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Well ID: 34-005-21155 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Perry Township | |
Operator Name: MOHICAN RIVER ENERGY HOLDINGS | |
Well Pad ID: | |
Farm/Lease Name: FUNK (ERP # 18) | |
License Status: Final Restoration | |
License Date: 2012-07-12 | |
Spud Date: 1955-03-09 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 1955-03-15 | |
Well Total Depth: 630.00 ft | |
Configuration: Vertical | |
Latitude: 40.830000 | |
Longitude: -82.140000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1955-03-09 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
Completed | 1955-03-15 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
Reached Total Depth | 1955-03-15 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
Completion Report Received | 1955-04-10 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
CO | 1985-04-02 | 1496 KATE PAUL & KEVIN GeoDate 4/2/85 |
Enhanced Recovery | 1985-04-02 | Issued Date 4/2/85 Expired Date 9/29/85 Acres 0183240 Tool Type CT Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000 |
Annulus Pressure Monitoring Approved | 1986-12-16 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
Change of Owner | 1997-10-21 | Operator changed from 1496, KATE PAUL & KEVIN to 3687, MOUNT RICHARD |
Last Compliance Report | 2000-01-06 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
Change of Owner | 2006-09-13 | Operator changed from 3687, MOUNT RICHARD to 7923, TERRABYTE LLC |
Change of Owner | 2008-06-19 | Operator changed from 7923, TERRABYTE LLC to 8182, MOHICAN RIVER ENERGY HOLDINGS |
APP | 2012-07-12 | Proposed Formations:BEREA, Issued Date:7/12/2012, Expired Date:7/12/2014 12:00:00 PM, Drilling unit acres:630, Proposed Well Type:EOR, Proposed Well Class:ERP |
Plugged/Abandoned | 2012-08-29 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
Construction Permit Expires | 2014-07-12 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
Record Last Modified | 2017-02-15 | RBDMS Rec PA CHANGED TO FR STATUS PER FACILITY REPORT FROM TOM ZACHARYASZ 8/26/2014 CM |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-23 | 537 | 630 | 0 |
537 | 630 | 0 | |
537 | 630 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 100 Qts | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | MOUNT RICHARD | 0.00 | 24.00 | 250 |
1999 | MOUNT RICHARD | 0.00 | 19.00 | 280 |
2000 | CHESAPEAKE APPALACHIA LLC | 1362.00 | 0.00 | 365 |
2001 | MOUNT RICHARD | 0.00 | 9.00 | 270 |
2002 | MOUNT RICHARD | 0.00 | 17.00 | 250 |
2003 | MOUNT RICHARD | 0.00 | 14.00 | 275 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1998 | MOUNT RICHARD | Brine | 38 | 250 |
1999 | MOUNT RICHARD | Brine | 15 | 280 |
2000 | CHESAPEAKE APPALACHIA LLC | Brine | 0 | 365 |
2001 | MOUNT RICHARD | Brine | 0 | 270 |
2002 | MOUNT RICHARD | Brine | 0 | 250 |
2003 | MOUNT RICHARD | Brine | 0 | 275 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-107289304 | 2013-3-12 0:00: | PW | No Violations | 0.50 |
-1076893282 | 2009-1-27 0:00: | SW | No Violations | 1.00 |
-1092713810 | 2011-7-29 0:00: | ER | No Violations | |
-1299475436 | 2007-8-21 0:00: | SW | No Violations | 1.00 |
-1873020661 | 2010-9-17 0:00: | SW | No Violations | 1.00 |
-356770949 | 2004-6-21 0:00: | SW | No Violations | 0.50 |
-553021676 | 2009-6-23 0:00: | SW | No Violations | 1.00 |
-99760586 | 2003-12-16 0:00 | SW | No Violations | 1.00 |
0000UIC275 | 1987-08-10 | Enhanced Recovery Project | No Violations | 1509.22 (A)(2) |
0000UIC276 | 1987-08-10 | Enhanced Recovery Project | No Violations | 1501:9-5-01 (A)(6) |
0000UIC277 | 1987-08-10 | Enhanced Recovery Project | No Violations | 1501:9-5-05 (H) |
0000UIC278 | 1987-08-10 | Enhanced Recovery Project | No Violations | 1509.072 (A) |
0000UIC279 | 1987-08-10 | Enhanced Recovery Project | No Violations | 1501:9-5-10 (E)(F) |
0000UIC825 | 1989-12-19 | Enhanced Recovery Project | No Violations | 1501:9-5-10 (E) monitor/rept. |
0000UIC826 | 1989-12-19 | Enhanced Recovery Project | No Violations | 1501:9-5-10 (F) monitor annulus |
0000UIC889 | 1990-04-30 | Enhanced Recovery Project | No Violations | 1509.22(C)3 MAINTAIN DIKE |
0000UIC890 | 1990-04-30 | Enhanced Recovery Project | No Violations | 1501:9-5-09 A,6 PREVENT OF POLLUTION |
000UIC1122 | 1991-06-21 | Enhanced Recovery Project | No Violations | 1501:9-5-10 (E) & (F) 1ST.QTR 1991 RPT. |
