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34-005-21918

Well Details

Well ID: 34-005-21918
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Country: United States
State: Ohio
County: Ashland
Municipality: Perry Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: BROWN UNIT
License Status: Active Injection
License Date: 1986-07-14
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1986-08-08
Well Total Depth: 760.00 ft
Configuration: Vertical
Latitude: 40.900000
Longitude: -82.140000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1961-07-03 133 QUAKER STATE OIL REF CORP GeoDate 7/3/61
Oil and Gas 1961-07-03 Issued Date 7/3/61 Expired Date Acres 0085000 Tool Type CT Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
CO 1986-07-07 133 QUAKER STATE OIL REF CORP GeoDate 7/7/86
Enhanced Recovery 1986-07-07 Issued Date 7/14/86 Expired Date 7/14/87 Acres 0150047 Tool Type NT Proposed Formation BEREA Proposed Depth 00760 Proposed Drill Depth 00760
Completed 1986-08-08 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472
Reached Total Depth 1986-08-08 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472
First Injection 1986-11-26 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472
Completion Report Received 1987-01-05 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472
Construction Permit Expires 1987-07-14 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 7/7/86
Annulus Pressure Monitoring Approved 1999-03-08 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472
Last Compliance Report 2000-01-12 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15 ALSO DRILLED BY P.M. DRLG CONVERT 7-12-86, LOG TYPE=X,Y, ACRES 150.0472

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-23 641 701 0
641 701 0
641 701 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NONE

