations inspect well.
0925317236 2017-07-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0944485105 2011-10-17 Enhanced Recovery Project No Violations Inspect well.
0963433160 2018-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0965536617 2005-04-27 Enhanced Recovery Project No Violations Injection well test.
0969019889 2016-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The annulus test port shut off valve has failed.
1010955511 2018-04-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head tubing in poor condition.
1043457072 2004-11-18 Enhanced Recovery Project No Violations Injection pressure test.
1048734563 2015-03-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Main flow line valves shut off during inspection.
1113927055 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1193415588 2007-10-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1238714666 2018-05-01 Enhanced Recovery Project No Violations Inspect well with operator to preform monthly pressure test of the annulus on the well. The annulus shut off valve was replaced for this test.
1247684209 2009-05-23 Enhanced Recovery Project No Violations Pressured up annulus to 200 psi and 0 psi decline in 15 minutes. NOV in compliance.
1248996885 2014-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1253640933 2020-1-27 0:00: ER No Violations
1268278262 2016-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Retest wellhead. Fittings have thawed out after freezing due to cold weather.
1302621711 2011-04-12 Enhanced Recovery Project No Violations Injection and annulus pressure test.
133075958 2008-3-13 0:00: ER No Violations 1.00
1354518112 2016-01-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Annulus fitting was frozen due to cold weather.
1362199934 2016-05-09 Enhanced Recovery Project No Violations Follow up inspection from April 19, 2016. The operator has replaced the fitting that were in poor condition.
1405945494 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1433665861 2008-02-21 Enhanced Recovery Project No Violations Retest packer. Pressured up annulus to 300 psi and pressure dropped to 0 psi immediately. Injection is at 330 psi. Tubing problem.
1451405245 2010-11-26 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1495455948 2017-04-13 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1614329016 2015-05-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1642419334 2007-05-31 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1701887985 2009-10-20 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1739686434 2018-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1754306171 2011-07-12 Enhanced Recovery Project No Violations inspect well.
1822637501 2006-04-06 Enhanced Recovery Project No Violations Injection and annulus pressure test. Constructed with 2 tubing cemented at Berea cap. 1 tubing on a packer used for injection.
1854512457 2020-4-10 0:00: ER No Violations
1877645203 2018-05-01 Enhanced Recovery Project No Violations Inspect well with operator to preform monthly pressure test of the annulus on the well.
1903735574 2013-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Pump shut down during inspection.
1967981771 2017-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
2033592345 2015-05-15 Enhanced Recovery Project No Violations The well is an injection well in the waterflood enhanced recovery project. ID posted. The well is in use.
2069282918 2012-05-30 Enhanced Recovery Project No Violations Inspect Well.
2089122184 2016-07-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head fittings have been repaired recently.
2101991558 2011-04-13 Enhanced Recovery Project No Violations Injection and annulus pressure test.
2132338957 2015-10-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in fair condition. The operator reported a flow line leak and repaired the fittings.
278066807 2019-11-18 0:00 ER No Violations
30408130 2003-8-7 0:00:0 ER No Violations
373331196 2005-11-29 0:00 ER No Violations 0.50
522032175 2006-12-13 0:00 ER No Violations 1.00
679387333 2014-3-17 0:00: ER No Violations
720934733 2008-2-20 0:00: ER No Violations 1.00
748631443 2018-12-18 0:00 WR No Violations
805316189 2013-3-4 0:00:0 ER No Violations
818339814 2017-11-14 0:00 ER No Violations
832372216 2013-4-15 0:00: ER No Violations
869892637 2008-12-2 0:00: ER No Violations 1.00
915459370 2012-2-27 0:00: ER No Violations
925317236 2017-7-19 0:00: ER No Violations
944485105 2011-10-17 0:00 ER No Violations
965536617 2005-4-27 0:00: ER No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0436038962 US-OH-124688 2009-04-23 Failure to conduct or pass mech. integrity test
0720934733 US-OH-128196 2008-02-20 Failure to conduct or pass mech. integrity test

For data sources see[5]

References