000UIC1209 | 1992-01-02 | Enhanced Recovery Project | No Violations | 1501: 9-3-07 (E) QUARTERLY REPORTS |
000UIC1397 | 1993-05-12 | Enhanced Recovery Project | No Violations | 1509.03 RULES & REGULATIONS |
000UIC1398 | 1993-05-12 | Enhanced Recovery Project | No Violations | 1501: 9-5-06 PREVENT CONTAMINATE |
000UIC1399 | 1993-05-12 | Enhanced Recovery Project | No Violations | 1501: 9-9-05 (A) (7) (9) PRODUCING OPERATIONS |
000UIC1422 | 1993-06-22 | Enhanced Recovery Project | No Violations | 1501: 9-5-10 (E) (F) QUARTERLY REPORTS |
001220i265 | 2002-09-27 | Enhanced Recovery Project | Violations Noted | Met with Richard Mount at well site to discuss violations. Brine is being injected by gravity. Advised him to install a barrel counter between storage tanks and well. Replace pressure gauge fittings on well head. Clean-up oil residue and brine spill around well head. Screwed a 2 bull plug in dike drain |
001220i297 | 2002-10-22 | Salt Water Injection Well | No Violations | Valves on well have been cleaned up and are working. Tom Tomastic advised a barrel counter is not needed if fluids are monitored by tanks. Nov in compliance. Brine is injected by gravity. 40 degrees, sunny. Violation 1509.22a. |
0026478763 | 2002-09-23 | Salt Water Injection Well | No Violations | Nov was written to Richard Mount to replace valve on well head that operates pressure gauge. It has not been replaced. Well does not seem to be active at this time. Valves and fittings are rusted and wont turn.3x3 dead vegetation area 2west of well. Called Richard Mount to meet on site at later date to discuss compliance. |
0099760586 | 2003-12-16 | Salt Water Injection Well | No Violations | No violations, well on vacume.Cloudy 40 degrees. |
0107289304 | 2013-03-12 | Production Wells | No Violations | Well is due for final restoration. I spoke with Rod at Mohican River and he advised that they would be finishing up clean up and grading of the site when weather is more favorable for reclamation. The site is rough graded now and the well head has been cut off. Tanks have been removed. |
0206510166 | 2006-10-30 | Salt Water Injection Well | Violations Noted | Called by pumper to investigate brine spill. During Saturday or Sunday 10-28-,10-29-2006 vandals opened brine storage valve inside dike, spilling 30 barrels of brine. Dike had a 1.5 drain in bottom of concrete dike. Plug was removed and brine escaped and ran down township road 65 approximatly 500. TR 65 is a gravel road and brine stayed on roadway. Puddles in road read over 6000 ppm chlorides. Advised company to plug drain and lock valves on tanks. I will monitor roadway. |
0223051147 | 2010-09-17 | Salt Water Injection Well | No Violations | FOLLOW UP TO NOV # 1284730287 Injection well is idle. Tank battery has been removed and concrete dike remains on site. No response to verbal recommendations to put well in production or plug and abandon. Cloudy, 60 degrees. |
0356770949 | 2004-06-21 | Salt Water Injection Well | No Violations | Nov in compliance |
0553021676 | 2009-06-23 | Salt Water Injection Well | No Violations | Well is in compliance. 50 psi on annulus side and vacume on tubing. Clean and mowed around pump house and tank battery. Sun, 85 degrees. |
0872994796 | 2006-11-29 | Salt Water Injection Well | No Violations | Brine contamination has been removed and new gravel is replaced on TR 65 by Perry Township Trustees. Drain in dike has been tapped and plugged. Locks have been placed on drain valves. NOV in compliance. Rain, 60 degrees. |
1076893282 | 2009-01-27 | Salt Water Injection Well | No Violations | Injection well is shut in at this time due to cold weather. 10 degrees. 0 psi on gauges. No violations. |
1084366014 | 2004-05-12 | Salt Water Injection Well | No Violations | 1x1 area inside dike is oil stained. Brine is gravity fed to well. In compliance |
1092713810 | 2011-07-29 | Enhanced Recovery Project | No Violations | Inspect well. Well is idle. NOV of 9/17/2011 to plug well is in force. Operator needs to plug well or put into production. |
1096465218 | 2004-09-29 | Salt Water Injection Well | No Violations | Well is gravity feed and gauges read 0 psi on tubing and annulus. 3-100 barrel tanks inside concrete dike and 2-100 barrel tanks outside dike. Dike is free of oil and water.Cloudy 55 degrees. |
1119444168 | 2005-06-22 | Salt Water Injection Well | No Violations | Well is on vacume. No violations. Sun 70 degrees. |