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1012048814 2016-5-9 0:00:0 ER No Violations
-1095614617 2012-9-11 0:00: ER No Violations
-1191837821 2014-10-29 0:00 ER No Violations
-1238812669 2008-3-13 0:00: ER No Violations 0.50
-1442788976 2009-10-6 0:00: ER No Violations 0.50
-1495534446 2016-4-15 0:00: ER No Violations
-150377399 2015-3-19 0:00: ER No Violations
-1594753256 2018-9-6 0:00:0 WR No Violations
-1597933583 2010-4-6 0:00:0 ER No Violations 0.50
-1642337969 2020-1-22 0:00: ER No Violations
-1660917286 2017-1-5 0:00:0 ER No Violations
-1662390210 2019-4-17 0:00: ER No Violations
-168220149 2012-3-5 0:00:0 ER No Violations
-1727056000 2010-12-16 0:00 ER No Violations 1.00
-1790131421 2007-5-24 0:00: ER No Violations 1.00
-1809697017 2005-4-27 0:00: ER No Violations 0.50
-1845255212 2014-5-6 0:00:0 ER No Violations
-2140810724 2012-12-4 0:00: ER No Violations
-272076406 2016-7-8 0:00:0 ER No Violations
-348771545 2004-11-17 0:00 ER No Violations
-368469829 2018-1-18 0:00: ER No Violations
-390474189 2013-10-29 0:00 ER No Violations
-494283911 2016-11-1 0:00: ER No Violations
-542748239 2019-7-3 0:00:0 ER No Violations
-598142916 2012-2-6 0:00:0 ER No Violations
-664699459 2017-11-14 0:00 ER No Violations
-838588812 2013-4-15 0:00: ER No Violations
-971041674 2009-4-27 0:00: ER No Violations 0.50
-990171065 2006-8-21 0:00: ER No Violations 0.50
0093064011 2008-03-24 Enhanced Recovery Project No Violations Pressured up annulus to 310 psi and no decline in pressure after 15 minutes.
0105827733 2017-04-24 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Measure the specific gravity of the water at 1.055 units.
0150377399 2015-03-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0157775923 2005-12-01 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0168220149 2012-03-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0183439854 2015-08-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The union and injection line fitting were leaking. Contacted operator and fittings were replaced and repaired.
0272076406 2016-07-08 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head fittings have been replaced. The tubing is in fair condition and is not leaking.
0312990111 2009-01-06 Enhanced Recovery Project No Violations Pumped annulus side to 200 psi and 0 psi decline in 15 miutes.
0348771545 2004-11-17 Enhanced Recovery Project No Violations Injection pressure test.
0363323470 2015-05-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0368469829 2018-01-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in very poor condition.
0390474189 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0465361943 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0494283911 2016-11-01 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0598142916 2012-02-06 Enhanced Recovery Project No Violations Inspect well.
0625121315 2012-05-31 Enhanced Recovery Project No Violations Inspect Well. Injector threads leak during testing with guage.
0664699459 2017-11-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0807490275 2003-08-07 Enhanced Recovery Project No Violations
0838588812 2013-04-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well was serviced and packer was released and reset prior to retesting. Conduct fifteen minute pressure test on well. Passed test.
0934189572 2019-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0971041674 2009-04-27 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0990171065 2006-08-21 Enhanced Recovery Project No Violations Injection and annulus pressure test. 0 psi annulus side. Re-pressure annulus to 200 psi. Sun, 75 degrees.
1012048814 2016-05-09 Enhanced Recovery Project No Violations Follow up inspection from April 15, 2016. The operator has replaced the fitting that were in poor condition. The one inch injection tubing is in fair condition.
1019343868 2011-07-11 Enhanced Recovery Project No Violations Inspect well. Pressure zero, pressure up to 190 lost pressure, well needs rework.
1035377081 2015-10-26 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Well head is in fail condition. No leaks.
105827733 2017-4-24 0:00: ER No Violations
1060948326 2016-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1095614617 2012-09-11 Enhanced Recovery Project No Violations Inspect Well. Site ok.
1191837821 2014-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1229690324 2008-12-18 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. Annulus pressure is 0 psi.
1237945214 2007-01-31 Enhanced Recovery Project No Violations Annulus mini-test is @150 psi and injection pressure is 300 psi. Last test annulus pressure reading was 0 psi. Test approved. 15 degrees,sun.
1238176765 2020-7-17 0:00: ER No Violations
1238812669 2008-03-13 Enhanced Recovery Project Violations Noted Annulus and injection pressure test. Annular side is at 0 psi. Is not holding pressure from last inspection.
1258854472 2018-08-14 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The injection tubing and annulus have equalized. The well was shut-in.
1283130224 2007-10-22 Enhanced Recovery Project No Violations Injection and annulus pressure test. Pumped annular side to 350 psi and tested for 15 minutes. 0 psi decline. NOV in compliance.
1296146665 2011-01-27 Enhanced Recovery Project No Violations Injection and annulus pressure test. Re-set packer. Pressured annulus to 250 psi. 10 psi drop in 15 minutes. 10 psi drop after 5 minutes.
1355195964 2013-08-27 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1369752351 2013-04-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Test failed. Well shut in.
1408483731 2011-10-18 Enhanced Recovery Project No Violations Inspect well.
1442788976 2009-10-06 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1495534446 2016-04-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. The well head is in poor condition.
1500640352 2017-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1521672278 2006-12-19 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1536603099 2018-09-05 Work Over Reconditioning No Violations The operator pulled the packer and 26 joins of Sealtite lined tubing from the well due to integrity failure. The packer was lost in the hole as the tubing was being pulled out of the well. There was 33 inches of rusted tubing cut off on the top most joint. A packer and tubing was run in the hole to be set at a depth of 647 below grade. The packer would not set at this depth or at shallower depths that were attempted. The string was pulled out of the well and it was discovered the new packer was lost in the hole. A second new Parmaco packer was attached to the tubing and run in the hole.
157775923 2005-12-1 0:00: ER No Violations 0.50
1594753256 2018-09-06 Work Over Reconditioning No Violations Tom Benko, ODNR requested assistance with packer installation and pressure testing in the well. The operator set the packer and pressured up to 410 psi at 3:25 PM. At 3:40 pm, pressure was at 399 psi. The test passed.
1597933583 2010-04-06 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1660917286 2017-01-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1667837264 2018-10-09 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1681373576 2007-10-17 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. 0 psi on annular side. Needs pressured to 200 psi and tested.
1727056000 2010-12-16 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. ERP# 19, W-4.
1729516534 2018-05-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1761912755 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1790131421 2007-05-24 Enhanced Recovery Project No Violations Injection and annulus pressure test. Advised Len Rex to pressure up on annular side to 200 psi and report to inspector. Need a 3/4 plug in annular valve. Pressured up to 260 psi and 0 psi decline in 15 minutes.
1809697017 2005-04-27 Enhanced Recovery Project No Violations Injection well test.
183439854 2015-8-27 0:00: ER No Violations
1845255212 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1856077855 2010-12-17 Enhanced Recovery Project No Violations Annular test failed at 250 psi. Pressure dropped 20 psi in 15 minutes.Find leak and test.
1859411840 2018-09-06 Work Over Reconditioning No Violations The parmaco packer was run into the hole to a depth of 647 feet. Fresh water with rust inhibitor was circulated throughout the well bore. Inspector Thomas Zacharyasz witnessed the setting of the packer and pressuring the anulus. The well was pressured up and held for 15 minutes, the loss was less than three percent and was within the margin of error. The operator was notified that the well could be put into operation. The compliance notice of August 14, 2018 was resolved.
1859920424 2015-05-18 Enhanced Recovery Project No Violations The well is an injection well in the waterflood enhanced recovery project. ID posted.
195418885 2019-11-18 0:00 ER No Violations
2140810724 2012-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
312990111 2009-1-6 0:00:0 ER No Violations 1.00
363323470 2015-5-20 0:00: ER No Violations
417068095 2020-4-21 0:00: ER No Violations
465361943 2014-7-17 0:00: ER No Violations
625121315 2012-5-31 0:00: ER No Violations
807490275 2003-8-7 0:00:0 ER No Violations
93064011 2008-3-24 0:00: ER No Violations 1.00
934189572 2019-1-4 0:00:0 ER No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1229690324 US-OH-106181 2008-12-19 Failure to conduct or pass mech. integrity test
1238812669 US-OH-106362 2008-03-13 Failure to conduct or pass mech. integrity test
1258854472 US-OH-106970 2018-09-25 9-5-10(H) Mechanical failure/contamination
1681373576 US-OH-116645 2007-10-17 Failure to conduct or pass mech. integrity test
1727056000 US-OH-117141 2010-12-16 Failure to conduct or pass mech. integrity test

For data sources see[5]

References