1148047087 | 2006-05-19 | Salt Water Injection Well | No Violations | Well is in operation. Called Jon Hiller to advise of annular pressure test is needed on well and packer. Presure gauge is rusted and I cannot install my gauge. Schedule date to test packer after Memorial day. Well is on vacume. Rain, 50 degrees. |
1156357047 | 2006-08-23 | Salt Water Injection Well | Violations Noted | Requested by Jim Watson to pressure test tubing and packer in injection well. Injection tubing is on vacume. Pressured up on annulus between 2 3/8 and 1 tubing to 120 psi and pressure dropped to 80 psi in 2 minutes. Pressured up again and it did not hold. Bubbles began to come thru cement between 2 and 5 casing. Advised company to shut down injection untill repaired. Well ownership on database is Richard Mount. Advised Jim Watson to have well transferred to his bond. |
1162470503 | 2006-11-02 | Salt Water Injection Well | No Violations | Inspect facility for plugs in tank battery dike drain. Plug was installed. Plug was installed in 1/4 inpection valve and valves are closed. Perry township has spread new gravel on roadway where brine was spilled. No attempt at this time to repair injection well violation. Sun, 30 degrees. |
1164828023 | 2006-11-29 | Salt Water Injection Well | Violations Noted | C. O. 2006-126 in compliance.Terrabyte repaired 2 tubing by digging 5 below grade, cutting bad tubing off and replaced with sleeve and welded together. Pumped annulus full of inhibitor and pressured up to 200 psi. Pressure held for 30 minutes with zero drop in pressure. Gave approval to inject brine in well. Rain, 60 degrees. |
1181234241 | 2007-06-07 | Salt Water Injection Well | No Violations | Well gauge on injection tubing is showing vacume and packer side is holding at 120 psi. No violations at this time. Sun, 75 degrees. |
1192193851 | 2007-10-12 | Salt Water Injection Well | No Violations | Tank battery and well have been reconstructed. Old tanks removed and new tanks placed in battery inside concrete dike. Spill prevention tubs and locks are installed on pickup lines. New paint on well head, tanks and building. Area is graded with gravel around facility. Clean operation. Cloudy, 50 degrees. |
1198250868 | 2007-12-21 | Salt Water Injection Well | No Violations | Well is on vacume. Two 100 barrel brine tanks in battery. Tank batterry is reconstructed and very clean. New paint on tanks and building. Drip containers are attached to end of tank lines. Cloudy, 35 degrees. |
1220i265 | 2002-9-27 0:00: | ER | No Violations | 1.00 |
1220i297 | 2002-10-22 0:00 | SW | No Violations | 1.00 |
1239219567 | 2009-03-04 | Salt Water Injection Well | No Violations | Well is idle due to cold weather. No violations. |
1253725357 | 2009-09-23 | Salt Water Injection Well | Violations Noted | Called by Rod Robison to advise me of an acid spill at injection facility. Acid and brine was stored in a 100 barrel tank at the injection tank battery. The acid deteriorated the nipple on bottom of tank and acid leaked in dike and thru dike near stream. No acid or brine entered stream. Brought in equipment and removed 4 yards of contaminated soil and stored in steel container. I advised them to remove concrete dike and replace with pit liner and earthen dike. Submit plan to UIC section. Showers, 70 degrees. |
1257421362 | 2009-11-05 | Salt Water Injection Well | No Violations | Contaminated soil has been removed and new soil replaced. Dike has been repaired. NOV in compliance. Cloudy, 40 degrees. |
1259157303 | 2009-11-25 | Salt Water Injection Well | No Violations | Called by Rod Robinson. Concrete dike is breaking down since acid spill. Company is removing tank battery and dike. Injection well is idle until battery is replaced. Rain, 45 degrees. |
1284730287 | 2010-09-17 | Salt Water Injection Well | Violations Noted | Injection well is idle. Tank battery has been removed and concrete dike remains on site. No response to verbal recommendations to put well in production or plug and abandon. Cloudy, 60 degrees. |
1288963935 | 2010-11-05 | Salt Water Injection Well | No Violations | Well remains idle. No response from company on compliance notice.ERP# 20. Called Chad Whited and left a message to address compliance notice. Well is shut in on 2 tubing. Tanks have been removed in battery. Rain, 40 degrees. |
1299475436 | 2007-08-21 | Salt Water Injection Well | No Violations | Quarterly inspection. Injection well head has been reconstructed with new fittings and pressure gauges. Tank battery has been reconstructed with 2-100 barrel holding tanks inside concrete containment wall. Storage building has been reconstructed with new material and door repaired. No violations. Rain, 70 degrees. |
1300378913 | 2011-03-17 | Salt Water Injection Well | No Violations | Injection well remains idle. All equipment has been removed. Well is shut in on tubing. Sun, 60 degrees. |
1321273014 | 2011-11-07 | Enhanced Recovery Project | No Violations | Shut in, no fittings. |
1331749759 | 2012-03-14 | Enhanced Recovery Project | No Violations | Inspect Well. Shut in. existing NOV. Requested info about well, and plug and abandon application. |
1341507920 | 2012-07-05 | Enhanced Recovery Project | No Violations | Inspect well. spoke with operator regarding Compliance Order. Operator will apply for plug permit and plug well when permit issued. Extended compliance to 8/31/2012. |
1346417152 | 2012-08-29 | Plug / Plug Back | No Violations | Contacted by operator. Plug injection well with cement through one inch tubing. |
1477367326 | 2012-06-06 | Enhanced Recovery Project | No Violations | Inspect Well. incapable of production. |
1642246479 | 2014-08-20 | Final Restoration | No Violations | The location has been finish graded and the concrete removed. There is native vegetation established at the well location. Final restoration is approved. |
1661164113 | 2003-06-17 | Salt Water Injection Well | No Violations | No violations at site. Cloudy 65 degrees. |
1873020661 | 2010-09-17 | Salt Water Injection Well | No Violations | FOLLOW UP TO NOV # 1284730287 Injection well is idle. Tank battery has been removed and concrete dike remains on site. No response to verbal recommendations to put well in production or plug and abandon. Cloudy, 60 degrees. Operator will purchase plug permit. |
206510166 | 2006-10-30 0:00 | SW | No Violations | 2.00 |
2114816481 | 2003-08-15 | Salt Water Injection Well | Violations Noted | Oil inside concrete dike has ran over and in secondary dike. Oil is contained. Called Richard Mount to advise. Heavy rains flooded dike. Sunny, 80 degrees. |
223051147 | 2010-9-17 0:00: | SW | No Violations | 1.00 |
26478763 | 2002-9-23 0:00: | SW | No Violations | 2.00 |
872994796 | 2006-11-29 0:00 | SW | No Violations | 1.00 |
iTOMK00001 | 1999-06-17 | Enhanced Recovery Project | No Violations | 1509.03 & 1501:9-5-1(E,F) PERMIT CONDITIONS |
iTOMK00001147878 | 1999-6-17 0:00: | ER | No Violations | |
UIC1122 | 1991-6-21 0:00: | ER | No Violations | |
UIC1209 | 1992-1-2 0:00:0 | ER | No Violations | |
UIC1397 | 1993-5-12 0:00: | ER | No Violations | |
UIC1398 | 1993-5-12 0:00: | ER | No Violations | |
UIC1399 | 1993-5-12 0:00: | ER | No Violations | |
UIC1422 | 1993-6-22 0:00: | ER | No Violations | |
UIC275 | 1987-8-10 0:00: | ER | No Violations | |
UIC276 | 1987-8-10 0:00: | ER | No Violations | |
UIC277 | 1987-8-10 0:00: | ER | No Violations | |
UIC278 | 1987-8-10 0:00: | ER | No Violations | |
UIC279 | 1987-8-10 0:00: | ER | No Violations | |
UIC825 | 1989-12-19 0:00 | ER | No Violations | |
UIC826 | 1989-12-19 0:00 | ER | No Violations | |
UIC889 | 1990-4-30 0:00: | ER | No Violations | |
UIC890 | 1990-4-30 0:00: | ER | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
001220i265 | US-OH-105938 | 2002-09-27 | Mechanical failure/contamination | |
0206510166 | US-OH-121046 | 2006-10-30 | Pollution/Contamination | |
0206510166 | US-OH-121047 | 2006-10-30 | Contamination at surface facility (permit after 6-1-82) | |
0206510166 | US-OH-121048 | 2006-10-30 | Pits not liquid tight/Improper construction or use | |
1156357047 | US-OH-104116 | 2006-08-23 | Failure to conduct or pass mech. integrity test | |
1156357047 | US-OH-104117 | 2006-08-23 | Mechanical failure/contamination | |
1156357047 | US-OH-104118 | 2006-08-23 | Mechanical failure/contamination | |
1164828023 | US-OH-104380 | 2006-08-23 | Mechanical failure/contamination | |
1253725357 | US-OH-106843 | 2009-09-23 | Contamination at surface facility (permit after 6-1-82) | |
1284730287 | US-OH-107908 | 2010-09-17 | Failure to plug | |
1284730287 | US-OH-107909 | 2010-09-17 | Defective casing, leaking well | |
2114816481 | US-OH-121637 | 2003-08-15 | Pits not liquid tight/Improper construction or use |
For data sources see[9]